• Title/Summary/Keyword: Bearing Vibration

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Analysis of a Journal and Thrust FDB and a Conical FDB in the Spindle Motor of a Computer Hard Disk Drive (HDD 스핀들 모터용 저널-스러스트 유체동압 베어링과 코니컬 유체동압 베어링의 특성해석비교)

  • Kim, Bum-Cho;Jang, Gun-Hee
    • Proceedings of the Korean Society for Noise and Vibration Engineering Conference
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    • 2005.05a
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    • pp.478-483
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    • 2005
  • This paper presents the comparison analysis of a Journal and thrust FDB (fluid dynamic bearing) and a conical FDB in a HDD spindle motor. The Reynolds equation is appropriately transformed to describe journal, thrust and conical bearing. Finite element method is applied to analyze the FDB by satisfying the continuity of mass and pressure at the interface between the hearings. The pressure field of the bearings is numerically approximated by applying the Reynolds boundary condition. The load and friction torque are obtained by integrating the pressure and the velocity gradient along the fluid film. The flying height of the spindle motor is measured to verify the proposed analytical result. This research shows that the conical bearing generates bigger load capacity and less friction torque than the journal and thrust bearing in a HDD spindle motor.

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Experimental Characterization of Hydrodynamic Bearing Spindle Motor for High Performance Hard Disk Drive (고성능 하드 디스크 드라이브 개발을 위한 유체베어링 스핀들 모터의 특성분석(현장개발사례: SAMSUNG HDD ′SPINPOINT POLARIS SERIES′))

  • Son, Young;Hwang, Tae-Yeon;Han, Tun-Sik;Kang, Seong-Woo;Morris, Frank
    • Proceedings of the Korean Society for Noise and Vibration Engineering Conference
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    • 2001.05a
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    • pp.930-935
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    • 2001
  • The experimental characterization of hydrodynamic bearing spindle motor is performed for the practical implementation of high-performance hard disk drive system. Firstly, the design concept of hydrodynamic bearing for the disk drive system is addressed including the herringbone grooved journal bearing, the spiral grooved thrust bearing, capillary seal design, and the viscous pumping of fluid. Secondly, the experimental evaluation is performed for the disk drive system in which the hydrodynamic bearing spindle motor is implemented and its dynamic performances are compared with conventional ball-bearing spindle motor. The key parameters include NRRO(Non Repeatable Run-Out), disk dynamics, acoustics, and resultant PES (Position Error Signal). Finally, the external gyro-exciting test results including 200k CSS(Continuous Start-Stop) on three angular attitudes(0,90, 180 degree) are presented in order to verify the practical reliability of disk drive system subject to the gyro-motion of hydrodynamic bearing spindle motor.

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A Design of Air-Lubricated Slider Bearings for Improving the Flying Stability in Track Seek and Increasing the Air-Bearing Stiffness (트랙탐색 안정성과 베어링 강성 향상을 위한 공기윤활 슬라이더 베어링의 최적설계)

  • Kang, Tae-Sik;Park, No-Yeol;Lee, Sung-Chang;Choi, Dong-Hoon;Jeong, Tae-Gun
    • Proceedings of the Korean Society for Noise and Vibration Engineering Conference
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    • 2000.06a
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    • pp.1561-1569
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    • 2000
  • Flying attitudes of the slider, which are flying height, pitch and roll, are affected by the air flow velocity, the skew angle, and the manufacturing tolerances. Traditional designs of the air bearing surface have considered only the flying performances for the variations in the air flow velocity and the skew angle, which are determined by the radial position. In this study, we present the new shape design of the air bearing surface by considering the track seek performance and the air bearing stiffness as well as the traditional design requirements. The optimization technique is used to improve the dynamic characteristics and operating performance of the newly proposed air bearing surface shape design further. The optimized configuration is obtained automatically and the optimally designed sliders show the enhanced flying and dynamic characteristics.

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Stability analysis of the rotating and stationary grooved journal bearings (정지홈과 회전홈을 갖는 저널베어링의 안정성 평가)

  • Lee, M.H.;Lee, J.H.;Jang, G.H.
    • Proceedings of the Korean Society for Noise and Vibration Engineering Conference
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    • 2013.04a
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    • pp.141-146
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    • 2013
  • This research investigates the stability analysis for the rotating and the stationary grooved journal bearing. The dynamic coefficients of the journal bearing are calculated by using FEM and the perturbation method. When journal bearing is in whirling motion, the dynamic coefficients have time-varying components as a sine wave due to the reaction force of oil film toward the center of journal even in the steady state. The solutions for the equations of motion can be assumed as the Fourier series expansion. The equations of motion can be rewritten as the linear algebraic equations with respect to the Fourier coefficients. Then, stability of the grooved journal bearing can be calculated by Hill's infinite determinant. The periodic function of dynamic coefficients is derived using Fourier Fast Transform(FFT).The stability of journal bearing is determined as rotating speed increases and the stability of rotating grooved journal bearing is compared and discussed with the stability of stationary grooved journal bearing.

