• Title/Summary/Keyword: 2D/3D switch

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A 900 MHz Zero-IF RF Transceiver for IEEE 802.15.4g SUN OFDM Systems

  • Kim, Changwan;Lee, Seungsik;Choi, Sangsung
    • ETRI Journal
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    • v.36 no.3
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    • pp.352-360
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    • 2014
  • This paper presents a 900 MHz zero-IF RF transceiver for IEEE 802.15.4g Smart Utility Networks OFDM systems. The proposed RF transceiver comprises an RF front end, a Tx baseband analog circuit, an Rx baseband analog circuit, and a ${\Delta}{\Sigma}$ fractional-N frequency synthesizer. In the RF front end, re-use of a matching network reduces the chip size of the RF transceiver. Since a T/Rx switch is implemented only at the input of the low noise amplifier, the driver amplifier can deliver its output power to an antenna without any signal loss; thus, leading to a low dc power consumption. The proposed current-driven passive mixer in Rx and voltage-mode passive mixer in Tx can mitigate the IQ crosstalk problem, while maintaining 50% duty-cycle in local oscillator clocks. The overall Rx-baseband circuits can provide a voltage gain of 70 dB with a 1 dB gain control step. The proposed RF transceiver is implemented in a $0.18{\mu}$ CMOS technology and consumes 37 mA in Tx mode and 38 mA in Rx mode from a 1.8 V supply voltage. The fabricated chip shows a Tx average power of -2 dBm, a sensitivity level of -103 dBm at 100 Kbps with PER < 1%, an Rx input $P_{1dB}$ of -11 dBm, and an Rx input IP3 of -2.3 dBm.

Estimation of Individual Vehicle Speed Using Single Sensor Configurations (단일 센서(Single Sensor)를 활용한 차량속도 추정에 관한 연구)

  • Oh, Ju-Sam;Kim, Jong-Hoon
    • KSCE Journal of Civil and Environmental Engineering Research
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    • v.26 no.3D
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    • pp.461-467
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    • 2006
  • To detect individual vehicular speed, double loop detection technique has been widely used. This paper investigates four methodologies to measure individual speed using only a single loop sensor in a traveling lane. Two methods developed earlier include estimating the speed by means of (Case 1) the slop of inductance wave form generated by the sensor and (Case 2) the average vehicle lengths. Two other methods are newly developed through this study, which are estimations by measuring (Case 3) the mean of wheelbases using the sensor installed traversal to the traveling lane and (Case 4) the mean of wheel tracks by the sensor installed diagonally to the traveling lane. These four methodologies were field-tested and their accuracy of speed output was compared statistically. This study used Equality Coefficient and Mean Absolute Percentage Error for the assessment. It was found that the method (Case 1) was best accurate, followed by method (Case 4), (Case 2), and (Case 3).

Interaction of Ruthenium(II)[(1,10-phenanthroline)2benzodipyrido[3,2-a:2',3'-c]-phenazine]2+ with Single Stranded Poly(dA) and Poly(dT): Turning off the Light Switch

  • Lee, Jeong-Mi;Choi, Ji-Yoon;Kim, Jong-Moon;Lee, Sang-Yong;Lee, Hyo-Sun;Kim, Seog-K.;Cho, Tae-Sub
    • Bulletin of the Korean Chemical Society
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    • v.28 no.6
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    • pp.965-969
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    • 2007
  • The spectral properties, namely the circular dichroism, electric absorption and luminescence properties, of Λ- and Δ-[Ru(II)(1,10-phenanthroline)2benzodipyrido[b:3,2-h:2',3'-j]phenazine]2+ ([Ru(phen)2BDPPZ]2+) in the presence and absence of single stranded poly(dA) and poly(dT) were compared in this work. In the presence of single stranded DNAs, hypochromism in the absorption spectrum and significant changes in the circular dichroism spectrum in the ligand absorption band were apparent, indicating the strong interaction of the [Ru(phen)2BDPPZ]2+ complex with the single stranded DNAs. The luminescence intensity of the Ru(II) complex decreased stoichiometrically with increasing concentrations of the single stranded DNAs. All of these spectral changes were independent of the configuration of the Ru(II) complex and the nature of the DNA bases. Therefore, it is conceivable that both enantiomers of the [Ru(phen)2BDPPZ]2+ complex interact electrostatically with the negatively charged phosphate groups of DNA. However, the spectral properties of [Ru(II)(1,10-phenanthroline)3]2+ were not altered even in the presence of single stranded DNAs. Therefore, the size of the ligand involved in the interaction of the metal complex with the phosphate group of DNA may play an important role, even when the nature of the interaction is electrostatic.

