• Title/Summary/Keyword: KUH-1

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A Study on Quality Improvement of Electrical Master Box for KUH (한국형 기동헬기 전원분배 제어장치의 품질 향상에 관한 연구)

  • Kim, Young Mok;Jun, Byung Kyu;Jeong, Sang Gyu;Lee, Joo Hyung
    • Journal of the Korean Society for Aeronautical & Space Sciences
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    • v.45 no.1
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    • pp.71-78
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    • 2017
  • The electrical power system of Korean Utility Helicopter(KUH) is designed as a dual control system to enhance the system safety of aircraft and each system is installed separately at left and right of the aircraft. The system is composed of 2 AC generators, 1 APU generator, 2 Transformer Rectifier Units(TRU), AC/DC Electrical Master Box(AC/DC EMB). The AC/DC EMB, consists of 2 AC EMB and 2 DC EMB, is essential equipment which supply and distribute electric power to the aviation electronics and electrical equipment of KUH. There were defects caused by internal short circuit in AC EMB during the first production phase of the KUH. This paper describes the analysis of the defects, troubleshooting process, root cause, and the solution by design change.

A Study on Winter Season Usability Performance Improvement of Flapper Valve for KUH-1 (한국형 기동헬기 동계운용능력 향상을 위한 플래퍼밸브 개선연구)

  • Choi, Jae Hyung;Chang, In ki;Shim, Dai Sung;Ahn, Jeong Min
    • Journal of the Korean Society for Aeronautical & Space Sciences
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    • v.44 no.1
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    • pp.49-56
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    • 2016
  • Flapper Valve of Korean Utility Helicopter(KUH-1) is an essential equipment in Environmental Control System(ECS) for pilot to perform flight mission. It provides pilots and crews with heating, ventilating and air conditioning. It has function of maintaining room temperature to sustain operational capability for pilot and crew. This paper summarizes pilot comments in flight test which are classified by cause of occurrence and the troubleshooting process about each comment. It also describes design improvements which was derived from troubleshooting and suggests verification results of flight test at low temperature.

An Improvement Study on Brake System for KUH-1 (한국형 기동헬기의 제동장치 개선에 관한 연구)

  • Choi, Jae Hyung;Lim, Hyun-Gyu;Yoon, Jong Jin;Kang, Deuk Soo
    • Journal of the Korean Society for Aeronautical & Space Sciences
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    • v.45 no.4
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    • pp.292-299
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    • 2017
  • The KUH-1's Wheel Brake Assembly which is Brake System is an essential component to perform flight mission for pilot. It has function of taxing, differential braking and parking to sustain landing capability. However, the skid and abrasion of tire were occurred in mass-produce operation. Also, if it is occurred on the ground, the flight can not be performed. In this case, the defect is a major cause of the decrease in the operation rate of aircraft. In this paper, the cause of the defect in flight was identified and the failure process was organized. Also, it describes design improvements which was derived from troubleshooting and suggests verification results of flight test.

A study on improvement of painting quality through a de-painting phenomenon of KUH-1 tail blade (한국형 기동헬기 꼬리 날개 디페인팅 현상을 통한 도장 품질 향상에 관한 연구)

  • Chang, In-Ki;Kim, Young-Jin;Seo, Hyun-Soo;Jeon, Boo-Il
    • Journal of Korean Society for Quality Management
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    • v.42 no.3
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    • pp.325-338
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    • 2014
  • Purpose: The purpose of this study was to explain de-painting phenomenon of KUH-1 tail blade and to propose useful solution of it by test. The proposed solution was evaluated by real flight, and then it applied to mass product to improve the paint qual ity of KUH-1 tail blade. Methods: This study investigated an adhesive ability of primer following surface sanding condition. The cross cut and scratch test were conducted to evaluate the adhesive strength. And the water flow test was designed to simulate a real flight condition under rain. Through water flow test, an optimal condition of tail blade to prevent a de-painting phenomenon was deduced. Finally, the improvement method was evaluated by real flight under rain. Results: The results of this study are as follows; The sequential polishing was most excellent method in primer painting quality. The results of test including cross cut, scratch and water flow showed that MIL-DTL-53039 paint with epoxy primer has excellent adhesive ability. To proof the effect of improvement, a real flight during a rain condition was conducted. Finally, the comparison between original and improved configuration was conducted. Conclusion: The painting quality of KUH-1 tail blade was improved through deriving an optimal painting condition. In detail, a condition of optimal sanding and a sort of primer and paint was showed. Finally, the reliability of tail blade was guaranteed through improving the quality of painting.

Development of Nitrogen Charging Trailer for Aircraft Improved Operability (운용성을 개선한 항공기용 질소충전트레일러 국산화 개발)

  • Park, Hyo-Jin
    • Journal of the Korean Society for Aeronautical & Space Sciences
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    • v.46 no.6
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    • pp.513-518
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    • 2018
  • Nitrogen charging trailer applied to KUH-1 is a device to charge Nitrogen in main front wheel buffer, tail bumper buffer, brake accumulator and tire of aircraft. As the name suggests, it is a device that has mobility along with nitrogen charging. Originally supplied by Tronair in the United States, it was imported from Korea, and the locally developed product not only satisfies the performance of the existing product, but also designed to be easier than the product introduced in the operation. It was selected as the joint investment project of the 15th civilian government building, and development needs analysis and test evaluation were carried out under the support of development and management of Korea Aerospace Industries and Defense Agency for Technology and Quality.