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Vibration Characteristics of a Synchro Clutch Coupling for Steam Turbine (증기터빈용 Synchro Clutch Coupling의 진동 특성)

  • Shim, Eung-Gu;Lee, Tae-Gu;Moon, Seung-Jae;Lee, Jae-Heon
    • Plant Journal
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    • v.4 no.3
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    • pp.66-72
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    • 2008
  • The vibration of steam turbine is caused by Mass unbalance, Shaft misalignment, Oil whip and rubbing etc. But in turbine which is normally operated and maintained, the Mass unbalance component possesses the greatest portion. Our power plant has two steam turbines in capacity of 200 MW and 135 MW respectively and each turbine is supported by 6 journal bearings. However, we had many difficulties because the vibration amplitude of #3 and #4 Bearings was high during the start-up and operation mode change of steam turbine. But, with this study, we completely solved the vibration problem caused by the mass unbalance of #1 steam turbine. Until a recent date, #3 and #4 bearings which support high pressure turbine for #1 steam turbine had shown about $135{\mu}m$ in vibration amplitude (sometimes it increased to $221{\mu}m$ maximum. alarm: 6 mils, trip: 9 mils) at base load. After applying the study, they decreased to about $45{\mu}m$ maximum. It is a result from that we did not change the setting value of bearing alignment and only changed the assembly position of internal parts in Synchro clutch coupling rachet wheel which links between high pressure turbine and low pressure turbine, and increased the internal gap and machining of the Pawl cage surface. In the operation of steam turbine, if the vibration value increases by 1X, we should reduce the vibration of bearing by weight balancing. However, unless the vibration of bearing is declined by the balancing, we will have to disassemble and check the component and find the cause. In this study, we researched the way to lower mass unbalance that is 1X vibration component which has the greatest portion of vibration generated by steam turbine and we got good result by applying the findings of this study.

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A study on Mass Unbalance Vibration Generated from 200MW Steam Turbine Synchro Clutch Coupling (증기터빈용 Synchro Clutch Coupling에서 발생하는 진동에 관한 연구)

  • Shim, Eung-Gu;Kim, Young-Kyun;Moon, Seung-Jae;Lee, Jae-Heon
    • 한국전산유체공학회:학술대회논문집
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    • 2008.03b
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    • pp.232-235
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    • 2008
  • The vibration of steam turbine is caused by Mass Unbalance, Shaft Misalignment, Oil Whip and Rubbing etc. but in turbine which is normally operated and maintained, the Mass Unbalance component possesses the greatest portion. Our power plant has two steam turbines in capacity of 200MW and 135MW respectively and each turbine is supported by 6 journal bearings. However, we had many difficulties because the vibration amplitude of No 3 and 4 Bearings was high during the start-up and operation mode change of steam turbine. But, with this study, we completely solved the vibration problem caused by the mass unbalance of No 1 steam turbine. Until a recent date, No 3 and 4 bearings which support high pressure turbine for No 1 steam turbine had shown about 135${\mu}$m in vibration amplitude (sometimes it increased to 221${\mu}$m maximum. alarm: 6mils, trip: 9mils) at base load. After applying the study, they decreased to about 40${\mu}$m maximum. It is a result from that we did not change the setting value of Bearing Alignment and only changed the assembly position of internal parts in Synchro Clutch Coupling Rachet Wheel which links between high pressure turbine and low pressure turbine, and increased the internal gap and machining of the Pawl stopper surface. In the operation of steam turbine, if the vibration value increases by 1X, we should reduce the vibration of bearing by weight balancing. However, unless the vibration of bearing is declined by the balancing, we will have to disassemble and check the component and find the cause. In this study, We researched the way to lower mass unbalance that is 1X vibration component which has the greatest portion of vibration generated by steam turbine and We got good result by applying the findings of this study.

