• Title/Summary/Keyword: Chamber Structure

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3-Dimensional Numerical Analysis of Air Flow inside OWC Type WEC Equipped with Channel of Seawater Exchange and Wave Characteristics around Its Structure (in Case of Irregular Waves) (해수소통구를 구비한 진동수주형 파력발전구조물 내 공기흐름과 구조물 주변에서 파랑특성에 관한 3차원수치해석(불규칙파의 경우))

  • Lee, Kwang Ho;Lee, Jun Hyeong;Jeong, Ik Han;Kim, Do Sam
    • Journal of Korean Society of Coastal and Ocean Engineers
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    • v.30 no.6
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    • pp.253-262
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    • 2018
  • Oscillating Water Column (OWC) Wave Energy Converters (WEC) harness electricity through a Power-Take-Off (PTO) system from the induced-airflow by seawater oscillating inside a chamber. In general, an air chamber with a relatively small cross-sectional area is required compared to seawater chamber to obtain high-velocity air in the PTO system, and in order to simulate an accurate air flow rate in the air chamber, a three-dimensional study is required. In this study, the dynamic response of OWC-WEC that is equipped with the channel of seawater exchange for the case of irregular waves has been numerically studied. The open source CFD software, OLAFLOW for the simulation of wave dynamics to the openFOAM and FOAM-extend communities, was used to simulate the interaction between the device and irregular waves. Based on the numerical simulation results, we discussed the fluctuation characteristics of three dimensional air flow in the air-chamber, wave deformation around the structure and the seawater flow inside the channel of seawater exchange. The numerical results the maximum air flow velocity in the air-chamber increases as the Ursell value of the significant wave increases, and the velocity of airflow flowing out from the inside of air chamber to the outside is greater than the speed of flowing into the air chamber from the outside.

Fabrication of Full-Scale Combustion Chamber of Liquid Rocket Engine for Ground Hot Firing Tests (실물형 고압 연소기의 연소시험 검증용 제작)

  • Kim Jonggyu;Seo Seonghyeon;Kim Seunghan;Han Yeoungmin;Ryu Chulsung;Seol Wooseok
    • Proceedings of the Korean Society of Propulsion Engineers Conference
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    • v.y2005m4
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    • pp.305-308
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    • 2005
  • This paper presents a fabrication of a full-stale combustion chamber of a liquid rocket engine for a ground hot firing test. Engine drawings for manufacturing were prepared after conceptual and detail designs. The combustor is composed of a head and a chamber. SUS316L is used for materials of the head because of the good quality in low temperature. Inner materials of the ablative cooling chamber is silica/phenolic and outer case materials is the SUS316L. Materials of the regenerative cooling chamber are C18200 and SUS316L. After lathe, general milling and MCT machinings, components were finished by electrolytic polishing. A brazing method was applied for bonding the injectors and the injector plate, the regenerative cooling chamber because of structure configurations.

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Development of Porthole Extrusion Die for Improving Welding Pressure in Welding Chamber by Using Numerical Analysis (수치해석을 이용한 접합실 내 접합압력 향상을 위한 포트홀 압출금형 개발)

  • Lee, S.Y.;Lee, I.K.;Jeong, M.S.;Ko, D.C.;Kim, B.M.;Lee, S.K.
    • Transactions of Materials Processing
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    • v.26 no.2
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    • pp.115-120
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    • 2017
  • Porthole extrusion process is a very effective metal forming process to produce aluminum profiles with hollow sections. The structure of porthole extrusion die is very complex. In this process, the billet is divided by porthole bridge, and then the divided billet is welded in the welding chamber. The welding pressure in the welding chamber is very important. The higher welding pressure improves the quality of the aluminum profiles. Therefore, the objective of this study is to develop a new porthole extrusion die for improving the welding pressure in the welding chamber by using numerical analysis. The effectiveness of the new porthole extrusion die was verified by using numerical analysis. Through numerical analysis, the welding pressures in the welding chamber between the new porthole die and the conventional porthole die were compared with each other.

