• Title/Summary/Keyword: 시험연소로

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Combustion Stability Test of LRE Thrust Chamber using Artificial Perturbation Method (강제교란 방법을 이용한 액체로켓엔진 연소기의 연소안정성 시험)

  • Lee, Kwang-Jin;Seo, Seong-Hyeon;Han, Yeoung-Min;Choi, Hwan-Seok;Ko, Young-Sung
    • Journal of the Korean Society of Propulsion Engineers
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    • v.14 no.3
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    • pp.52-60
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    • 2010
  • Combustion stability tests of 30 $ton_f$-class LRE thrust chamber with double swirl coaxial injector were carried out in domestic ground combustion test facility by means of artificial perturbation method. In these tests, thrust chambers with varying design factors like recess number of injector, baffle length, types of film cooling and chamber diameter were used and test results showed that these design factors are closely related with high frequency combustion stability. By using the oscillation decrement instead of the decay time in the combustion stability analysis of artificially perturbed LRE thrust chamber, it was confirmed that increment of damping factor results in the improvement of high frequency combustion stability of LRE thrust chamber.

Ignition Characteristics of Combustion Chamber with $LO_X$ Lead Cyclogram for Liquid Rocket Engine (액체로켓엔진 연소기 산화제 선공급 Cyclogram에 의한 점화특성)

  • Han, Yeoung-Min;Kim, Jong-Gyu;Lee, Kwang-Jin;Lim, Byoung-Jik;Ahn, Kyu-Bok;Kim, Mun-Ki;Seo, Seong-Hhyeon;Choi, Hwan-Seok
    • Proceedings of the Korean Society of Propulsion Engineers Conference
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    • 2008.11a
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    • pp.137-142
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    • 2008
  • Ignition characteristics of combustion chamber with LOx lead cyclogram for liquid rocket engine were described. The combustion chamber has chamber pressure of 60 bar, propellant mass flow rate of 89 kg/s, and nozzle expansion of 12. Cold flow test to determine the filling time of propellant for cyclogram with LOx lead supply, ignition test to check the ability to ignite starting fuel from the ignitor, low pressure combustion test to check the propagation of flame into main fuel-oxidizer mixture from starting fuel and the main combustion stage, and design point combustion test to check the combustion performance were performed. Ignition and combustion tests with LOx lead supply were successfully performed and the stable cyclogram of start sequence for combustion chamber was developed.

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Simulating Combustion Tests for the Verification of Baffle Gap of Optimal Damping Characteristics in Liquid Rocket Combustors (로켓연소기에서 최적의 감쇠특성을 보이는 분사기형 배플의 간극 검증을 위한 상압모사연소시험)

  • Kim, Hong-Jip;Lee, Kwang-Jin;Choi, Hwan-Seok
    • Journal of the Korean Society for Aeronautical & Space Sciences
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    • v.36 no.2
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    • pp.179-185
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    • 2008
  • Simulating combustion tests have been performed to elucidate the effect of baffle gaps on the optimal damping characteristics in liquid rocket combustors where coaxial injectors are installed. Amplitude of pressure oscillation in model combustion chamber and the combustion stability margin are used to quantify the damping capacitance of baffles. Satisfactory agreement has been achieved with the results of cold acoustic tests. Present results have shown that the optimal gap for high acoustic damping capacity has also the large combustion stability margin in simulating combustion tests. Therefore, the present results can be utilized to determine the baffle length and optimal gap in full-scaled rocket combustors.

Full Rig Test and High Altitude Ignition Test of Micro Turbojet Engine Combustor (초소형 터보제트엔진 연소기의 리그시험 및 고고도 점화시험)

  • Lee, Dong-Hun;Kim, Hyung-Mo;Park, Poo-Min;You, Gyung-Won;Paeng, Ki-Suk
    • Proceedings of the Korean Society of Propulsion Engineers Conference
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    • 2009.05a
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    • pp.373-376
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    • 2009
  • A full rig combustor test and altitude ignition test were carried out for radial-annular combustor of micro turbojet engine. 11.2% total pressure loss and 99.85% of combustion efficiency were measured at design point of engine under sea level standard condition and $2{\sim}6$ of air excess ratio for ignition envelope was achieved on engine starting regime. Finally, A 30,000 ft high altitude ignition test was also performed and finally we found out that the developed radial-annular combustor is appropriate to micro turbojet engine.

