• Title/Summary/Keyword: Wheel rotor

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Fabrication arid Performance Tests of Flywheel Energy Storage System using High Tc Superconducting Bearing (고온초전도체 베어링을 사용하는 에너지 저장용 플라이휠 장치의 제작 및 성능 평가)

  • Lee, Ho-Jin;Kim, Ki-Baik;Koh, Chang-Seop;Lee, Soo-Hoon;Hong, Gye-Won
    • 한국초전도학회:학술대회논문집
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    • v.9
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    • pp.310-314
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    • 1999
  • A prototype of Flywheel Energy Storage System with high Tc superconducting bearings was fabricated and tested to verify its applicability for the energy industry. The moment of inertia of assembled wheel with rotor magnets is about 1.072${\times}$10$^{-1}$ Kg-m$^2$. The wheel was designed to withstand its integrity up to the rotation speed of 20,000 rpm. YBCO bulk superconductors prepared by seed growth method were used as bearing to levitate and stabilize the rotating wheel. High speed rotation of the flywheel without mechanical contact was achieved by using specially designed Halbach type motor. The flywheel system showed very high stability during test operation performed up to the speed of about 10,000rpm. The energy loss measured by free decay test performed between 9,300 rpm and 7,000 rpm was calculated as about 45 W.

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Development of a Remote Controlled Weeder Driven by Solar Battery Power (태양전지를 이용한 원격조종 중경제초기 개발)

  • Kim, T.S.;Jang, I.J.
    • Journal of Biosystems Engineering
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    • v.32 no.2 s.121
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    • pp.91-96
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    • 2007
  • In this study, a prototype remote controlled weeder using solar module was developed and the evaluations of weeding, side walking and weeding performance were conducted to see if actual application was feasible in the paddy field. When traveling, the loss electric current was 8 to 15 A depending on operating and soil conditions. The average traveling speed was 0.25 m/s and the average slippage was 18%. When it side walked row by row, electric current consumption was 7 A on the average. When wheel rotors line went initially up and last down, electric current consumption was 12 to 15 A due to soil resistance. Electric current consumption when shifting wheel rotors line was less than 5 A due to no resistance. Field efficiency was 105 min/10a based on the test field. Operation was able to be done for 4.16 hours continually by 52 AH battery based on 300 W average maximum power consumption and 4.6 hours under sunny day considering solar module.

Vibration Control of Flywheel Energy Storage System (플라이휠 에너지 저장장치의 진동 제어 성능 평가)

  • Lee, Jeong-Phil;Han, Sang-Chul;Park, Byeong-Cheol;Han, Young-Hee;Park, Byung-Jun;Jung, Se-Yong
    • The Transactions of The Korean Institute of Electrical Engineers
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    • v.58 no.9
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    • pp.1750-1756
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    • 2009
  • In this paper, 5 kWh class Superconductor Flywheel Energy Storage System (SFES) was constructed including motor/generator, superconductor magnetic bearing(SMB), composite rotor and electromagnetic damper(EMD) system. High speed rotation test was performed after levitating flywheel rotor only using EMD without SMB. the PD controller of EMD was designed. the control system is constructed using xPC which is real time digital control system. the results of high speed rotation test showed that proposed EMD system have sufficient damping in cylindrical mode and conical mode, and vibration of wheel was suppressed below 10 ${\mu}m$.

Running Bucket Vibration Test of Steam Turbines (증기 터빈 버켓의 회전 진동 시험)

  • 박종포;신언탁;김호종
    • Proceedings of the Korean Society for Noise and Vibration Engineering Conference
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    • 1997.10a
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    • pp.96-100
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    • 1997
  • A design modification was made on the 9-th stage wheel dovetail of a high-intermodiate pressure (HIP) turbine rotor for a fossil power plant that necessitates the use of new long-shank buckets for the row. A bucket vibration test is necessary to verify that the new 9-th stage buckets have adequate frequency margin from a nozzle passing frequency when running at speed. A finite element analysis (FEA) has been performed using a commercial S/W to approximately estimate bucket natural frequencies, and thus to help the vibration test. A row of the new buckets has been assembled on the HIP rotor for the vibration tests using dynamic balancing facilities. The tests have been done during deceleration run with air excitation. The test results are compared with the calculation using our empirical formula, and show that the modified design meets the frequency-margin requirements.

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An Experimental Study on the Performance of the Vertical-Axis Wind Turbine (수직축 풍력터빈 성능개선에 관한 실험적 연구)

  • Kim, Byung-Kook;Kim, Young-Ho;Song, Woo-Seog;Lee, Seung-Bae;Nam, Sang-Kyu;Kim, Sa-Man
    • The KSFM Journal of Fluid Machinery
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    • v.10 no.3 s.42
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    • pp.17-24
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    • 2007
  • This paper presents the design procedure of a vertical wind turbine named jet-wheel-turbo turbine and the numerical and experimental verifications. The design parameters such as the rotor inlet angle, the diameter-to-hub ratio, the inlet guide outlet angle and the solidity were optimized to maximize the energy transfer, and to further increase the turbine efficiency by applying the side guide vane and the side opening to the rotor. The maximum power coefficient of 0.59, which is much higher than the ever-designed three-bladed horizontal turbines, was experimentally obtained when the optimal inlet- and side-guide vanes were installed and both sides of the rotor were 80% opened. The maximum power coefficients occur at the tip speed ratio ranging between 0.6 and 0.7. This vertical-axis turbine model can be applied to the large-scale power generation system with the speed and torque control algorithm for the specified wind characteristics.

