• Title/Summary/Keyword: turbine trip

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Economic Optimization Study for a $125,000m^3$ Class LNG Carrier

  • Lee, Kyu-Yeul;Lee, Dong-Kon;Jung, Ho-Hyun;Lee, Chul-Hee
    • Bulletin of the Society of Naval Architects of Korea
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    • v.21 no.4
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    • pp.1-9
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    • 1984
  • This study is concerned with the economic aspects of $125,000m^3$ class LNG carriers with different propulsion plant such as conventional steam turbine and slow speed diesel engine with reliquefaction plant. The ship's speed and L/B ratio were optimized with criterion of required freight rate(RFR) by using the PROCAL computer program package. In order to investigate the effect of fuel oil price, round trip distance and boil-off rate on the RFR and the optimum speed, sensitivity analysis were also performed.

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Analysis on Hypothetical Multiple Events of mSGTR and SBO at CANDU-6 Plants Using MARS-KS Code (중수로 원전 가상의 mSGTR과 SBO 다중 사건에 대한 MARS-KS 코드 분석)

  • Seon Oh YU;Kyung Won LEE;Kyung Lok BAEK;Manwoong KIM
    • Transactions of the Korean Society of Pressure Vessels and Piping
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    • v.17 no.1
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    • pp.18-27
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    • 2021
  • This study aims to develop an improved evaluation technology for assessing CANDU-6 safety. For this purpose, the multiple steam generator tube rupture (mSGTR) followed by an unmitigated station blackout (SBO) in a CANDU-6 plant was selected as a hypothetical event scenario and the analysis model to evaluate the plant responses was envisioned into the MARS-KS input model. The model includes logic models for controlling the pressure and inventory of the primary heat transport system (PHTS) decreasing due to the u-tubes' rupture, as well as the main features of PHTS with a simplified model for the horizontal fuel channels, the secondary heat transport system including the shell side of steam generators, feedwater and main steam line, and moderator system. A steady state condition was successfully achieved to confirm the stable convergence of the key parameters. Until the turbine trip, the fuel channels were adequately cooled by forced circulation of coolant and supply of main feedwater. However, due to the continuous reduction of PHTS pressure and inventory, the reactor and turbine were shut down and the thermal-hydraulic behaviors between intact and broken loops got asymmetric. Furthermore, as the conditions of low-flow coolant and high void fraction in the broken loop persisted, leading to degradation of decay heat removal, it was evaluated that the peak cladding temperature (PCT) exceeded the limit criteria for ensuring nuclear fuel integrity. This study is expected to provide the technical bases to the accident management strategy for transient conditions with multiple events.

An Expanded Use of Reactor Power Cutback System to Avoid Reactor Trips in the Event of an Inward Control Element Assembly Deviation (제어봉 인입편차시의 원자로 비상정지 방지를 위한 출력 급감발 계통의 확대 적용)

  • Hwang, Hae-Ryong;Ahn, Dawk-Hwan
    • Nuclear Engineering and Technology
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    • v.25 no.2
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    • pp.276-284
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    • 1993
  • The ABB-CE System-80 reactor power cutback system(RPCS) is designed to enable continuous operation of the reactor without trip in the events of the loss of one of the two main feedwater pumps and loss of load, and thus improves plant availability in a cost effective manner. In this study expansion of RPCS has been investigated for continuous reactor operation without trip in the event of an inward control element assembly(CEA) deviation including a single rod drop. Under the expanded function of RPCS the control system will provide a rapid core power reduction on demand by releasing CEAs to drop into the core and reduce the turbine power, if necessary, to follow the reactor power variation. This design feature which is included as the new design features to be incorporated in the ABB-CE System-80+ meets the EPRI advanced light water reactor(ALWR) requirements. For this study core analysis models of System-80+ have been developed to simulate the nuclear steam supply system(NSSS) response as well as the RPCS initiation of rapid CEA insertion. The results of this study demonstrate that the reactor trip can be avoided in the event of inward CEA deviation including a single rod drop by the RPCS initiation and thus the plant availability and capacity factor would be increased.

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Reactor Power Cutback System Test Experience at YGN 4

  • Chi, Sung-Goo;Kim, Se-Chang;Seo, Jong-Tae;Eom, Young-Meen;Wook, Jeong-Dae;Park, Young-Boo
    • Proceedings of the Korean Nuclear Society Conference
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    • 1995.10a
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    • pp.235-241
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    • 1995
  • YGN 3 and 4 are the nuclear power plants having System 80 characteristics with a rated thermal output of 2815 MWth and a nominal net electrical output of 1040 MWe. YGN 3 achieved commercial operation on March 31, 1995 and YGN 4 completed Power Ascension Test (PAT) at 20%, 50%, 80% and 100% power by September 23, 1995. YGN 3 and 4 design incorporates the Reactor Power Cutback System (RPCS) which reduces plant trips caused by Loss of Load (LOL)/Turbine Trip and Loss of One Main Feedwater Pump (LOMFWP). The key design objective of the RPCS is to improve overall plant availability and performance, while minimizing challenges to the plant safety systems. The RPCS is designed to rapidly reduce reactor power by dropping preselected Control Element Assemblies (CEAs) while other NSSS control systems maintain process parameters within acceptable ranges. Extensive RPCS related tests performed during the initial startup of YGN 4 demonstrated that the RPCS can maintain the reactor on-line without opening primary or secondary safety valves and without actuating the Engineered Safety Features Actuation System (ESFAS). It is expected that use of the RPCS at YGN will increase the overall availability of the units and reduce the number of challenges to plant safety systems.