A 900MHz CMOS RF Power Amplifier with Digitally Controllable Output Power (Digital 방식으로 출력 전력을 조절할 수 있는 900MHz CMOS RF 전력 증폭기)

  • 윤진한;박수양;손상희
    • Journal of the Korean Institute of Electrical and Electronic Material Engineers
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    • v.17 no.2
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    • pp.162-170
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    • 2004
  • A 900MHz CMOS RF power amplifier with digitally controllable output power has been proposed and designed with 0.6${\mu}{\textrm}{m}$ standard CMOS technology. The designed power amplifier was composed of digitally controllable switch mode pre-amplifiers with an integrated 4nH spiral inductor load and class-C output stage. Especially, to compensate the 1ow Q of integrated spiral inductor, cascode amplifier with a Q-enhancement circuit is used. It has been shown that the proposed power control technique allows the output power to change from almost 3dBm to 13.5dBm. And it has a maximum PAE(Power Added Efficiency) of almost 55% at 900MHz operating frequency and 3V power supply voltage.

Operative Treatment of Congenitally Corrected Transposition of the Great Arteries(CCTGA) (교정형 대혈관 전위증의 수술적 치료)

  • 이정렬;조광리;김용진;노준량;서결필
    • Journal of Chest Surgery
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    • v.32 no.7
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    • pp.621-627
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    • 1999
  • Background: Sixty five cases with congenitally corrected transposition of the great arteries (CCTGA) indicated for biventricular repair were operated on between 1984 and september 1998. Comparison between the results of the conventional(classic) connection(LV-PA) and the anatomic repair was done. Material and Method: Retrospective review was carried out based on the medical records of the patients. Operative procedures, complications and the long-term results accoding to the combining anomalies were analysed. Result: Mean age was 5.5$\pm$4.8 years(range, 2 months to 18years). Thirty nine were male and 26 were female. Situs solitus {S,L,L} was in 53 and situs inversus{I,D,D} in 12. There was no left ventricular outflow tract obstruction(LVOTO) in 13(20%) cases. The LVOTO was resulted from pulmonary stenosis(PS) in 26(40%)patients and from pulmonary atresia(PA) in 26(40%) patients. Twenty-five(38.5%) patients had tricuspid valve regurgitation(TR) greater than the mild degree that was present preoperatively. Twenty two patients previously underwent 24 systemic- pulmonary shunts previously. In the 13 patients without LVOTO, 7 simple closure of VSD or ASD, 3 tricuspid valve replacements(TVR), and 3 anatomic corrections(3 double switch operations: 1 Senning+ Rastelli, 1 Senning+REV-type, and 1 Senning+Arterial switch opera tion) were performed. As to the 26 patients with CCTGA+VSD or ASD+LVOTO(PS), 24 classic repairs and 2 double switch operations(1 Senning+Rastelli, 1 Mustard+REV-type) were done. In the 26 cases with CCTGA+VSD+LVOTO(PA), 19 classic repairs(18 Rastelli, 1 REV-type), and 7 double switch operations(7 Senning+Rastelli) were done. The degree of tricuspid regurgitation increased during the follow-up periods from 1.3$\pm$1.4 to 2.2$\pm$1.0 in the classic repair group(p<0.05), but not in the double switch group. Two patients had complete AV block preoperatively, and additional 7(10.8%) had newly developed complete AV block after the operation. Other complications were recurrent LVOTO(10), thromboembolism(4), persistent chest tube drainage over 2 weeks(4), chylothorax(3), bleeding(3), acute renal failure(2), and mediastinitis(2). Mean follow-up was 54$\pm$49 months(0-177 months). Thirteen patients died after the operation(operative mortality rate: 20.0%(13/65)), and there were 3 additional deaths during the follow up period(overall mortality: 24.6%(16/65)). The operative mortality in patients underwent anatomic repair was 33.3%(4/12). The actuarial survival rates at 1, 5, and 10 years were 75.0$\pm$5.6%, 75.0$\pm$5.6%, and 69.2$\pm$7.6%. Common causes of death were low cardiac output syndrome(8) and heart failure from TR(5). Conclusion: Although our study could not demonstrate the superiority of each classic or anatomic repair, we found that the anatomic repair has a merit of preventing the deterioration of tricuspid valve regurgitations. Meticulous selection of the patients and longer follow-up terms are mandatory to establish the selective advantages of both strategies.

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Design of Antenna for Beam Scanning for Dual-Band base station (이중대역 기지국용 빔 스캔 안테나 설계)

  • Ko Jin-Hyun;Jang Jae-Su;Ha Jae-Kwon;Park Sae-Houn
    • Proceedings of the Korean Institute of Information and Commucation Sciences Conference
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    • 2006.05a
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    • pp.632-636
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    • 2006
  • It is needed to use the beam scanning to control the cell coverage of the base station considering operation conditions, season, time period, radiation character and mobility of customers and vehicles for varied wireless communication service and quality improvement. This paper proposes a mobile antenna system which can obtain the characteristics of the beam scanning by controlling the directivity depending on the operation condition. Radiation block is made of 2 sub-array of $1\times3$ patched antennas for ITS of 5.8GHZ bandwidth with the gain of 13dBi, and of 2 sub-array of single patched antenna for WiBro of 2.3GHZ bandwidth with the gain of 12dBi. RF module is made of a switch, an amplifier, a PAD, a 3-Bit phase shifter, and a power divider. The system is able to control the beam tilting with electronic methode by using 3-bit phase shifter$(45^{\circ},\;90^{\circ},\;180^{\circ})$.

