• Title/Summary/Keyword: concrete quality

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An Application of the Mass Concrete Using Ternary Blended Cement (3성분계 시멘트를 사용한 매스콘크리트의 시공사례)

  • 권영호;하재담;전성근;김무한
    • Proceedings of the Korea Concrete Institute Conference
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    • 2001.11a
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    • pp.1229-1234
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    • 2001
  • The bottom slab of Inchon LNG in-ground #213 tank is designed as a massive structure witch has a large depth and section. The purpose of this study is to determine the optimum mix design having good workability and low hydration heat for bottom slab concrete and to control the actual concrete quality in site. For this purpose, we select the optimum mix design used ternary blended cement(furnace slag cement+fly ash) and design factors. As test results of actual application, we have finish placing the bottom slab concrete of 23,180㎥ during 68hours with good success and obtain the good quality of fresh and hardened concrete including slump, air contents, no-segregation, compressive strength and low hydration heat in actual data. All test results are satisfied with our specifications for bottom slab concrete and we cut costs as the use of ternary blended cement and the reduction of placing hours.

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An Application of Mat Foundation using Self Compacting Concrete (무다짐 콘크리트를 이용한 두께 3.5m인 대형 Mat 기초의 시공)

  • 손유신;이승훈;박찬규;김규동
    • Proceedings of the Korea Concrete Institute Conference
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    • 2002.05a
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    • pp.979-984
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    • 2002
  • The mat foundation of Tower Palace III is designed as a massive structure which has a 3.5m depth. The purpose of this study is to determine the optimum mix design having good workability and to control the actual concrete quality in site. For this purpose, we select the Self Compacting Concrete. Recently, the Self Compacting Concrete has been applied to achieve workability improvement. As the result of actual application, we have finished placing the mass concrete of 8, 000m$^3$ during 14hours with good success and obtain the good quality concrete. All test results are satisfied with our specifications for mat foundation and cut cost as the reduction of placing hours.

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The On-site Quality Characteristics of the Cold Weather Concrete using High Early Strength Portland Cement (조강포틀랜드시멘트를 사용한 한중콘크리트의 현장품질 특성)

  • Lee, Won-Am;Um, Tae-Sun;Ryu, Jae-Sang;Lee, Jong-Ryul;Kang, Ji-Hun
    • Proceedings of the Korea Concrete Institute Conference
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    • 2004.05a
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    • pp.224-227
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    • 2004
  • The cement can be influenced by the temperature. Especially, when it is cold weather, it causes some problems in such properties as mixing, placing and curing of concrete. According to the Concrete Standard Specification(2003), in case of the average daily outdoor temperature below $4^{\circ}C$, it recommends to use the cold weather concrete. In this research, the on-site quality characteristics of the cold weather concrete using high early strength portland cement(Type III cement) were studied. As a result, the cold weather concrete using high early strength portland cement can obtain its excellent properties and benefit the cost of construction.

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Study on the Development and Field Application of Glossing Exposure Concrete (광택노출콘크리트의 개발 및 실용화 연구)

  • 하재담;정태웅;이현희;공양식;강창운;정일모
    • Proceedings of the Korea Concrete Institute Conference
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    • 1998.04a
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    • pp.249-254
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    • 1998
  • Recently, high quality architectural concrete, i.e., appearance of natural stone and a marbling effect, is needed, to achieve high quality glassy reflective surface for outer wall of the building. In this study to achieve above characteristics of the "glossing exposure concrete" we developed a form practice and the best mix proportion and derived the optimistic removal time of form to bring out the durable glassy reflective surface and durable concrete. Hereby with the "glossing exposure concrete" obtained we applicate for first time, to Electronics and Telecommunications Research Institute situated on Taedok Science Town and it will be the beginning of the construction of "glossing exposure concrete" in this country.oncrete" in this country.ntry.

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An Experimental Study on the Quality of High Flowing Concrete according to Ignition Loss of Fly-ash (플라이애쉬의 미연탄소 함유량에 따른 고유동콘크리트의 품질에 관한 실험적 연구)

  • 신흥철;강희관;최세진;김규용;김진만;김무한
    • Proceedings of the Korea Concrete Institute Conference
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    • 1997.10a
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    • pp.381-384
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    • 1997
  • It is necessary for manufacturing the high flowing to use the fly-ash as binder of concrete, therefore, Quality of fly-ash is very important to the fluidity of high flowing concrete. In this study, it is comparing and investigating the fludity of high flowing concrete used some fly-ash which it's Ignition loss is 2.44, 4.90, 7.10%. As a result of this experimental study, Ignition loss of fly-ash effects the properties of high flowing concrete, such as air content, flowability, passability etc. but even if valve of ignition loss is upper the specification, properties of high flowing concrete such as setting and hardening time, compressive strength etc.

