• 제목/요약/키워드: state retaining reduced model

검색결과 2건 처리시간 0.014초

저차원제어기로부터 상태변수를 재구성하는 방법 (Reconstruction of the state variables from the low order controller)

  • 정광영
    • 제어로봇시스템학회논문지
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    • 제4권1호
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    • pp.19-25
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    • 1998
  • 발란싱 축소모델의 상태변수는 플랜트의 상태변수에 대한 정보를 주지 못한다. 발란싱 축소모델을 좌표 변환하여 얻은 상태유지 축소모델은 그 축소오차가 발란싱 축소모델의 축소오차와 같음을 증명하였다. 상태축소오차를 정의하였고, 이 오차를 구하는 방법을 제시하였는데, 이 오차는 축소모델의 차수가 정해지면 불변임을 증명하였다. 상태유지 축소모델의 상태변수는 그 상태축소오차가 작은 경우 원 시스템의 상태변수를 근사하는 장점이 있다. 상태유지 축소모델을 저차원제어기 설계에 적용하여 저차원 상태변수가 플랜트의 상태변수를 근사하는 예를 보여주었다.

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흙 필터재의 폐색으로 인한 투수성 저하 모델 개발 (Modelling of Permeability Reduction of Soil Filters due to Clogging)

  • 이인모;박영진
    • 한국지반공학회:학술대회논문집
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    • 한국지반공학회 1999년도 가을 학술발표회 논문집
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    • pp.271-278
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    • 1999
  • Soil filters are commonly used to protect the soil structures from eroding and piping. When filters are clogged by fine particles which are progressively accumulated, these may lead to buildup of excessive pore pressures also leading to instability in subsurface infrastructure. A filter in the backfill of a retaining wall, a filter adjacent to the lining of a tunnel, or a filter in the bottom of an earth dam can be clogged by transported fine particles. This causes reduction in the permeability, which in turn may lead to intolerable decreases in their drainage capacity. In this thesis, the extent of this reduction is addressed using results from both experimental and theoretical investigations. In the experimental phase, the permeability reduction of a filter is monitored when an influent of constant concentration flows into the filter (uncoupled test), and when the water flow through the soil-filter system to simulate an in-situ condition (coupled test), respectively. The results of coupled and uncoupled test are compared with among others. In the theoretical phase of the investigation, a representative elemental volume of the soil filter was modeled as an ensemble of capillary tubes and the permeability reduction due to physical clogging was simulated using basic principles of flow in cylindrical tubes. In general, it was found that the permeability was reduced by at least one order of magnitude, and that the results from the uncoupled test and theoretical investigations were in good agreement. It is observed that the amount of deposited particles of the coupled test matches fairly well with that of the uncoupled test, which indicates that the prediction of permeability reduction is possible by preforming the uncoupled test instead of the coupled test, and/or by utilizing the theoretical model.

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