• Title/Summary/Keyword: static pressure efficiency

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Numerical Analysis on the Effect of Blade Sweep and Lean on the Performance of a Partial Admission Supersonic Turbine (스윕과 린을 적용한 부분흡입형 초음속 터빈의 성능 특성에 관한 수치적 연구)

  • Kwon, Ta-Eun;Jeong, Soo-In;Cho, Jong-Jae;Kim, Kui-Soon;Jeong, Eun-Hwan
    • Proceedings of the Korean Society of Propulsion Engineers Conference
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    • 2010.11a
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    • pp.786-792
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    • 2010
  • The present study deals with numerical flow analysis to investigate the effect of sweep and lean on the performance characteristics of a partial admission supersonic turbine. The flow analysis was performed for three different angles. The angles of sweep and lean are $5^{\circ}$, $10^{\circ}$, $15^{\circ}$. The results of the flow analysis showed that the efficiency is improved as the sweep angle is increased. However, a sweep angle of $5^{\circ}$ was less effective in comparison with the baseline model. The total pressure loss was reduced as the lean angle is increased, but the total to static efficiency was decreased.

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The Status of Maintenance of Exhaust Fans and Bag filters in Melting Processes in a foundry industrial complex (주물 공단 용해공정의 송풍기 및 백필터 관리 실태)

  • Kim, Tae Hyeung;Ha, Hyun Chul;Jeoung, Chun Hwa;Seo, Jeoung Yoon;Piao, Cheng Xu;Yang, Jun Ho;Li, Xiaoyu
    • Journal of Korean Society of Occupational and Environmental Hygiene
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    • v.17 no.3
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    • pp.212-223
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    • 2007
  • 18 Local exhaust ventilation systems in 10 melting companies located in an industrial complex were tested to know the status of maintenance. Test items were fan flowrates, fan static pressures, rotational speeds and differential pressures of bag filters. Only 22% of the tested fans has more than 80% flowrate efficiency. 44% of the fans has lower than 60% efficiency. The performance of the fans are not in a good status. For the fans with lower than 60% efficiency, the analysis shows that the lower flowrate might be caused by the degradation of fan performance. On the other hand, for the fan s with higher than 60% efficiency, the main cause of flowrate reduction might be too much pressure losses due to clogging of filter bags. The degradation of fans usually lead the reduction of hood capture efficiency, resulting in the increase of contaminant concentrations in workplace. To keep fans in good status, self inspections should be periodically conducted. This inspection should include the measurements of flowrate and pressures. The most important thing to be performed is the initial test of local exhaust ventilation system because the initial test data should be used to know the level of system degradation.

A Study of the One-Stage Axial Turbine Performance with Various Axial Gap Distances between the Stator and Rotor (정.동익 축방향 간격에 따른 단단 축류터빈의 성능시험에 관한 연구)

  • Kim, Dong-Sik;Cho, Soo-Yong
    • Journal of the Korean Society for Aeronautical & Space Sciences
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    • v.30 no.4
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    • pp.99-105
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    • 2002
  • The performance test of an axial-type turbine is carried out with various axial gap distances between the stator and rotor. The turbine is operated at the low pressure and speed, and the degree of reaction is 0.373 at the mean radius. The axial-type turbine consists of ons-stage and 3-dimensional blades. The chord length of rotor is 28.2mm and mean diameter of turbine is 257.56mm. The power of turbo-blower for input power is 30kW and mass flow rate is $340m^3$/min at 290mmAq static-pressure. The RPM and output power are controlled by a dynamometer connected directly to the turbine shaft. The axial gap distances are changed from a quarter to three times of stator axial chord length, and performance curves are obtained with 9 different axial gaps. The efficiency varies about 8% of its peak value due to the variation of axial gap on the same non-dimensional mass flow rate and RPM, and experimental results show that the optimum axial gap is 1.6-1.9Cx.