Experimental Study on the Characteristics of Pressure Fluctuation in the Combustion Chamber with Branch Tube (분기관을 가진 연소 챔버 내 압력변동 특성에 관한 실험적 연구)

  • Park, Jang-Hee;Lee, Dae-Keun;Shin, Hyun-Dong
    • Transactions of the Korean Society of Mechanical Engineers B
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    • v.33 no.7
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    • pp.552-558
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    • 2009
  • An experimental study using the combustor with branch tube was conducted in order to model the industry combustor with FGR (flue gas recirculation) system and to study a thermo-acoustic instability generated by a branch tube. The branch tube is a structure used to modify a system geometry and then to change its pressure field, and the thermo-acoustic instability, usually occurs in a confined geometry, can result in serious problems on industrial combustors. Thus understanding of the instability created by modifying geometry of combustor is necessary to design and operate combustor with FGR system. Pressure fluctuation in the combustion chamber was observed according to diameter and length of branch and it was compared with the solution of 1-D wave equation. It was found that branch tube affects the pressure field in the combustion chamber, and the pressure fluctuation in the combustion chamber was reduced to almost zero when phase difference between an incipient wave in the combustion chamber and a reflected wave in the branch tube is $\pi$ at the branch point. Also, the reduction of pressure fluctuation is irrespective of the installed height of branch tube if it is below $h^*=0.9$ in the close-open tube and open-open tube.

An Experimental Study to Develop the Perforated Panel System for Noise Chamber (소음쳄버용 다공판 시스템 개발을 위한 실험적 연구)

  • Lee, Young-Sup;Lee, Dong-Hoon;Chung, Kwang-Seop
    • Journal of the Korean Society for Railway
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    • v.12 no.5
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    • pp.806-810
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    • 2009
  • The air conditioner system that is used in large structure, such as hospital, hotel, railway platform and train generate a high level noise generally. A chamber with sound absorbing materials, such as glass wool and polyurethane foam, are installed in this system to reduce the noise. However, these chambers cause environmental problems owing to the sound absorbing materials recently. Therefore, we develop noise chamber a built-in perforated panel resonance system as eco-friendly chamber to solve this problems. This noise chambers show the same noise reduction performance as the current chambers in the range above 500Hz. But, it reduces the noise up to 8dB(A) comparison to the current chambers in the range 200Hz~400Hz.

Hydraulic Experiments for the Reflection Characteristics of Perforated Breakwaters (유공방파제의 반사특성에 관한 수리실험)

  • 박우선;전인식;이달수
    • Journal of Korean Society of Coastal and Ocean Engineers
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    • v.5 no.3
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    • pp.198-203
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    • 1993
  • Hydraulic experiments were carried out to investigate the reflection characteristics of perforated breakwaters in regular wave conditions varying the width of wave chamber and the shape of perforated wall. It was found that the reflection coefficient of the perforated breakwater was very sensitive to the change of wave chamber width. giving its minimal value when the width of the wave chamber is approximately 0.2 times the wave length in the wave chamber. This phenomenon may be resulted from the wave resonance inside the wave chamber. The reflection coefficients slightly varied for all shapes of perforated wall. i.e., vortical slit, horizontal slit or circular hole. However, the reflection trend of the structure was not significantly affected by the shape of the perforated wall.

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Design and Fabrication of Technology Demonstration Model of 75 tonf Regenerative Cooling Thrust Chamber (75톤급 재생냉각 연소기 기술검증용 시제 설계 및 제작)

  • Kim, Jong-Gyu;Ahn, Kyu-Bok;Lim, Byoung-Jik;Kim, Mun-Ki;Kang, Dong-Hyuk;Choi, Hwan-Seok
    • Proceedings of the Korean Society of Propulsion Engineers Conference
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    • 2011.04a
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    • pp.31-34
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    • 2011
  • Design and fabrication of Technology Demonstration Model(TDM) of 75 tonf regenerative cooling thrust chamber were described. It has design chamber pressure of 60 bar, propellant mass flow rate of 243.6 kg/s, and nozzle expansion ratio of 12. It has a single welded structure of the mixing head and the chamber. Design and fabrication technologies established through this TDM can be used to development of flight model.