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Concrete Recycling considering Risk Evaluation of Impurities in Recycled Aggregate (순환골재 불순물의 위험성을 고려한 콘크리트 리사이클링)

  • Park, Won-Jun
    • Proceedings of the Korean Institute of Building Construction Conference
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    • 2012.05a
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    • pp.95-97
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    • 2012
  • Recycled aggregate (RA) produced from demolished concrete waste can bring about several problems on concrete performance, when it is used as aggregate for new concrete. Because RA generally has lower quality than natural aggregate due to the residual cement paste attached on RA and various impurities. It is also very difficult to ensure that the quality of RA remains consistent, because generally RA is produced variously. Thus, in concrete recycling, it is extremely important to estimate the risk of the impurities which could affect performances of recycled aggregate concrete (RAC) focusing on the material flow of concrete waste and its recycling. This study suggests an evaluation result to expect the possibility of impurity mixing in RA production procedure. and suggests a risk evaluation model to expect the changes of RAC performances based on conventional data in Japan.

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An Experimental Study on the Engineering Properties of the Three Components Middle Fluidity Concrete (3성분계 중유동 콘크리트의 공학적 특성에 관한 실험적 연구)

  • 김갑수;조봉석;윤종기;윤문기;장종호;김무한
    • Proceedings of the Korean Institute of Building Construction Conference
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    • 2003.05a
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    • pp.9-12
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    • 2003
  • High flowing concrete has not spread whole in the normal concrete structure, because it requires special quality control technique. And recently owing to the lack of natural resources and reinforcement of environmental standard, the construction cost of cement is increased rapidly. Also remicon industry has gone through various economical difficulty as the manufacture cost of concrete is increased. So, the purpose of this study is to evaluate the qualities of middle fluidity concrete using the fly-ash and portland blast-furnace slag cement in order to decrease the amount of cement and resolve the problem of the quality control of high flowing concrete and the manufacture cost. The results of this study show that it reduce the amount of addition of superplasticizer and develope properties of concrete to the use the fly-ash and portland blast-furnace slag cement.

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Effects of Curing Method on the Mechanical Properties of Recycled Coarse Aggregate Concrete (양생방법에 따른 순환굵은골재 콘크리트의 강도특성)

  • Jeon, Esther;Yun, Hyun-Do;You, Young-Chan;Lee, Sea-Hyun;Shim, Jong-Woo;Choi, Ki-Sun
    • Proceedings of the Korea Concrete Institute Conference
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    • 2006.11a
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    • pp.525-528
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    • 2006
  • Recently, Korea government prepared Act on facilitation of construction waste recycling in December 2003 for effective recycling of rapidly increasing construction wastes, and has enforced the Act on Jan. 2005. This Act limits the definition of recycled aggregates to the aggregates which obtained quality certificate and for this purpose, government has operated quality standard and certificate system of recycling aggregate. The objective of this experimental study is to evaluate the mechanical properties of recycled coarse aggregate concrete according to curing method by ready-mixed concrete. Compressive strength ratio of recycled aggregate concrete under air-dry curing/wet curing was $74{\sim}91%$. KCI code for conventional concrete overestimated elastic modulus for recycled coarse aggregate concrete.

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Investigation of Internal Temperature and Relative Humidity of Concrete Immediately After Mix and Placement (양생직후 초기재령의 콘크리트 내부 온도와 상대습도의 측정 및 분석)

  • Park, Cheol-Woo;Park, Young-Hoon;Park, Yong-Gul
    • Proceedings of the KSR Conference
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    • 2008.11b
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    • pp.1065-1068
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    • 2008
  • Concrete is still one most common construction materials even in railway structures. As structures become massive and mega-sized, the importance of early age concrete quality control becomes more significant. Among various factors, relative humidity and temperature are the primary factors governing the early age quality. Temperature raise due to cement hydration causes stress, which can develop to cracking with internal and/or external restraints. Exposure conditions including ambient temperature, humidity and wind also significantly affect the cracking behavior of early age concrete. Among many of studies on the early age concrete behavior, investigation on the variation of temperature and relative humidity internal of concrete is not common. That is in part because the difficulties in measuring the relative humidity and temperature inside the concrete. This study used a digital sensor with an appropriate logger to measure internal temperature and relative humidity. This direct measuring method is expected to provide more reliable and comprehensive data acquisition on the early age behavior of concrete.

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The Development of Normal Strength-High Fluidity Concrete to Improve Compaction of Concrete Wall and Flatness of Slab (충전성 및 평탄도 개선을 위한 일반강도 중유동 콘크리트 개발)

  • Kim, Yong-Ro;Park, Jong-Pil;Kim, Rae-Hwan
    • Proceedings of the Korean Institute of Building Construction Conference
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    • 2022.04a
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    • pp.55-56
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    • 2022
  • Recently, water leak is increasing due to poor compaction or segregation of concrete on external wall. In addition, the flatness quality of the slab is lowered due to the deterioration of the workability of concrete. In this study, the performance of high fluidity concrete of 21MPa using a polycarboxylate-based superplasticizer was evaluated to improve the compaction and quality of the concrete wall.

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