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MyWorkspace: VR Platform with an Immersive User Interface (MyWorkspace: 몰입형 사용자 인터페이스를 이용한 가상현실 플랫폼)

  • Yoon, Jong-Won;Hong, Jin-Hyuk;Cho, Sung-Bae
    • 한국HCI학회:학술대회논문집
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    • 2009.02a
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    • pp.52-55
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    • 2009
  • With the recent development of virtual reality, it has been actively investigated to develop user interfaces for immersive interaction. Immersive user interfaces improve the efficiency and the capability of information processing in the virtual environment providing various services, and provide effective interaction in the field of ubiquitous and mobile computing. In this paper, we propose an virtual reality platform "My Workspace" which renders an 3D virtual workspace by using an immersive user interface. We develop an interface that integrates an optical see-through head-mounted display, a Wii remote controller, and a helmet with infrared LEDs. It estimates the user's gaze direction in terms of horizontal and vertical angles based on the model of head movements. My Workspace expands the current 2D workspace based on monitors into the layered 3D workspace, and renders a part of 3D virtual workspace corresponding to the gaze direction. The user can arrange various tasks on the virtual workspace and switch each task by moving his head. In this paper, we will also verify the performance of the immersive user interface as well as its usefulness with the usability test.

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Inductor-less 6~18 GHz 7-Bit 28 dB Variable Attenuator Using 0.18 μm CMOS Technology (0.18 μm CMOS 기반 인덕터를 사용하지 않는 6~18 GHz 7-Bit 28 dB 가변 신호 감쇠기)

  • Na, Yun-Sik;Lee, Sanghoon;Kim, Jaeduk;Lee, Wangyoung;Lee, Changhoon;Lee, Sungho;Seo, Munkyo;Lee, Sung Chul
    • The Journal of Korean Institute of Electromagnetic Engineering and Science
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    • v.27 no.1
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    • pp.60-68
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    • 2016
  • This paper presents a 6~18 GHz 7-bit digital-controlled attenuator. The proposed attenuator is based on switched-T architecture, but no inductor is used for minimum chip size. The designed attenuator was fabricated using $0.18{\mu}m$ CMOS process, and characterized using on-wafer testing setup. The resolution(minimum attenuation step) and the maximum attenuation range of the attenuator were measured to be 0.22 dB and 28 dB, respectively. The measured RMS attenuation error and the RMS phase error for 6~18 GHz were less than 0.26 dB and $3.2^{\circ}$, respectively. The reference state insertion loss was less than 12.4 dB at 6~18 GHz. The measured input and output return losses were better than 9.4 dB over all frequencies and attenuation states. The chip size is $0.11mm^2$ excluding pads.

1.8-GHz Six-Port-Based Impedance Modulator Using CMOS Technology (CMOS 공정을 이용한 1.8 GHz 6-포트 기반의 임피던스 변조기)

  • Kim, Jinhyun;Kim, Jeong-Geun
    • The Journal of Korean Institute of Electromagnetic Engineering and Science
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    • v.29 no.5
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    • pp.383-388
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    • 2018
  • This paper presents a 1.8 GHz six-port-based impedance modulator using CMOS technology, which can select an arbitrary load impedance with switch control. The proposed 1.8-GHz impedance modulator comprises a Wilkinson power divider, three quadrature hybrid couplers, and four SP3T switches for each load impedance selection. The measured insertion loss of -13 dB and the input/output return losses of >10 dB are achieved in the range of 1.4~2.2 GHz. The low drop output regulator for a stable 3.3 V DC power and the serial peripheral interface(SPI) for an easy digital control are integrated. The chip size, including the pads, is $1.7{\times}1.8mm^2$.

Design of the Rain Sensor using a Coaxial Cavity Resonator (동축 공동 공진기를 이용한 물방울 감지 센서 설계에 관한 연구)

  • Lee, Yun-Min;Kim, Jin-Kook
    • The Journal of the Institute of Internet, Broadcasting and Communication
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    • v.18 no.5
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    • pp.223-228
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    • 2018
  • In this paper the water sensor using a coaxial cavity resonator is designed and manufactured. The water sensor which can sense water drop linearly has been constructed with voltage controlled oscillator(VCO), coaxial cavity resonator, RF switch, RF detector, A/D converter, DAC and micro controller. The operating frequency range of the designed water sensor is from 2.5GHz to 3.2GHz and the input voltage and current source are 24[V/DC] and 1[A]. The designed sensor circuit includes VCO, RF switch, RF detector which varies the frequency characteristics of the devices in the high frequency of 3GHz. And so we should correct the error of the frequency characteristics of those devices in the sensor circuit. To do this, we make the reference path which switches the signals to the RF detector directly without sending it to the resonator. According to the result of simulation and measurement, we can see that there is 0-50MHz difference between simulated resonator frequency and manufactured resonator frequency.