• Title/Summary/Keyword: 파열압력

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PREPREG 제작 방식에 의한 압력용기(STEB)의 시험 및 고찰

  • 이원복;손원경;유광호
    • Proceedings of the Korean Society of Propulsion Engineers Conference
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    • 1997.11a
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    • pp.30-30
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    • 1997
  • 국내에서는 시도되지 않았던 조립식 맨드렐 및 prepreg 제작 방식을 적용하여 filament winding machine으로 압력 용기(STEB)를 제작, 음향 방출 측정 장비 및 strain gage 등을 부착한 수압 시험으로 압력용기의 구조적 건전성 예측 및 파열 압력을 측정하여 성능을 분석하였다. 동일한 winding pattern 및 조건하에 prepreg winding과 wet winding 방식을 적용하여 제작한 압력 용기의 성능을 비교하였고, prepreg winding의 설계 조건, 공정 변화를 통해 제작한 압력 용기의 파열 압력 및 형태를 분석하였다. 이러한 winding 조건들에 따라 제작된 압력용기는 최종적으로 PR(Performance ratio) 값을 산출하고, 이를 통하여 prepreg 제작 방식의 장단점, 제작에 필요한 설계 조건 및 기초 자료 등을 고찰하여 보았다.

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Burst Performance Test of Filament Wound Kick Motor Case (필라멘트 와인딩으로 제작된 킥모터 연소관의 파열 성능 시험)

  • Yi, Moo-Keum;Kil, Gyoung-Sub;Cho, In-Hyun;Park, Jae-Sung;Kim, Joong-Suk
    • Proceedings of the Korean Society of Propulsion Engineers Conference
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    • 2008.05a
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    • pp.183-186
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    • 2008
  • Both structural analysis and hydraulic test have been conducted to confirm the burst characteristics of filament wound solid motor case. Failure criteria have been defined with bursting above 150% of MEOP and failure in the cylinder. The results of analysis showed that filament fiber in the cylinder should be broken at about 2088psig. From a hydraulic test the same failure mode and the level of 2200psig of burst pressure have been proved. With these results, it is verified that a filament wound case meets burst requirements.

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Evaluation of Structural Stiffness Degradation and Burst Pressure Measurement of the FM Kick-Motor Combustion Case (킥모터 FM 규격 연소관에 대한 강성저하 평가 및 파열압력 측정)

  • Yi, Moo-Keun;Cho, In-Hyun;Kim, Joong-Suk;Lee, Won-Bok
    • Aerospace Engineering and Technology
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    • v.9 no.1
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    • pp.72-77
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    • 2010
  • A hydraulic test on a filament wound case of Kick-Motor was conducted to evaluate the structural stiffness degradation and to confirm the burst performance. Failure criteria have been defined with bursting above 150% of MEOP(Maximum Expected Operation Pressure) and failure in the cylinder. The analysis result showed that filament fiber in the cylinder should be broken at about 2088psig. From a hydraulic test it has been verified that composite case meets the failure requirements, and that the stiffness does not decrease even after a year since the manufacturing.

Analysis of Forming Pressure and Burst Pressure of Rupture Disc (Rupture Disc의 성형압력 및 파열압력 해석)

  • Kang, Young-Kyu
    • Journal of the Korean Society for Precision Engineering
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    • v.18 no.6
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    • pp.109-114
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    • 2001
  • Forming pressure of the rupture disc has been analyzed theoretically and verified by experiments. Final shape of the rupture disc after forming process is assumed to be hemi-ellipsoid for small height of the rupture disc. The predicted forming pressures are in good agreement with those by experiment. A new simple model has been proposed to predict the burst pressure of the rupture disc. Experimental results show that the proposed model of burst pressure describes the bursting characteristics of the rupture disc very well.

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Rupture Prediction of the Rupture Disc Tests using Elastic-Plastic Analysis (탄소성해석을 이용한 파열판의 파열예측)

  • Han, Houk-Seop;Lee, Won-Bok;Koo, Song-Hoe;Lee, Bang-Eop
    • Proceedings of the Korean Society of Propulsion Engineers Conference
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    • 2011.11a
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    • pp.481-487
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    • 2011
  • This paper provides a comparison between finite element analysis results and test data of rupture disc. Rupture disc is safety device of high pressure equipment. Rupture disc of solid rocket motor is a device to control rupture pressure. Rupture discs were made of AISI 316L. By the elastic-plastic analysis, the stress limit of rupture discs were compared to the test results. The results can be used to control the rupture pressure by the change of the disc size.

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Decrease of Burst Pressure used a Nozzle Closure and Ignition Characteristics for a Gas Generator (가스발생기용 노즐마개 파열압력 저감화에 따른 점화특성)

  • Cha, Hong-Seok;Oh, Seok-Jin;Park, Jae-Beom;Lee, Yeung-Jo
    • Proceedings of the Korean Society of Propulsion Engineers Conference
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    • 2010.11a
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    • pp.217-220
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    • 2010
  • This paper presents an achieving method of reducing maximum acceleration for the missile by decrease of burst pressure in a nozzle closure. The relation of notch shape and burst pressure for a nozzle closure is examined by experiment. In the point of maximum acceleration reduction for a missile, an improved nozzle closure effects well compared with that of a reference closure by ground burning test of a gas generator.

