• 제목/요약/키워드: Rotating Parts

검색결과 251건 처리시간 0.03초

새로운 내측기어 성형용 사출성형 금형구조의 개발 (Development of a new injection mold structure for internal gears)

  • 권윤숙;제덕근;정영득
    • 한국금형공학회:학술대회논문집
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    • 한국금형공학회 2008년도 하계 학술대회
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    • pp.129-133
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    • 2008
  • As a rotating machine element, plastic gears are more and more widely used in such as industrial machine element, since plastic gear is lighter, higher wear-resistance, and higher vibration absorbing ability than metal gears. When operating plastic parts, tooth breakage and fatigue life shortened due to increasing number of applying load and tooth flank temperature rising, such that accuracy of plastic gears is divided from allowable range to cause vibration and noise. On this study, a internal plastic gears are developed which improved the filling balance molding process by a new injection mold structure. The new mold structure called HR3P(hot runner type 3plate mold). As the result from this studies, we obtained a very accurate roundness internal gears by using design of experiment.

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가스질화처리 적용을 통한 스마트무인기 머레이징강 로터허브 부품 품질개선 (Quality Improvement of Smart UAV Rotor-Hub Part Through Gas Nitriding of Maraging Steel)

  • 이명규;최성욱;김재무
    • 항공우주시스템공학회지
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    • 제8권2호
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    • pp.33-39
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    • 2014
  • Feathering spindle is one of the critical parts of the rotor system in the Smart Unmanned Aerial Vehicle(SUAV) that it was manufactured with special material, Maraging C300. During the initial ground and tie-down flight tests of the SUAV, surface of the feathering spindle contacting to the needle-roller bearings showed excessive wear and dent due to high vibrating loads transferred from the rotating blades. Gas nitriding process was applied to the bearing contact surface of the feathering spindle to increase surface hardness so as to improve the surface defects. This paper briefly presents the gas nitriding process adopted and the spindle quality improvements including wear and corrosion resistance.

디스크형 캠의 자동설계용 CAD S/W 개발-Part I :설계 및 해석 알고리즘 개발 (Development of CAD Software for Automatic Design of Disk-Typed Cams-Part I : Iterative Contact Method)

  • 손주리;신중호
    • 한국기계연구소 소보
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    • 통권19호
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    • pp.149-154
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    • 1989
  • Generally Cam-Follower systems consist of two elements: Cam is for rotating motion and follower for reciprocating motion. Depending on the shape of cam and type of follower, the motion of cam-follower system is determined. Thus design process and analysis process must be well defined. The design process means to find the coordinates of cam shape which can be defined the given motion of follower and the analysis process means to determine the motion curve of follower corresponding to the given cam based on the dimensions of a cam-follower system. This paper consists of two parts: One is development of a numerical method for design and analysis of cam-follower systems, the other is for development of a CAD program and its application. As the first part of the paper, an iterative contact method is proposed. This method can calculate the contact points between cam and roller and determine their contact angles iteratively. The second part of the paper presents the structure of a CAD program and its availability to the industrial applications.

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회전 스웨이징을 이용한 자동차용 카울크로스바의 일체화 제조공정 개발 (Development of One-Piece Manufacturing Process for Automotive Cowl Cross Bar Using Rotary Swaging)

  • 김홍석;윤재웅
    • 소성∙가공
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    • 제25권5호
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    • pp.332-337
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    • 2016
  • The automobile cowl cross bar which is a backbone frame part holding electrical and air conditioning components inside the cockpit module has been designed with more complex geometries recently due to demands of its enhanced functions and reduced weight of frame parts. The traditional manufacturing process using welding between tubes with different diameters shows several problems such as poor mechanical characteristics and appearance, etc. Therefore, in this study, one-piece manufacturing processes which can eliminate the welding process were developed by applying the rotary swaging process. CAE analyses were conducted to examine the feasibility of the process and prototypes were manufactured by using a rotary swaging machine with 4 split rotating dies and 12 head rollers. Bending tests of the manufactured prototypes confirmed that the rotary swaging process gives better mechanical properties comparing with the conventional processes.

항만용 크레인 구동 모터 고진동 사례 연구 (A Case Study of the Higher Vibration on the Driving Motors of Port Crane)

  • 김영춘;박희주
    • 대한기계학회:학술대회논문집
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    • 대한기계학회 2001년도 춘계학술대회논문집B
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    • pp.416-421
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    • 2001
  • It was firstly issued that frequently broken of Encoder installed at travelling motor during RTGC operation. Estimated as broken due to excessive vibration of traveling and motor manufacturer claimed it as resonance of motor base. The principal vibration of Encoder was caused by the rotating vibration component of motor and by traveling wheel. The component transmitted from the wheel didn't have great vibration by the resonance with motor and other parts. Therefore, the plans was tried to add the support point to prevent the Encoder shaft vibrated greatly and inhibit the vibration. These showed good results.