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A Study on the Fault Detection of Roller Bearings in the Auto-Transmission (자동변속기에서의 롤러 베어링 결함 검출에 관한 연구)

  • Park, Ki-Ho;Jung, Sang-Jin;Wee, Hyuk;Lee, Gook-Sun;Cho, Seong-Ho
    • Proceedings of the Korean Society for Noise and Vibration Engineering Conference
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    • 2008.11a
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    • pp.84-88
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    • 2008
  • The roller bearings play an important role not only sustain radial or axial load of system, but carry out a rotatory movement as a various operating conditions. They happen that incipient faults which were caused by excessive load, manufacturing or assembling process's errors and many other reasons are created. The bearing faults make noise and vibration by a continuous collision of rotatory components, which can lower the quality and stability of auto-transmission. Therefore, it is important to detect the early fault as soon as possible. This paper presents a detecting method for the improvement in quality by developing the program which can be used to analyze and predict the vibrational characteristics caused by roller bearing faults. We completed development of the inspection system of vibration by appling the most efficient detecting methods and verified the system's reliability through experiments.

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Three-dimensional Rotordynamic Analysis Considering Bearing Support Effects (베어링 지지 효과를 고려한 3차원 로터동역학 해석)

  • Park, Hyo-Keun;Kim, Dong-Man;Kim, Yu-Sung;Kim, Myung-Kuk;Chen, Seung-Bae;Kim, Dong-Hyun
    • Transactions of the Korean Society for Noise and Vibration Engineering
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    • v.17 no.2 s.119
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    • pp.105-113
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    • 2007
  • In this study, three-dimensional rotordynamic analyses have been conducted using equivalent beam, hybrid and full three-dimensional models. The present computational method is based on the general finite element method with rotating gyroscopic effects of the rotor system. General purpose commercial finite element code, SAMCEF which includes practical rotordynamics module with various types of rotor analysis tools and bearing elements is applied. For the purpose of numerical verification, comparison study for a benchmark rotor model with support bearings is performed first. Detailed finite element models based on three different modeling concepts are constructed and then computational analyses are conducted for the realistic and complex three-dimensional rotor system. The results for rotor stability and mass unbalance response are presented and compared with the experimental vibration test data conducted herein.

A case study on the vibration by fluid induced instability at large steam turbine-generator (대형 터빈-발전기에서의 유체 불안정진동 해소사례)

  • Han, Seung-Woo;Noh, Chel-Woo;Kim, In-Chul;Joo, In-Gouk;Kim, Myong-Shik
    • Proceedings of the Korean Society for Noise and Vibration Engineering Conference
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    • 2007.11a
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    • pp.1066-1071
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    • 2007
  • This case study refers to turbine-generator with retrofitted turbine rotor. Vibration problem occurring after the retrofit was mainly due to high vibration from exciter side. However, repeated test run and operation during scheduled maintenance caused high vibration from generator bearing, and post-overhaul test run before turbine vibration correction caused oil whip on the bearing. This case study shows how to analyze vibration condition of high turbine generator vibration detected during the post-overhaul test run and vibration condition of offline and online data to reflect it on establishing maintenance schedule and overhaul correction procedure. Vibration data could be acquired during steady load operation or even with varying speed and load. Each data is important for machinery condition evaluation. This case study shows that the vibration data during extreme condition is the key factor in analysis, which helps to find the machinery problem.

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A Case Study on the Vibration by Fluid Induced Instability at Large Steam Turbine-generator (대형 터빈-발전기에서의 유체 불안정진동 해소사례)

  • Han, Seung-Woo;Roh, Cheol-Woo;Yoo, Mu-Sang;Kim, In-Chul;Joo, In-Gouk;Kim, Myong-Shik
    • Transactions of the Korean Society for Noise and Vibration Engineering
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    • v.18 no.2
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    • pp.238-246
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    • 2008
  • This case study refers to turbine-generator with retrofitted turbine rotor. Vibration problem occurring after the retrofit was mainly due to high vibration from exciter side. However, repeated test run and operation during scheduled maintenance caused high vibration from generator bearing, and post-overhaul test run before turbine vibration correction caused oil whip on the bearing. This case study shows how to analyze vibration condition of high turbine generator vibration detected during the post-overhaul test run and vibration condition of offline and online data to reflect it on establishing maintenance schedule and overhaul correction procedure. Vibration data could be acquired during steady load operation or even with varying speed and load. Each data is important for machinery condition evaluation. This case study shows that the vibration data during extreme condition is the key factor in analysis, which helps to find the machinery problem.