• Title/Summary/Keyword: mold insert

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A technical study on mold construction development for junction improvement and productivity improvement of Double-Injection molding (이중사출의 접합성 개선 및 생산성향상을 위한 금형구조 개발기술연구)

  • Kim, O.R.;Lee, S.Y.;Kim, Y.K.;Woo, C.K.;Han, I.Y.
    • Design & Manufacturing
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    • v.2 no.6
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    • pp.49-55
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    • 2008
  • Double-injection molding can inject two different materials or two colors in the same mold and process. If this injection process use, product has ability because the base part maintain strength and specified part can inject soft-material. It makes the cost down by single operation automatically for saving wages. In this paper, we designed double-injection mold for automobile remote control to inject secondary using this part as insert after inject external appearance of product. CAE analysis was progressed gate location and runner size as variable and analysis result is reflected in mold design process. As a result, it could solved badness that is generated at the conventional mold. Additionally, cost is downed by reducing loss of runner as well as could omit painting process because surface of finished product is improved through new mold.

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A Study of Mold Technology for Manufacturing of CFRTP Parts (CFRTP 부품제조를 위한 금형 및 성형 기술에 대한 연구)

  • Jung, Eui-Chul;Kim, Jong-Sun;Son, Jung-Eon;Yoon, Kyung-Hwan;Lee, Sung-Hee
    • Design & Manufacturing
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    • v.11 no.3
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    • pp.25-28
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    • 2017
  • The production of carbon fiber reinforced thermoplastics(CFRTP) parts using an injection/compression molding process that differs from the conventionally used fabrication methods was investigated Before the application of composite molding in the injection/compression molding process, a simple compression molding experiment was performed using a hydraulic press machine to determine the characteristics of resin impregnation and to obtain a basic physical property data for the CFRTP. Based on these results, injection/compression molded specimens were manufactured and an additional insert/over molding process was applied to improve the impregnation rate of the molded specimens. The results demonstrated that the tensile strength of the molded parts using the faster injection/compression process was similar to that of a hydraulic press molded product.

Innovations in Micro Metal Injection Molding Process by Lost Form Technology

  • Nishiyabu, Kazuaki;Kanoko, Yasuhiro;Tanaka, Shigeo
    • Proceedings of the Korean Powder Metallurgy Institute Conference
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    • 2006.09a
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    • pp.43-44
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    • 2006
  • The production method of micro sacrificial plastic mold insert metal injection molding, namely ${\mu}-SPiMIM$ process has been proposed to solve specific problems involving the miniaturization of MIM. Two types of sacrificial plastic molds (SP-mold) with fine structures were used: 1) PMMA resist, 2) PMMA mold injected into Ni-electroform, which is a typical LIGA (${\underline{L}}ithographie-{\underline{G}}alvanoformung-{\underline{A}}bformung$) process. Stainless steel 316L feedstock was injection-molded into the SP-molds with multi-pillar structures. This study focused on the effects of metal particle size and processing conditions on the shrinkage, transcription and surface roughness of sintered parts.

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Improvement of Insert Molding for Refrigerator Glass Shelves Using Numerical Analysis (수치해석을 이용한 냉장고용 유리선반 성형용 인서트 금형의 개선)

  • Han, Seong-Ryeol
    • Journal of the Korean Society of Manufacturing Process Engineers
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    • v.15 no.6
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    • pp.50-57
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    • 2016
  • Refrigerator glass shelves are manufactured by Insert Injection Molding. The current process of injection of glass into the mold induces movement of the core, on urethane springs. Defects in the product can result from too low a force being transmitted from the springs. To solve this problem, the force on the moving core and the injection molding pressure were subjected to numerical analysis. Based on this, the number of urethane springs as well as their hardness was changed to improve the situation. The number of springs was changed from 6 to 4. The diameter of the springs was increased from ${\emptyset}75$ to ${\emptyset}100$, and the hardness was increased from 70 (shore A) to 90 (shore A). These improvements caused the force on the molding core to increase by approximately 65,442 N. The proportion of defects decreased by 66%.

Mold-design Verification of Ball Housing Insert Die in Non Processing Type Multi-stage Cold Forging (다단냉간단조 비가공 타입에서 볼하우징 인서트 다이의 금형설계 검증)

  • Hwang, Won-Seok;Choi, Jong-Won;Jung, Eu-Enn;Kang, Myungchang
    • Journal of the Korean Society of Manufacturing Process Engineers
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    • v.20 no.12
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    • pp.8-15
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    • 2021
  • Cold forging is a method in which molding is performed at room temperature. It has a high material recovery rate and dimensional precision and produces excellent surface quality, and it is mainly used for the production of bolted or housing products. The lifespan of cold forging molds is generally determined by the wear of the mold, plastic deformation of the mold, and fatigue strength. Cold forging molds are frequently damaged due to fatigue destruction rather than wear and plastic deformation in a high-temperature environment as it is molded at room temperature without preheating the raw material and mold. Based on the results analyzed through FEM, an effective mold structure design method was proposed by analyzing the changes in tensile and compressive stresses on molds according to the number of molds and reinforcement rings and comparing the product geometry and mold stress using three existing mold models.