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스폿용접 로봇용 스위블 유닛의 개발 (The Development of Swivel Unit for Spot Welding Robots)

  • 김용석;박성호;양순용
    • 한국공작기계학회논문집
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    • 제17권4호
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    • pp.119-125
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    • 2008
  • A new type of swivel unit is suggested in order to complement weak points of the existing. This new type of Swivel unit is developed by adopting a spring type cable which has elasticity and restoring force. To minimize the troubles in the process of manufacturing during operating the new type system, strength analysis and the check of interference between parts are accomplished with CATIA. The check of rotating performance is also carried out to determine the diameter and length of spring type cable by SimDesigner motion analysis. Swivel unit used in the robot spot welding is developed with spring type cable and its usefulness in the industrial field is verified through experiments. This system has been registered for patent.

굴삭기공장에서 로봇을 이용한 용접공정의 3D 시뮬레이션 사례 연구 (A Case Study of the Design of Robot Welding Station in an Excavator Factory Using 3D Simulation)

  • 문덕희;조현일;백승근
    • 한국시뮬레이션학회:학술대회논문집
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    • 한국시뮬레이션학회 2005년도 추계학술대회 및 정기총회
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    • pp.113-121
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    • 2005
  • Virtual Manufacturing is a powerful methodology for developing a new product, new equipment and new production system. It enables us to check the errors in design before production. This paper deals with a case study of virtual manufacturing in an excavator factory. Boom and rotating table of upper body are selected for application. 3D models of parts and fixtures are developed with CATIA and 3D simulation models are developed with IGRIP. These models are used for the design of fixture to verify the motion of the equipment. As a result, the manual welding systems are replaced by automatic systems and many design errors are corrected in the design phase, which enables us to reduce the developing cost and time.

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부하변동에 따른 유도전동기 전류와 전력 특성 (Characteristics for Current and Power of Induction Motor by Load Variation)

  • 김종겸
    • 조명전기설비학회논문지
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    • 제25권8호
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    • pp.82-87
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    • 2011
  • Induction motor is most widely used as the driving power in the industrial site. Induction motor current is composed of two parts, magnetizing current and load current. Load current uses energy what is doing the work. Load current varies with load variance but magnetizing current is constant, regardless of load variation. Magnetizing current needs for establishing the rotating magnetic field of induction motor and lags behind the voltage. Generally capacitor is used for power-factor compensation of inductive load. Self-excitation occurs when the capacitive reactive current from the capacitor is greater than the magnetizing current of the induction motor. When this occurs, excessive voltages can result on the terminals of the motor. This excessive voltage can cause insulation degradation and ultimately result in motor insulation failure. In this paper, we analyzed that how the magnetizing current and condenser current is operating at the allowable limit by the load variation. Condenser current is below allowable limit of magnetizing current but magnetizing current is above allowable limit at the lower load operation condition.

배전용 지지물의 FRP 적용 기술 (Applied Technology of FRP Single Pole for Power Distribution Line)

  • 박기호;조한구;한동희
    • 한국전기전자재료학회:학술대회논문집
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    • 한국전기전자재료학회 2000년도 하계학술대회 논문집
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    • pp.79-81
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    • 2000
  • Outdoor insulation of overhead distribution lines with wood, concrete and steel pole has been safety under various environmental conditions including contamination, moisture condensation, rain and lightning overvoltages. In this paper introduce to FRP technology of the power distribution single pole. FRP pole has been used very much as high strength material for insulators because of its high strength and good insulation properties. In addition, FRP pole was made by filament winding method. In a filament winding process, a band of continuous resin-impregnated rovings or monofilaments is wrapped around a rotating mandrel and cured to produce axisymmetric hollow parts.

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누설 유동을 고려한 스크롤 압축기의 동적 거동 해석 (Dynamic Behavior Analysis of Scroll Compressor Considering Leakage Flow)

  • 정영철;원성규;정의봉
    • 한국소음진동공학회:학술대회논문집
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    • 한국소음진동공학회 2005년도 추계학술대회논문집
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    • pp.417-420
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    • 2005
  • This paper presents an analytical method to evaluate the dynamic behavior of the scroll compressor. Unbalanced forces and moments act on the compressor body because of the reaction forces acting on rotating components like the orbiting scroll, Oldham coupling ring, and the crank shaft. The vibration of the compressor is induced by the forces and the moments. In this paper, through modeling of the leakage flow, solving the forces from the equations of motion of the moving parts, the analysis of vibration of the compressor was performed. According to the operating condition, the variation of acceleration of the compressor body were calculated and compared.

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