• 제목/요약/키워드: Shedding frequency

검색결과 272건 처리시간 0.024초

발전용 보일러 후부 전열면 소음진동 저감에 관한 연구 (A Case Study on the Reduction of Noise and Vibration at the Backpass Heat Surface in the Power Plant Boiler)

  • 이경순;이태구;문승재;이재헌
    • 플랜트 저널
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    • 제4권3호
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    • pp.54-59
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    • 2008
  • The resonance of boiler is caused by exciting force in the gas path and it generates the vibration by the harmony of boiler's dimensional factor. According to trending toward the boiler of increasing capacity and a bigger size, it has a problem of the vibration at back-pass heating surfaces. We can predict such vibrations as comparison between vortex frequency and gas column's natural frequency. We can't rely on the method for the past decades because of changing parameters, such as an allowable error, gas temperature, gas velocity, Strouhal number. We can reduce the vibration to use the seasoning effect and change the operating condition in coal fired boiler but it's not essential solution. When the vibration occurred in the model boiler, we must measures the acoustic pressure and frequency of places for considering the means. So far, we confirmed the problem from field measures and theoretical analysis about the acoustic vibration of boiler. We installed anti-acoustic baffle in a existing boiler to change the acoustic natural frequency at the cavity, which results in reducing the acoustic vibration. The first, we prove that the acoustic resonance is caused by harmonizing vortex shedding frequency of tube heat surface with acoustic natural frequency of cavity in the range of 650~750 MW loads. The second, the acoustic resonance at the back-pass heating surface has the third order of acoustic natural frequency at the second economizer. We install five anti-acoustic baffles at the second economizer to reducing the resonance. We confirm considerably reducing the acoustic vibration of boiler during the commercial boiler.

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연소실 형상 변화에 의한 하이브리드 로켓의 저주파수 연소불안정 (Low frequency Instability in Hybrid Rocket Post-chamber Configuration)

  • 박경수;이창진
    • 한국항공우주학회지
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    • 제42권1호
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    • pp.29-36
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    • 2014
  • 하이브리드 로켓 연소에서는 다양한 종류의 저주파수 연소 압력진동이 나타난다. 10Hz 대역의 저주파수 압력진동은 고체연료와 연소가스의 열 관성 차이 때문에 발생하지만 그외의 저주파수 진동은 고체로켓에서 관찰되는 헬름홀츠 및 $L^*$ 모드에 의해 발생하는 것으로 연소실 부피 변화와 밀접한 관련이 있다. 따라서 유동 특성이 고체로켓과 유사한 하이브리드 로켓 연소에서 연소실 부피 변화는 저주파수 특성에 영향을 미치는 중요한 인자이다. 본 연구에서는 연소실과 후연소실의 형상 변화에 따른 연소 압력의 저주파수 특성 변화를 관찰하였다. 특히 주 연소실과 후연소실의 부피 비가 특정한 값이 되면 연소 도중에 10~30Hz 연소 압력 진동의 진폭이 갑자기 증폭되는 연소불안정 현상이 나타났다. 산화제 유량 조절 및 연료 변경에 의한 O/F 비 변화는 연소 압력의 저주파수 증폭과 무관한 것으로 밝혀졌다. 후연소실로 연소가스가 팽창할 때 발생하는 와류 흘림 현상이 저주파수 불안정 현상과 직접적인 관련 있는 것으로 판단되며 이에 관한 연구가 더 필요하다.

평판 가까이에 놓인 타원형 실린더 주위 유동에 관한 연구 (Flow Around an Elliptic Cylinder Placed Near a Plane Boundary)

  • 김성민;이상준
    • 대한기계학회논문집B
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    • 제20권8호
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    • pp.2637-2649
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    • 1996
  • Flow characteristics and aerodynamic forces acting on an elliptic cylinder placed in a plane boundary layer were investigated experimentally. Four cylinder models with axis ratio(major axis to minor axis, AR=A/B) of 1, 2, 3, and 4 having the same equivalent diameter were used in this experiment. The Reynolds number based on the equivalent diameter $D_e$(=20mm) was 13,000. In the case of circular cylinder, regular vortex shedding occurs for the cylinder gaps larger than G/B=0.3 and is not almost related to the boundary layer thickness. But, for the elliptic cylinders, the vortex shedding frequency is increased with increasing the gap ratio (G/B) and the axis ratio (AR) of elliptic cylinders. The maximum drag coefficient acting on a circular cylinder is mainly affected by the boundary layer thickness. But, the elliptic cylinders(AR$\geq$2), except for the smaller gap G/B<0.2, show a nearly constant drag coefficient which is much smaller than that of a circular cylinder. The base pressure on the flat plate decreases with increasing the axis ratio(AR) of the elliptic cylinder. In the case of a circular cylinder, the base pressure has the minimum value at the gap ratio G/B=0.4, but it occurs at G/D=2 for elliptic cylinders. The mean velocity of the cylinder wake is quickly recovered at a small cylinder height ratio(H/$\delta$), but the turbulent intensity is rapidly recovered at a large cylinder height ratio(H/$\delta$). The effective wake region in the plane boundary layer is shrinkaged with increasing the axis ratio(AR) of elliptic cylinder. And the drag coefficient and streamwise turbulent intensity of the elliptic cylinder with AR=4 are less than half of those for the circular cylinder(AR=1).

