• Title/Summary/Keyword: Two phase flow accelerated corrosion

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A Two-Phase Flow Accelerated Corrosion Study on Water Wall Tube of Coal-Fired Boiler According to Flexible Operation (유연운전에 따른 석탄화력보일러 수계통 튜브에서의 이상 유동가속부식(Two-Phase Flow Accelerated Corrosion) 고찰)

  • Sang-Ho Kim;Seung-Min Lee;Jae-Hong Lee
    • Corrosion Science and Technology
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    • v.23 no.3
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    • pp.246-254
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    • 2024
  • Recently, coal-fired power plants are experiencing many problems that they have never experienced before due to an increase in flexible operation. In particular, a two-phase flow accelerated corrosion on water wall tubes in a boiler has not been detected overseas or domestically. There is no response plan to deal with such corrosion problem either. However, oxide film damage and tube material corrosion due to a two-phase flow accelerated corrosion are being discovered on water wall boiler tubes of domestic coal-fired power plants recently. If this situation is severe, it can cause enormous damage such as tube rupture. Therefore, in this paper, in order to prepare a response plan for a two-phase flow accelerated corrosion on water wall tubes in the future, differences between a two-phase flow accelerated corrosion and a single-phase flow accelerated corrosion were investigated and an example of discovery of a two-phase flow accelerated corrosion on water wall tubes was presented.

Analysis of Wall-Thinning Effects Caused by Power Uprates in the Secondary System of a Nuclear Power Plant (원전 2차계통의 출력증강 운전에 따른 배관감육 영향 분석)

  • Yun, Hun;Hwang, Kyeongmo;Lee, Hyoseoung;Moon, Seung-Jae
    • Corrosion Science and Technology
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    • v.15 no.3
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    • pp.135-140
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    • 2016
  • Piping and equipment are degraded by flow-accelerated corrosion (FAC) in nuclear power plants. FAC causes numerous problems and nuclear utilities maintain programs to control FAC. The key parameters influencing FAC are hydrodynamic conditions, water chemistry, and effect of materials. Recently, a nuclear utility has planned slight power uprates in Korea. Operating conditions need to be changed in the secondary system according to power uprates. This study analyzed the effect of wall-thinning caused by power uprates. The change of operation data in the secondary cycle is reviewed, and wall-thinning rates are analyzed in the main lines. As a result, two phase (mixture of water and steam) lines have a greater impact than a water line under power uprate conditions. Also, the quality of steam is the most important factor for FAC in two phase lines.

Dynamic Boric Acid Corrosion of Low Alloy Steel for Reactor Pressure Vessel of PWR using Mockup Test (가압형 경수로 압력용기 재료인 저합금강의 동적 붕산 부식 실증 연구)

  • Kim, Sung-Woo;Kim, Hong-Pyo;Hwang, Seong-Sik
    • Corrosion Science and Technology
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    • v.12 no.2
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    • pp.85-92
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    • 2013
  • This work is concerned with an evaluation of dynamic boric acid corrosion (BAC) of low alloy steel for reactor pressure vessel of a pressurized water reactor (PWR). Mockup test method was newly established to investigate dynamic BAC of the low alloy steel under various conditions simulating a primary water leakage incident. The average corrosion rate was measured from the weight loss of the low alloy steel specimen, and the maximum corrosion rate was obtained by the surface profilometry after the mockup test. The corrosion rates increased with the rise of the leakage rate of the primary water containing boric acid, and the presence of oxygen dissolved in the primary water also accelerated the corrosion. From the specimen surface analysis, it was found that typical flow-accelerated corrosion and jet-impingement occurred under two-phase fluid of water droplet and steam environment. The maximum corrosion rate was determined as 5.97 mm/year at the leakage rate of 20 cc/min of the primary water with a saturated content of oxygen within the range of experimental condition of this work.