Design and Analysis of a Radial Turbine for Ocean Thermal Energy Conversion (해양온도차발전용 반경류 터빈의 설계 및 해석)

  • Nguyen, Van Hap;Lee, Geun Sik
    • Transactions of the Korean Society of Mechanical Engineers B
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    • v.39 no.3
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    • pp.207-214
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    • 2015
  • The preliminary design of a radial inflow turbine using R134a as the working fluid at 5 kW of power for application to ocean thermal energy conversion (OTEC) is performed to obtain the trends for the efficiency and geometrical dimensions of the turbine. Using input conditions that included a turbine inlet temperature of $25^{\circ}C$, an outlet static pressure of 4.9 bar, and a mass flow rate of 1.16 kg/s, the results of a mean flow analysis show the major dimensions of the turbine, along with an angular velocity of 12,820 rpm. Based on these results, a three-dimensional turbine model is constructed for a computational fluid dynamics (CFD) analysis. The flow characteristics inside the turbine, including the volute and nozzle, are investigated using the CFD software ANSYS CFX. For a pertinent number of nozzle guide vanes, ranging from 10 to 15, the turbine efficiency was higher than 80%, with the highest efficiency shown by a nozzle with 15 guide vanes.

Analysis of Propylen Chlorohydrin in Hydroxypropyl Distarch Phosphate by Accelerated Solvent Extractor (ASE) (가속화용매추출기를 이용한 히드록시프로필인산이전분의 프로필렌클로로히드린 분석방법에 관한 연구)

  • Lee, Myung-Ja;Sin, Yeong-Min;Jeong, Eui-Han;Choi, Tae-Jin;Chung, Sook-Hyun;An, Won-Gun
    • Journal of the Korean Society of Food Science and Nutrition
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    • v.31 no.4
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    • pp.604-608
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    • 2002
  • Accelerated solvent extraction (ASE) was used for a rapid and simple extraction of propylenchlorohydrin (PCH) residue in hydroxylpropyl modified starch. The effects of temperature, pressure and extraction solvent on the extraction efficiency were investigated to find the optimal condition of ASE. The optimal conditions for PCH extraction in hydroxylpropyl modified starch were static time of 50 min, purge time of 300 sec, heating time of 5min, temperature of 12$0^{\circ}C$, pressure of 2500 psi, flush (%) with 100 volumes, and ethylacetate as an extraction solvent. The recovery (96.1%) of this method was higher than that (76.4%) of Code of Food Additive. Therefore, the ASE was a good method in both aspects of efficiency and effectiveness.

Investigation of dust particle removal efficiency of self-priming venturi scrubber using computational fluid dynamics

  • Ahmed, Sarim;Mohsin, Hassan;Qureshi, Kamran;Shah, Ajmal;Siddique, Waseem;Waheed, Khalid;Irfan, Naseem;Ahmad, Masroor;Farooq, Amjad
    • Nuclear Engineering and Technology
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    • v.50 no.5
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    • pp.665-672
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    • 2018
  • A venturi scrubber is an important element of Filtered Containment Venting System (FCVS) for the removal of aerosols in contaminated air. The present work involves computational fluid dynamics (CFD) study of dust particle removal efficiency of a venturi scrubber operating in self-priming mode using ANSYS CFX. Titanium oxide ($TiO_2$) particles having sizes of 1 micron have been taken as dust particles. CFD methodology to simulate the venturi scrubber has been first developed. The cascade atomization and breakup (CAB) model has been used to predict deformation of water droplets, whereas the Eulerian-Lagrangian approach has been used to handle multiphase flow involving air, dust, and water. The developed methodology has been applied to simulate venturi scrubber geometry taken from the literature. Dust particle removal efficiency has been calculated for forced feed operation of venturi scrubber and found to be in good agreement with the results available in the literature. In the second part, venturi scrubber along with a tank has been modeled in CFX, and transient simulations have been performed to study self-priming phenomenon. Self-priming has been observed by plotting the velocity vector fields of water. Suction of water in the venturi scrubber occurred due to the difference between static pressure in the venturi scrubber and the hydrostatic pressure of water inside the tank. Dust particle removal efficiency has been calculated for inlet air velocities of 1 m/s and 3 m/s. It has been observed that removal efficiency is higher in case of higher inlet air velocity.

Analysis and Performance Test for the Fan of a Wide Area Sprayer of Livestock Farm (축산 농가용 광역방제기 팬의 성능실험 및 분석)

  • Hong, J.T.;Min, B.R.;Kim, D.W.;Seo, K.W.;Kim, W.;Lee, S.K.;Kim, S.Y.;Lee, D.W.
    • Journal of Animal Environmental Science
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    • v.13 no.2
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    • pp.105-112
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    • 2007
  • This research was carried out to test and analyse the capability of a fan for development of a sprayer in actual livestock farm. A fan was designed and made to be able to spray agricultural chemicals within 140mm in a maximum scattering range and 100m in an effective scattering range. Accordingly, its' flow rate was $3,600\;m^3/min$, and static pressure was 100 mmAq for a wide area sprayer to be sprayed widely and far. Fan performance, which was given $600\;m^3/min$ flow rate and 500 mmAq total pressure, was tested fur basic experiment. As the result, the axial power showed minimum error, which be designed to keep the fan performance. And power efficiency was the maximum. Sound level was 92.1dB that wasn't enough to environmental standard. If we take the sealed place into consideration, sound level is suitable for environmental standard.