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Frequency Range Expansion of Pneumatic Exciter by Using Dual-chamber (이중챔버를 이용한 공압가진기의 주파수 범위 확장)

  • Park, Young-Woo;Kim, Kwang-Joon
    • Transactions of the Korean Society for Noise and Vibration Engineering
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    • v.23 no.10
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    • pp.909-919
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    • 2013
  • Pneumatic exciters can be good replacements of electrodynamic, piezoelectric and hydraulic exciters owing to simple structure and large exciting force. One problem to be solved is a slow response caused by compressibility of air. Desirable frequency response characteristics of exciter are constant magnitude and zero degree phase, because users want no time delay between input signal and output force. For this reason, frequency range of pneumatic exciters is limited about 0~1 Hz. Therefore, expansion of frequency range is an important issue when designing the pneumatic exciter. In this paper, the pneumatic exciter which has same structure with active pneumatic isolator is dealt with. The dynamic characteristics are presented, and its limitation of expanding frequency range is shown based on analytical studies. Then the pneumatic exciter with dual-chamber is suggested to overcome this problem. Based on simulation study, a design method is presented.

A Study on the Design of Back Pressure for Automotive Scroll Compressor

  • Koo, In-Hwe;Lee, Geon-Ho
    • International Journal of Air-Conditioning and Refrigeration
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    • v.17 no.1
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    • pp.1-6
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    • 2009
  • The optimum design of back pressure chamber is one of the most important factors in designing scroll compressors because it has a great influence on the efficiency and other design parameters. The design process can be divided into 2 parts. One is obtaining the optimum pressure of the chamber and keeping it in constant value. The other is finding out the minimum inflow rate of medium with which back pressure chamber is filled. In this study we are focused on the first step. At first we added a simple structure that can change back pressure without reassembling compressor. It makes possible to obtaining optimum back pressure. Then we designed an equipment that the back pressure control valve assembly could be independently tested with. Spring was redesigned to decrease stiffness variation. Also sealing mechanism of back pressure control valve was improved to more effective way. As a result, it was verified that in a real mode test back pressure variation could be retained in 2.3% with discharge pressure and operating frequency varied. In addition the integrated structure of back pressure control valve is expected to contribute to effective manufacturing process.

Design of Back Pressure Control Valve for Automotive Scroll Compressor (차량용 전동식 스크롤 압축기의 배압제어밸브 설계)

  • Nam, Bo-Young;Koo, In-Hwe;Han, Young-Chang;Lee, Geon-Ho
    • Proceedings of the SAREK Conference
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    • 2007.11a
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    • pp.410-415
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    • 2007
  • The optimization of back pressure chamber is one of the most important factors in designing scroll compressors, because it has a great influence on the efficiencies and other design parameters. The design process can be divided into 2 parts. One is obtaining the optimum pressure of the chamber and keeping it in constant value. And the other is finding out the minimum inflow rate of medium with which back pressure chamber is filled. In this study we are focused on the first step. At first we added a simple structure that could change back pressure without reassembling compressor. It makes the optimum back pressure be obtained. And then we devised an equipment that the back pressure control valve assembly could be independently tested with. A spring was redesigned to decrease stiffness variation. And sealing mechanism of back pressure control valve was improved to more effective way. As a result it was verified in a real mode test that back pressure variation could be stabilized within 2.3% when discharge pressure and operating frequency varied. And the integrated structure of back pressure control valve is expected to contribute to an effective manufacturing process.

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