Design Modification and Correlation Verification between Reattachment Flow of Dispersed Jet and Local Thinning of Feedwater Heater (충돌로 인해 분산된 2상 제트스팀의 재부착 현상과 국부 감육 상관관계 규명 및 설계개선에 관한 연구)

  • Kim, Hyung-Joon;Kim, Kyung-Hoon;Hwang, Kyeong-Mo
    • Korean Journal of Air-Conditioning and Refrigeration Engineering
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    • v.21 no.9
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    • pp.483-495
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    • 2009
  • Feedwater heaters of many nuclear power plants have recently experienced severe wall thinning damange, which will increase as operating time progresses. Several nuclear power plants in Korea have experienced wall thinning damage in the area around the impingement baffle-installed downstream of the high pressure turbine extraction stream line-inside number 5A and 5B feedwater heaters. At that point, the extracted steam from the high pressure turbine is two phase fluid at high temperature, high pressure, and high speed. Since it flows in reverse direction after impinging the impingement baffle, the shell wall of the number 5 high pressure feedwater heater may be affected by flow-accelerated corrosion. This paper describes operation of experience and numerical analysis composed similar condition with real high pressure feedwater heater. This study applied squared, curved and new type impingement baffle plates to feedwater heater same as previous study. In addition, it shows difference of pressure distribution and value between single phase and two phase based on experience and numerical analysis.

A Study on the Relief of Shell Wall Thinning of High pressure Feedwater Heater (고압형 급수가열기 동체 감육 완화에 관한 연구)

  • Kim, Hyung-Joon;Park, Sang-Hoon;Seo, Hyuk-Ki;Kim, Kyung-Hoon;Hwang, Kyung-Mo
    • Proceedings of the KSME Conference
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    • 2008.11b
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    • pp.2664-2669
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    • 2008
  • Feedwater heaters of many nuclear power plants have recently experienced severe wall thinning damange, which will increase as operating time progresses. Several nuclear power plants in Korea have experienced wall thinning damage in the area around the impingement baffle-installed downstream of the high pressure turbine extraction stream line- inside number 5A and 5B feedwater heaters. At that point, the extracted steam from the high pressure turbine is two phase fluid at high temperature, high pressure, and high speed. Since it flows in reverse direction after impinging the impingement baffle, the shell wall of the number 5 high pressure feedwater heater may be affected by flow-accelerated corrosion. This paper describes operation of experience and numerical analysis composed similar condition with real high pressure feedwater heater. This study applied squared, curved and new type impingement baffle plates to feedwater heater same as previous study. In addition, it shows difference of pressure distribution and value between single phase and two phase based on experience and numerical analysis.

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A Flow Analysis in the surroundings of the Impingement Baffle of the Extracting Nozzle for Shell Wall Thinning of a Feedwater Heater (추기노즐 충격판 주변의 급수가열기 동체 감육에 대한 유동해석)

  • Jung, Sun-Hee;Kim, Kyung-Hoon
    • Proceedings of the KSME Conference
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    • 2007.05b
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    • pp.2977-2982
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    • 2007
  • Feedwater heaters of many nuclear power plants have recently experienced severe wall thinning damage, which will increase as operating time progresses. Several nuclear power plants in Korea have experienced wall thinning damage in the area around the impingement baffle - installed downstream of the high pressure turbine extraction steam line - inside number 5A and 5B feedwater heaters. At that point, the extracted steam from the high pressure turbine is two phase fluid at high temperature, high pressure, and high speed. Since it flows in reverse direction after impinging the impingement baffle, the shell wall of the number 5 high pressure feedwater heater may be affected by flow-accelerated corrosion. This paper describes the comparisons between the numerical analysis results using the FLUENT code and the down scale experimental data which effect on disclosing of the shell wall thinning of the high pressure feedwater heaters by porous plate.

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A Study on the Shell Wall Thinning by Flow Acceleration Corrosion and Mitigation Plan and Design Modification of a Feedwater Heater Impingement Baffle (유동가속부식으로 인한 급수가열기 동체 감육현상 규명과 완화 방안 및 충격판 설계개선에 관한 연구)

  • Kim, Kyung-Hoon;Hwang, Kyeong-Mo;Kim, In-Tae
    • Journal of ILASS-Korea
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    • v.15 no.2
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    • pp.83-93
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    • 2010
  • Feedwater heaters of many nuclear power plants have recently experienced severe wall thinning damage, which will increase as operating time progresses. Several nuclear power plants in Korea have experienced wall thinning damage in the area around the impingement baffle inside feedwater heater installed downstream of the turbine extraction stream line. At that point, the extract steam from the turbine is two phase fluid at high temperature, high pressure, and high speed. Since it flows to reverse direction after impinging the impingement baffle, the shell wall of feedwater heaters may be affected by flow-accelerated corrosion. In this paper, to compare degree of shell wall thinning mitigation rate to squared type with mitigation rate of other type baffle plate, four different types of impingement baffle plate-squared, curved, mitigating type and multi-hole type-applied inside the shell. With these comparison data, this paper describes operation of experiments and numerical analysis which is composed similar condition with real feed water heater. And flow visualization is operated for verification of experiments and numerical analysis. In conclusion, this study shows that mitigating type and multi-hole type baffle plate are more effective than other baffle plate about prevention of pressure concentration and pressure value decrease.