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Development of The New High Specific Speed Fixed Blade Turbine Runner

  • Skotak, Ales;Mikulasek, Josef;Obrovsky, Jiri
    • International Journal of Fluid Machinery and Systems
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    • v.2 no.4
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    • pp.392-399
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    • 2009
  • The paper concerns the description of the step by step development process of the new fixed blade runner called "Mixer" suitable for the uprating of the Francis turbines units installed at the older low head hydropower plants. In the paper the details of hydraulic and mechanical design are presented. Since the rotational speed of the new runner is significantly higher then the rotational speed of the original Francis one, the direct coupling of the turbine to the generator can be applied. The maximum efficiency at prescribed operational point was reached by the geometry optimization of two most important components. In the first step the optimization of the draft tube geometry was carried out. The condition for the draft tube geometry optimization was to design the new geometry of the draft tube within the original bad draft tube shape without any extensive civil works. The runner blade geometry optimization was carried out on the runner coupled with the draft tube domain. The blade geometry of the runner was optimized using automatic direct search optimization procedure. The method used for the objective function minimum search is a kind of the Nelder-Mead simplex method. The objective function concerns efficiency, required net head and cavitation features. After successful hydraulic design the modal and stress analysis was carried out on the prototype scale runner. The static pressure distribution from flow simulation was used as a load condition. The modal analysis in air and in water was carried out and the results were compared. The final runner was manufactured in model scale and it is going to be tested in hydraulic laboratory. Since the turbine with the fixed blade runner does not allow double regulation like in case of full Kaplan turbine, it can be profitably used mainly at power plants with smaller changes of operational conditions or in case with more units installed. The advantages are simple manufacturing, installation and therefore lower expenses and short delivery time for turbine uprating.

Characteristics of Energy Dissipation in Nano Shock Suspension System Using Silica Gel (세라믹 분말을 이용한 나노 충격 완화 장치의 에너지 소산 효율 특성에 대한 연구)

  • 문병영;정성원
    • Journal of the Earthquake Engineering Society of Korea
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    • v.7 no.3
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    • pp.17-22
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    • 2003
  • This paper presents an experimental investigation of a reversible colloidal seismic damper, which is statically loaded, The porous matrix is composed from silica gel (labyrinth or central-cavity architecture), coated by organo-silicones substances, in order to achieve a hydrophobic surface. Water is considered as associated lyophobic liquid. Reversible colloidal damper static test rig and the measuring technique of the static hysteresis are described. Influence of the pare and particle diameters, particle architecture and length of the grafted molecule upon the reversible colloidal damper hysteresis is investigated, for distinctive types and mixtures of porous matrices, Variation of the reversible colloidal damper dissipated energy and efficiency with temperature, pressure, is illustrated.

Design and Prediction of Three Dimensional Flows in a Low Speed Highly Loaded Axial Flow Fan

  • Liu, Xuejiao;Chen, Liu;Dai, Ren;Yang, Ailing
    • International Journal of Fluid Machinery and Systems
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    • v.6 no.2
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    • pp.94-104
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    • 2013
  • This paper describes the design to increase the blade loading factor of a low speed axial flow fan from normal 0.42 to highly loaded 0.55. A three-dimensional viscous solver is used to model the flows in the highly-loaded and normal loaded stages over its operation range. At the design point operation the static pressure rise can be increased by 20 percent with a deficit of efficiency by 0.3 percent. In the highly loaded fan stage, the rotor hub flow stalls, and separation vortex extends over the rotor hub region. The backflow, which occurs along the stator hub-suction surface, changes the exit flow from the prescribed axial direction. Results in this paper confirm that the limitation of the two dimensional diffusion does not affect primarily on the fan's performance. Highly loaded fan may have actually better performance than its two dimensional design. Three dimensional designing approaches may lead to better highly loaded fan with controlled rotor hub stall.