Design of KUH Main Rotor Small-scaled Blade (KUH 주로터 축소 블레이드 설계)

  • Kim, Do-Hyung;Kim, Seung-Ho;Han, Jung-Ho
    • Aerospace Engineering and Technology
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    • v.8 no.1
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    • pp.32-41
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    • 2009
  • In this study, scale-down design of full-scale Korean Utility Helicopter (KUH) main rotor blade has been investigated. The scaled model system were designed for the measurement of aerodynamic performance, tip vortex and noise source. For the purpose of considering the same aerodynamic loads, the Mach-scale method has been applied. The Mach-scaled model has the same tip Mach number, and it also has the same normalized frequencies. That is, the Mach-scaled model is analogous to full-scale model in the view point of aerodynamics and structural dynamics. Aerodynamic scale-down process could be completed just by adjusting scaling dimensions and increasing rotating speed. In the field of structural dynamics, design process could be finished by confirming the rotating frequencies of the designed blade with the stiffness and inertial properties distributions produced by sectional design. In this study, small-scaled blade sectional design were performed by applying domestic composite prepregs and structural dynamic characteristics of designed model has been investigated.

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An Overview of Flight Test Planning and Test Results for the Development of Korean Utility Helicopter (한국형 기동헬기 개발을 위한 비행시험 계획 및 시험결과 개요)

  • Kwon, Hyuk-Jun;Park, Jaeyoung
    • Journal of the Korea Institute of Military Science and Technology
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    • v.16 no.3
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    • pp.268-276
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    • 2013
  • The objective of this paper is to give a general understanding for the development flight test of Korean Utility Helicopter(KUH). This paper contains the contents of detailed flight test plan, the type of flight test, an introduction to main flight test area, and the overview of flight test results. At the beginning, more than 8,500 test points were identified for airworthiness certification to show the compliance for the KUH development requirements. However, the number of flight test points were optimized to 7,800 at the end. To accomplish the test objectives, about 860 flight test sorties had been performed, and more than 1,000 test sorties were consumed for trouble shooting. This paper also describes some major issues faced during development flight test phase.

Design of a Double-Faced Window Printed Antenna for Aircraft Applications (항공기용 양면 인쇄형 글래스 안테나 설계)

  • Byun, Gang-Il;Han, Wone-Keun;Choo, Ho-Sung
    • The Journal of Korean Institute of Electromagnetic Engineering and Science
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    • v.22 no.2
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    • pp.131-139
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    • 2011
  • In this paper, we propose a double-faced window printed antenna for aircraft applications. The proposed antenna structure consists of a feeding line and a multi-loop radiator located on different sides of the window to use the limited given-area effectively. The proposed antenna is optimized by the genetic algorithm in conjunction with the FEKO EM simulator. The optimized antenna is built and installed on a 1/10 sized KUH-Surion mock-up and antenna performances such as the reflection coefficient and the radiation patterns are measured. The optimized antenna shows a half power matching bandwidth of about 33 % at 60 MHz and an average bore-sight gain of about -3.49 dBi. To verify the reception capability of the optimized antenna, we simulated the received power according to a flight scenario. The result confirms that the optimized antenna shows a minimum received power level above -60 dBm at a range of 200 km, which is similar to the pole antenna that is currently used as a FM voice antenna for KUH-Surion.

Purification and Characterization of Antistaphylococcal Substance from Pseudomonas sp. KUH-001

  • Hwang, Se-Young;Lee, So-Hee;Song, Kook-Jong;Kim, Yong-Pil;Kawahara, Kazuyoshi
    • Journal of Microbiology and Biotechnology
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    • v.8 no.2
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    • pp.111-118
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    • 1998
  • A bacterium producing unique antistaphylococcal substance (ASS) was isolated from soil samples. The isolated strain KUH-001 was identified to belong to Pseudomonas species from the characteristic properties of its fluorescence and cellular 3-hydroxy fatty acid composition, etc. The ASS component was purified by procedures employing activated carbon adsorption, column chromatography with silica gel, preparative TLC and HPLC. This compound could also be purified mainly by repeating of trituration and precipitation with chilled ether. Purified ASS with a m.p. value of $140~142^{\circ}C$ showed marked stability at high temperature (at $121^{\circ}C$ for 10 min) and extreme pHs (in 1N HC1 and 1N NaOH for 1 day) without significant loss of antibiotic activity. From spectral data of UV, IR, NMR, and FAB-MS, the compound was elucidated as 2-heptyl-4-hydroxyquinoline N-oxide (HHQO). Under the conditions employed, HHQO exhibited a narrow antimicrobial spectrum. active particularly against Staphylococcus aureus including the methicillin resistant strain. Moreover, it did not induce resistance, and besides, interacted synergistically with certain antibiotics such as vancomycin or erythromycin.

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