A Study on the Fluid Mixing Analysis for Proving Shell Wall Thinning of a Feedwater Heater (급수가열기 동체 감육 현상 규명을 위한 유동해석 연구)

  • Shin, Min-Ho;Hwang, Kyeong-Mo;Kim, Kyung-Hoon
    • Proceedings of the KSME Conference
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    • 2004.04a
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    • pp.2017-2022
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    • 2004
  • There are multistage preheaters in the power generation plan to improve the thermal efficiency of the plant and to prevent the components from the thermal shock. The energy source of these heaters comes from the extracted two phase fluid of working system. These two-phase fluid can cause the so-called Flow Accelerated Corrosion(FAC) in the extracting piping and the bubble plate of the heater for example, in case of point Beach Nuclear Power Plant and in the Wolsung Nuclear Power Plant. The FAC is due to the mass transport of the thin oxide layer by the convection. FAC is dependent on many parameters such as the operation temperature, void fraction, the fluid velocity and pH of fluid and so on. Therefore, in this paper velocity was calculated by FLUENT code in order to find out the root cause of the wall thinning of the feedwater heaters. It also includeed in the fluid mixing analysis model are around the number 5A feedwater heater shell including the extraction pipeline. To identify the relation between the local velocities and wall thinning, the local velocities according to the analysis results were compared with distribution of the shell wall thicknes by ultrasonic test.

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A Stress Analysis of Feeedwater Heater Shell in Nuclear Power Plant (원전 급수가열기 동체 응력 해석)

  • Song, Seok-Yoon;Kim, Hyung-Nam
    • Transactions of the Korean Society of Pressure Vessels and Piping
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    • v.11 no.1
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    • pp.1-11
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    • 2015
  • Feedwater Heaters are important components in a nuclear power plant. As the age of heater increases, the maintenance cost required for continuous operation also increases. Most heaters have the carbon steel shells, tube support plates and flow baffles. The carbon steel is susceptible to flow-accelerated corrosion. This is especially true if the flow has a two-phase mixture of steam and condensate. The wall thinning around the wet steam entrance area of the shell is inevitable during some long term operation. The structural integrity of the feedwater heater shell affects the safe operation of the nuclear power plant. Therefore, it is needed for the thinned shell to be repaired. The maintenance method for preventing failure of the shell should be determined by investigating various factors including the stress distribution of thinned area. The stress analysis of the shell including the steam entrance region is studied in this paper. The results of thinned shell is compared with that of intact shell.

A Study on the Wall Thinning Range according to modified Extraction Nozzle Design in High Pressure Feedwater Heater (고압 급수가열기 추기노즐 설계변경에 따른 감육 범위 연구)

  • Park, Sang-Hoon;Yoo, Il-Gon;Kim, Kyung-Hoon;Hwang, Kyeong-Mo
    • Proceedings of the SAREK Conference
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    • 2009.06a
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    • pp.847-852
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    • 2009
  • Feedwater heaters of many nuclear power plants have recently experienced severe wall thinning damange, which will increase as operating time progresses. Several nuclear power plants in Korea have experienced wall thinning damage in the area around the impingement baffle inside feed-water heater installed downstream of the turbine extraction stream line. At that point, the extract steam from the turbine is two phase fluid at high temperature, high pressure, and high speed. Since it flows to reverse direction after impinging the impingement baffle, the shell wall of feedwater heaters may be affected by flow-accelerated corrosion. In this paper, to compare wall thinning range according to change entrance nozzle diameter and position with reference numerical analysis model's wall thinning range, various numerical analysis models applied. In case of changing diameter, four different diameter is applied. And a side of nozzle position, two different position-vertical type and parallel type-is applied. And then this paper describes operation of numerical analysis which is composed similar condition with real feed water heater. In conclusion, this study shows effective design for shall wall thinning by changing nozzle diameter and position.

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