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A Study on the Improved Protective Relaying Algorithm Applied in the Linked System Interconnecting Wind Farm with the Utilities (풍력발전단지 연계 전용선로 보호계전방식의 향상에 대한 연구)

  • 장성일;김광호;권혁완;김대영;권혁진
    • The Transactions of the Korean Institute of Electrical Engineers A
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    • v.52 no.12
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    • pp.675-683
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    • 2003
  • This paper describes the correction strategy of an overcurrent relay applied in the linked line for interconnecting wind farm with utility power networks in order to improve the capability of a fault detection. The fault current measured in a relaying point might vary according to the fault conditions. Generally, the current of the line to line fault or the line to ground fault in the linked line is much higher than the set value of protective relay due to the large fault level. However, when the high impedance fault occurs in the linked line, we can't detect it by conventional set value because its fault level may be lower than the generating capacity of wind farm. And, the protective relay with conventional set value may generate a trip signal for the insertion of wind turbine generators due to the large transient characteristics. In order to solve above problems and improve protective relaying algorithms applied in the linked line, we propose a new correction strategy of the protective relay in the linked line. The presented method can detect the high impedance fault which can't be detected by conventional relay set value and may prevent the mis-operation of protective relay caused by the insertion of wind farm.

Correction of Overcurrent Protective Relay on Distribution Feeders Considering the Power Output of Wind Farm Interconnected with Utility Networks (계통 연계 풍력발전단지의 출력 조건을 고려한 배전선 과전류 계전기 정정)

  • Kim, J.W.;Jang, S.I.;Kim, K.H.;Yoo, N.S.;Park, H.J.;Song, D.S.;Lee, J.M.
    • Proceedings of the KIEE Conference
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    • 2003.07a
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    • pp.342-344
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    • 2003
  • This paper describes the correction of overcurrent protective relaying set value in distribution networks interconnected with wind farm by dedicated line. The wind farm composed of wind turbine generators is one of the great energy sources; however, it would be also highly possible that the current in the point of common coupling is influenced by the output power of wind farm. So, the overcurrent relay applied in distribution feeders might generate trip signal for normal operation. In order to prevent the mal-operation of overcurrent relay, it is necessary to correct the relay's setting value according to the output power of end farm. This paper presents the influence of wind farm on the overcurrent relaying set value in distribution feeders for cases of fault as well as normal operation and proposes the basic strategy for correction of overcurrent relaying set value.

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Loss of a Main Feedwater Pump Test Simulation Using KISPAC Computer Code

  • Jeong, Won-Sang;Sohn, Suk-Whun;Seo, Ho-Taek;Seo, Jong-Tae
    • Nuclear Engineering and Technology
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    • v.28 no.3
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    • pp.265-273
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    • 1996
  • Among those tests performed during the Yonggwang Nuclear Power Plant Units 3 and 4 (YGN 3&4) Power Ascension Test period, the Loss of a Main Feedwater Pump test at l00% power is one of the major test which characterize the capability of YGN 3&4. In this event, one of the two normally operating main feedwater pumps is tripped resulting in a 50% reduction in the feedwater flow. Unless the NSSS and Turbine/Generator control systems actuate properly, the reactor will be tripped on low SG water level or high pressurizer pressure. The test performed at Unit 3 was successful by meeting all acceptance criteria, and the plant was stabilized at a reduced power level without reactor trip. The measured test data for the major plant parameters are compared with the predictions made by the KISPAC computer code, an updated best-estimate plant performance analysis code, to verify and validate its applicability. The comparison results showed good agreement in the magnitude as well as the trends of the major plant parameters. Therefore, the KISPAC code can be utilized for the best-estimate nuclear power plant design and simulation tool after a further verification using other plant test data.

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Acoustic Field Analysis of a Combustor-nozzle System with a Premixing Chamber (예혼합실을 갖는 연소-노즐 시스템의 음향장 해석)

  • Yoon, Myunggon;Kim, Jina;Kim, Daesik
    • Journal of the Korean Society of Propulsion Engineers
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    • v.21 no.5
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    • pp.46-53
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    • 2017
  • This paper deals with an acoustic model for a lean premixed gas turbine combustor composed of three stages: premixing chamber, nozzle and flame tube. Our model is given as an acoustic transfer function whose input is a heat release rate perturbation and output is a velocity perturbation at a flame location. We have shown that the resonance frequencies are functions of three round-trip frequencies of acoustic wave in each stage, and area ratios between stages. By analyzing poles of the acoustic transfer function, we could characterize resonant frequencies and their dependency on various system parameters of a combustor. It was found that our analytic findings match with existing numerical and experimental results in literature.