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Preliminary Design of Test Facility for 75-tonf-Class Liquid Rocket Engine Combustor (75톤급 액체로켓엔진 연소기 시험설비 기본설계)

  • Lim, Byoung-Jik;Seo, Seong-Hyeon;Kim, Mun-Ki;Kang, Dong-Hyuk;Han, Yeong-Min;Choi, Hwan-Seok
    • Journal of the Korean Society of Propulsion Engineers
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    • v.14 no.5
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    • pp.84-91
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    • 2010
  • For the successful development of 75-tonf-class liquid rocket engine, a plenty of tests on each engine component have to be performed and this is equally true for a combustor. However the test facility which is in operation at Korea Aerospace Research Institute lacks its capacity to perform fire tests of a 75 tonf class combustor at its nominal thrust. Since the test facility has to be ready prior to the start of development tests, it is very urgent to establish the test facility. The preliminary design of a test facility for a 75 tonf class combustor which was performed according to such a necessity is described in the paper.

Test Facility Improvement for Hot Firing Test of a 7-tonf Combustor in Sub-scale model (7톤급 연소기 축소형 모델 시험을 위한 설비 개량)

  • Kang, Dong-Hyuk;Lim, Byoung-Jik;Kim, Hyeon-Jun;Choi, Hwan-Seok
    • Proceedings of the Korean Society of Propulsion Engineers Conference
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    • 2012.05a
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    • pp.498-501
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    • 2012
  • The Model Rocket Engine Test Facility has been improved to develop the Korea Space Launch Vehicle II(KSLV-II). The modified Model Rocket Engine Test Facility will be used to develop 7-tonf class liquid rocket engine combustor. The test result and test technique acquired from this facility will be used to develop the high performance liquid rocket engine combustor. This paper describes the modified Model Rocket Engine Test Facility for a Sub-scale model test of the 7-tonf class combustor.

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Development and Performance Test of the KSLV-I KM Case (KSLV-I KM 케이스 개발 및 성능 시험)

  • Kil, Gyoung-Sub;Lee, Mu-Guen;Lee, Kyung-Won;Cho, In-Hyun
    • Aerospace Engineering and Technology
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    • v.6 no.2
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    • pp.188-196
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    • 2007
  • A composite case was designed to satisfy the required condition of KSLV-I kick motor system. we performed the structure and combustion tests to insure the reliability of the case before the production of the flight model. The hydraulic, vacuum and non destruction testes as the structure test were carried out to confirm the strength of the components of the case and the characteristics of the thermal and structure were investigated through the ground combustion test.

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Design of High-Frequency Data Acquisition System for Combustor Combustion Test Facility (연소기 연소시험설비 고주파 계측 시스템 설계)

  • Ahn, Kyu-Bok;Kang, Dong-Hyuk;Choi, Hwan-Seok
    • Proceedings of the Korean Society of Propulsion Engineers Conference
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    • 2012.05a
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    • pp.461-464
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    • 2012
  • The high-frequency data acquisition system of the rocket engine test facility has been updated to perform hot-firing tests of 7 ton-class liquid rocket engine combustion chambers which will be used for the third stage of the Korea space launch vehicle II. The paper deals with the design of the updated high-frequency data acquisition system and explains its main functions.

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Assessment of material analysis for Non-flammable of cable (케이블 연소방지제의 재료에 대한 성능평가 기술)

  • Soh, Jin-Joong;Shim, Dae-Sub
    • Proceedings of the KIEE Conference
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    • 2003.07c
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    • pp.1472-1474
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    • 2003
  • 연소방지재(난연테이프, 난연도료, 난연seal, 난연레진, 난연보드 등)란 지중 배전케이블, 접속재 및 통신케이블 등의 외피에 화재확산 방지를 위해 도포하여 사용하는 것으로서 화재 시 발포하거나 단열의 효과가 있어 케이블, 전선 등이 연소하는 것을 지연시킨다. 따라서 본 평가 기술에서는 수직불꽃시험, 산소지수, 저 염소시험, 발연농도, 케이블 허용전류저감률 등 주 재료시험에 대한 시험방법을 검토하고 시험에 적용하여 시험 시 문제점을 도출하여 시험방법을 정립하고자 한다.

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Experiments of Combustion Vibration in the Pilot Furnace for Fossil Power Plant under Combustion Test (I) (화력 발전용 시험연소로의 연소시험 중의 연소진동 실험(I))

  • Ju, Young-Ho;Kim, Cheol-Hong
    • Proceedings of the Korean Society for Noise and Vibration Engineering Conference
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    • 2004.11a
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    • pp.341-344
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    • 2004
  • This paper presents results of test for combustion vibration in the pilot furnace for fossil power plant under combustion test. We measured static pressure variation in the pilot furnace together with air and fuel flow. From test results, it shows that vibration magnitude is affected by air and fuel flow. Also, a finite element analysis using a commercial S/W is performed to calculate acoustic mode of the pilot furnace. These results show that dominant frequency occurred is related to acoustic natural frequency of furnace. After this, it needs to be studied the relation between dominant frequency of combustion vibration and air flow rate.

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