A study on the development of Gas-Vent Automatic Exchange Machine with Vision System (영상정보를 이용한 가스벤트자동교환 장치)

  • Kwon, Jang-Woo;Hong, Jun-Eui;Yoon, Dong-Eop;Kil, Gyung-Suk;Lee, Dong-Hoon;Lee, Dong-Hoon
    • Journal of the Korea Institute of Information and Communication Engineering
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    • v.11 no.6
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    • pp.1141-1149
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    • 2007
  • This paper describes two major techniques; image processing and gas vent insert and rejection control, for efficient gas vent exchange and holes detecting on the shoes mold. The key idea is to detect holes on the mold to select which holes to insert and to reject automatically guide center of hole's position. This allows us to save labor time while minimizing defective rate of PU shoes mold forming and production costs for gas vent exchange such as insertion and rejection.. Our experimental results have demonstrated that the hole's detection and gasvent exchange mechanism are more efficient and provide accurate mechanism to mitigate risks of vent injection/rejection failures.

A Study on the Runner and Gate Consequence of Manufacture Double Shot Molding using CAE (CAE 를 이용한 이중사출 제품의 러너 및 게이트 영향에 대한 연구)

  • Kim, O.R.;Cha, B.S.;Lee, S.Y.;Kim, Y.G.;Woo, C.K.
    • Transactions of Materials Processing
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    • v.18 no.2
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    • pp.160-165
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    • 2009
  • A Study on Effects of the Runner and the Gate of double shot injection molded Parts using CAE Double shot injection molding can inject two different materials or two different colors in the same mold in a injection molding process. Double shot injection molded parts can be characterized that the base part maintains strength and specified part can inject soft-material. It can reduce the production cost by single automatic operations. In this paper, we designed double shot injection mold for automobile emote control To inject secondary part, this part is used as an insert after external appearance of product is injected. CAE analysis was progressed gate location and runner size as variables. The analysis result is reflected in mold design process. As a result, it could solve problems which are generated in the conventional mold. Additionally, cost can be downed by reducing runner weight. As well as it could omit painting process because the surface of finished product is improved through new mold.

Development of double injection mold for fuel-tube holder (자동차 연료튜브 홀더용 이중사출 금형·성형기술)

  • Kim, Gun-Hee;Yoon, Gil-Sang;Heo, Young-Moo;Jung, Woo-Chul;Shin, Kwang-Ho
    • Design & Manufacturing
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    • v.1 no.1
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    • pp.1-5
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    • 2007
  • Double injection molding process is very efficient molding-method for molding the products which is consist of multi-materials. Fuel-tube holder which is necessary for automobil power train and circulation systems is composed of plastic and rubber materials to minimize the vibration and pulsation noises. In existing process, fuel-tube holder was made by the insert molding process or assembly process after molding. If fuel-tube holder is manufactured by double injection molding process, it may be realize to improve the product quality, efficiency of molding-process and retrenchment of manufacturing cost. In this study, for manufacturing fuel-tube holder by double injection molding process, the analysis of joining characteristics between PA6(polyamide 6) and TPE(thermoplastic elastomer) was executed and the double injectin mold for molding fuel-tube holder with core toggle mechanism was fabricated. Finally, fuel-tube holder was molding using fabricated double injection mold.

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A Study on Polycarbonate Microfabrication Using a Pneumatic Hot Press (공압 핫프레스를 이용한 마이크로 폴리카보네이트 성형에 관한 연구)

  • Yeo, Changyeong;Park, Taehyun
    • Journal of the Korean Society of Manufacturing Process Engineers
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    • v.20 no.4
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    • pp.106-112
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    • 2021
  • Thermoplastic microfluidic devices are used in BioMEMS for medical and biotechnology applications, such as gene extraction, DNA analysis, and virus detection. In this research, a simple fabrication protocol with a commercially available pneumatic hot press is proposed and demonstrated for polycarbonate microfluidic devices. Microfluidic channels with a width of 200 ㎛ and a height of 10 ㎛ were designed and machined onto a brass plate as a mold insert using a CNC milling machine. The resulting microfluidic channels on the mold insert were assessed and found to have an actual width of 198 ㎛ and a height of 10 ± 0.25 ㎛. The microfluidic channels were replicated on a polycarbonate sheet using the proposed replication technique at 146℃ for 20 minutes under a constant load of 2400 kgf. The devices were then naturally cooled to 100℃ while maintaining the same pressure. It was found that the microchannels were successfully replicated in the polycarbonate, with a width of 198 ㎛ and a height of 10.07 ㎛. The proposed replication technique thus offers the rapid mass production of high-quality microfluidic devices at a low cost with a process that, unlike conventional photolithography systems, does not require expensive equipment.

Filling Imbalance of Elastomer TPVs in Injection Mold with Multi-Cavity (다수캐비티 사출금형에서 엘라스토머 TPV의 충전 불균형)

  • Han, Dong-Yeop;Kwon, Yun-Suk;No, Byeong-Su;Jeong, Yeong-Deug
    • Journal of the Korean Society for Precision Engineering
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    • v.24 no.2 s.191
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    • pp.41-46
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    • 2007
  • Recently, the study for filling imbalance in thermoplastic polymer has gradually been increased. However, it is hard to find the researches for filling imbalance of thermoplastic elastomer(TPE). The experiment of filling imbalance was conducted for the three kinds of thermoplastic vulcanizes(TPVs) in the mold with geometrically balanced runner system. In this experiment, the effects of the melt temperature and injection speed on the filling imbalance were investigated. To solve the filling imbalance, Runner Core pin(RC pin) in the experimental mold was adopted and it's effects was tested. In this paper, we present that the insert length of RC pin is dependent to each polymers for optimal filling balance.