Development of Prototyping and Die/Mold Manufacturing Technology using Rapid Prototyping(SLA) (쾌속 3차원 조형법을 이용한 시작기술 및 시작금형)

  • Park, K.;Lee, S.C.;Jung, J.H.;Yang, D.Y.;Yoon, J.R.
    • Transactions of the Korean Society of Mechanical Engineers A
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    • v.20 no.5
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    • pp.1582-1589
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    • 1996
  • Rapid prototyping is a new prototyping technology which produces three dimensional part models directrly from CAD data and has been extensively applied to various manufacturing processes. There are many types of rapid prototyping systems due to their building principles and materials. In this work, Stereolithography Appaaratus(SLA) which is the most widely-used rapid prototyping system is introduced to achieve die/mold technology innovation. For the purpose, the prototyping technology using SLA is developed such that patterns of which shapes are quite complicated are successfully produced with high accuracy. Using these patterns, prototype die/molds are efficientrly manufactured; a turbocharger rotor, a fan and a wheel patterns, prototype die/molds are efficienterly manufactured ; a turbochager rotor, a fan and a wheel pattern are made, and the molds of the investment casting, the injection molding and the die casting are manufactured respectively. The casting products are produced using these molds and it turns out that these methods are quitre effective for manufacturing products of complicated geometry from the viewpoint of efficiency and productivity.

Running Bucket Vibration Test of Steam Turbines (증기 터빈 버킷의 회전 진동 시험)

  • 박종포;신언탁;김호종
    • Journal of KSNVE
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    • v.8 no.2
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    • pp.331-335
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    • 1998
  • A design modification was made on the 9-th stage wheel dovetail of a high-intermediate pressure (HIP) turbine rotor for a fossil power plant that necessitates the use of new long-shank buckets for the row. A bucket vibration test is necessary to verify that the new 9-th stage buckets have adequate frequency margin from a nozzle passing frequency when running at speed. A finite element analysis (FEA) has been performed using a commercial S/W to approximately estimate bucket natural frequencies, and thus to help the vibration test. A row of the new buckets has assembled on the HIP rotor for the vibration tests using dynamic balancing facilities. The tests have been done during deceleration run with air excitation. The test results are compared with the calculation using our empirical formula, and show that the modified design meets the frequency-margin requirements.

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Rotordynamic Characteristics Analysis of Turbocharger Turbine for Spin Test (터보차져용 터빈의 스핀 테스트를 위한 로터다이나믹 특성분석)

  • Kim, Byung-Ok;Yang, Sung-Jin;Lee, Myung-Ho
    • The KSFM Journal of Fluid Machinery
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    • v.14 no.6
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    • pp.91-95
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    • 2011
  • This paper deals with the detail rotordynamic analysis for the assembly rotor composed of turbine wheel, turbine shaft, connecting arbor, and flange & spindle in order to perform the spin test of turbocharger turbine. Prior to rotordynamic analysis, the 1st spin test was performed but the test was failed by excess vibration in the neighborhood rated speed. It is the reason for this fail that the separation margin between the rated speed and critical speed is not enough, confirmed by rotordynamic analysis results. Since then, the dimension of turbine shaft was modified and the critical speeds were again reviewed for modified assmebly rotor. In results, the separation margin between the rated speed and critical speed is over 20% and then the 2nd spin test was performed successfully. In preparing spin test for turbine, compressor wheels and etc., the geometry design of connecting arbor and dimension of rough machining should be reviewed by considering rotordynamic results, and the separation margin should be enough for successful spin test.

Verification of Roll Angle Estimation Performance of Slowly Rolling Guided Munition by Flight Experiment (비행 시험을 통한 저속 회전 유도형 탄약의 롤각 추정 성능 검증)

  • Park, Junwoo;Jung, Wooyoung;Bang, Hyochoong;Kim, Jin-Won;Heo, Junhoe;Pak, Chang-Ho;Seo, Songwon
    • Journal of the Korean Society for Aeronautical & Space Sciences
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    • v.48 no.9
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    • pp.681-689
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    • 2020
  • This paper presents methods and results of both flight test examining roll angle estimation performance of slowly rolling munition forced to spin in the air, and fabricating a replica of guided munition. Guided munition was deployed from multi rotor type UAV mother ship whose altitude and velocity was conveyed to it as initial state. Flight test scenario is composed of a sequence of munition drop(deployment), munition spin, roll angle estimation and stabilization. Munition was deployed from mother ship at around 200m high with horizontal velocity of 15m/s, and was made spun using internal reaction wheel. Performance analysis on roll angle estimation is provided in comparison with commercial aerospace graded GPS/INS. Moreover, several mechanisms that rotates munition using reaction wheel, and actual product that realizes one of them are introduced.