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An Evaluation on Rupture Behavior of Nozzle Closure in Multi-Nozzle System (멀티노즐시스템의 노즐마개 파열 거동 분석)

  • Ro, Young-Hee
    • Journal of the Korean Society for Aeronautical & Space Sciences
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    • v.42 no.9
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    • pp.745-751
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    • 2014
  • For the multi-nozzle propulsion, the rupture pressure of nozzle closure has an effect on the initial strain rate of ignition. Moreover, the deviation of rupture pressure for each nozzle closure leads to side forces which can disturb the attitude control of rocket. When designed, it should be considered whether nozzle closures are ruptured equally and exactly in the intented pressure. In this paper, the rupture behavior is analyzed by analytical and experimental methods for plate and "+" notched nozzle closures. The rupture pressure and deviation for operating temperature, whether notched or not and notched directions are analyzed. This paper provides a comparison between rupture pressure prediction of finite elements method which tool is Abaqus/Explicit and results of the rupture test. Jonson-Cook shear failure model which corresponds to the damage initiation criterion were used in this simulation.

Evaluation of the SWR′s Early Pressure Variations in the KALIMER IHTS (KALIMER IHTS의 SWR 초기 압력파 거동 분석)

  • 김연식;심윤섭;김의광;어재혁
    • Journal of Energy Engineering
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    • v.11 no.2
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    • pp.122-129
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    • 2002
  • The analytical models and algorithm of the SPIKE code, which has been developed by KAERI's KALIMER team to investigate the sodium-water reaction phenomena in the liquid metal reactor, were introduced with its verification calculation results. The sodium water reaction of KALIMER IHTS was evaluated. Early stage of the sodium-water reaction consists of wave and mass transfer regimes. The pressure variations were independent of specific design features in the wave transfer regime. However in the mass transfer regime, the pressure variations were strongly dependent on cover gas volume and rupture disk set pressure. The early stage SWR analysis showed that the KALIMER IHTS with an appropriate cover gas volume and rupture disk set pressure had enough margin to its design pressure.

Bursting Performance Analysis of a Pulse Separation Device for a Rocket Motor (추진기관 적용 펄스분리장치의 파열특성 분석)

  • Lee, Dong-Won;Lee, Won-Bok;Kim, In-Sik;Kim, Won-Hoon
    • Proceedings of the Korean Society of Propulsion Engineers Conference
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    • 2011.04a
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    • pp.245-248
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    • 2011
  • A multi pulse rocket motor(MPRM) has several advantages compared to the single one. The range and the terminal velocity of the guided missile can be remarkably increased by the application of the pulse separation device(PSD) to the solid rocket motor which resulted in appropriate thrust distribution. In this study, the full scale heavy type dual pulse rocket motor with the bulkhead type PSD was designed, manufactured, and fire-tested. The bursting time and pressure of PSD were analyzed by the pressure, thrust and vibration results of static fire tests. As a result, the design requirement was verified that bursting pressure is lower than 30% of 2nd pulse operating pressure.

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A Study on Performance of Pressure Relief Devices of CNG Cylinder Valves (CNG 용기용밸브의 압력방출장치 성능에 관한 연구)

  • Kim, Young-Seob;Kim, Lae-Hyun;Lee, Jae-Hun
    • Journal of the Korean Institute of Gas
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    • v.13 no.4
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    • pp.33-39
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    • 2009
  • This study is intended to experiment performance of pressure relief device and to extend the effective ways to prevent cylinders of NGV from bursting when they are exposed to local fire intensively or when they are overcharged under ambient temperature at fueling stations in summer. In the results of thermal cycling experiments, all products of three companies met the requirements for gas leakage in the qualification criteria between $82^{\circ}C$ and $-40^{\circ}C$. But the o-rings of two companies' specimens among the three companies' specimens got damaged under the accelerated conditions between $135^{\circ}C$ and $-45^{\circ}C$. It took one minute and thirty nine seconds for a glass bulb type of a thermal sensitive type PRD to activate and it took two minutes and thirty one seconds for a fusible plug type of a thermal sensitive type PRD to activate. These results indicated that a glass bulb type of a thermal sensitive type PRD was one minute faster than a fusible plug type of a thermal sensitive type PRD. Under the accelerated condition $135^{\circ}C$, the activation pressure of a pressure sensitive type PRD burst at 32.1 MPa and, under the condition of qualification criteria, it burst from 30.7 MPa to 32.1 MPa.. As a result of the experiment for performance of pressure relief device, in the case of the thermal sensitive type PRD, a glass bulb type is more effective to flame than a fusible plug type. we confirmed that the rupture pressure of a pressure sensitive type PRD could not be affected by temperature and pressure cycling.

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