The effect of Reynolds number on the elliptical cylinder wake

  • Shi, Xiaoyu;Alam, Md. Mahbub;Bai, Honglei;Wang, Hanfeng
    • Wind and Structures
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    • 제30권5호
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    • pp.525-532
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    • 2020
  • This work numerically investigates the effects of Reynolds number ReD (= 100 - 150), cross-sectional aspect ratio AR = ( 0.25 -1.0), and attack angle α (= 0° - 90°) on the forces, Strouhal number, and wake of an elliptical cylinder, where ReD is based on the freestream velocity and cylinder cross-section height normal to the freestream flow, AR is the ratio of the minor axis to the major axis of the elliptical cylinder, and α is the angle between the cylinder major axis and the incoming flow. At ReD = 100, two distinct wake structures are identified, namely 'Steady wake' (pattern I) and 'Karman wake followed by a steady wake (pattern II)' when AR and α are varied in the ranges specified. When ReD is increased to 150, an additional wake pattern, 'Karman wake followed by secondary wake (pattern III)' materializes. Pattern I is characterized by two steady bubbles forming behind the cylinder. Pattern II features Karman vortex street immediately behind the cylinder, with the vortex street transmuting to two steady shear layers downstream. Inflection angle αi = 32°, 37.5° and 45° are identified for AR = 0.25, 0.5 and 0.75, respectively, where the wake asymmetry is the greatest. The αi effectively distinguishes the dependence on α and AR of force and vortex shedding frequency at either ReD. In Pattern III, the Karman street forming behind the cylinder is modified to a secondary vortex street. At a given AR and α, ReD = 150 renders higher fluctuating lift and Strouhal number than ReD = 100.

The Experiment of Flow Induced Vibration in PWR RCCAs

  • Kim, Sang-Nyung;Cheol Shin
    • Journal of Mechanical Science and Technology
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    • 제15권3호
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    • pp.291-299
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    • 2001
  • Recently, severe wear on the shutdown rod cladding of Ulchin Nuclear Power Plant #1, #2 were observed by the Eddy Current Test(E.C.T.). In particular, the wear at the sixth card location was up to 75%. The test results indicated that the Flow Induced Vibration(F.I.V.) might be the cause of the fretting wear resulting from the contact between Rod Cluster Control Assemblies(RCCAs) and their spacing cards(guide plates) arranged in the guide tube. From reviewing RCCAs fretting wear repots and analyzing the general characteristics of F.I.V. mechanism in the reactor, geometric layout and flow conditions around the control rod, it is concluded that the turbulence excitation is the most probable vibration mechanism of RCCA. To identify the governing mechanism of RCCA vibration, an experiment was performed for a representative rod position in which the most serious fretting wear experienced among the six rod positions. The experimental rig was designed and set up to satisfy the governing nondimensional numbers which are Reynolds number and mass damping parameter. The vibration amplitude measurement by the non-contact laser displacement sensor showed good agreements in the frequency and the maximum wearing(vibration) location with Ulchin E.C.T. results and Framatome report, respectively. The sudden increase in the vibration amplitude was sensed around the 6th guide plate with mass flow rate variation. Comparing the similitude rod behaviour with the idealized response of a cylinder in flow induced vibration, it was found that he dominant mechanism of vibration was transferred from turbulence excitation to periodic shedding at the mass flow ate 90ι/min. Also the critical velocity of the vibration in RCCAs was determined and the vibration can be prevented by reducing the bypass flow rate below the critical velocity.

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대기경계층 내에 놓인 자유단 원주의 형상비가 후류유동에 미치는 영향에 관한 연구 (Effect of Cylinder Aspect Ratio on Wake Structure Behind a Finite Circular Cylinder Located in an Atmospheric Boundary Layer)

  • 박철우;이상준
    • 대한기계학회논문집B
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    • 제25권12호
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    • pp.1821-1830
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    • 2001
  • The flow around free end of a finite circular cylinder (FC) embedded in an atmospheric boundary layer has been investigated experimentally. The experiments were carried out in a closed-return type subsonic wind tunnel with varying aspect ratio of the finite cylinder mounted vertically on a flat plate. The wakes behind a 2-D cylinder and a finite cylinder located in a uniform flow were measured for comparison. Reynolds number based on the cylinder diameter was about Re=20,000. A hot-wire anemometer was employed to measure the wake velocity and the mean pressure distributions on the cylinder surface were also measured. The flow past the FC free end shows a complicated three-dimensional wake structure and flow phenomenon is quite different from that of 2-D cylinder. The three-dimensional flow structure was attributed to the downwashing counter rotating vortices separated from the FC free end. As the FC aspect ratio decreases, the vortex shedding frequency decreases and the vortex formation length increases compared to that of 2-D cylinder. Due to the descending counter-rotating twin-vortex, near the FC free end, regular vortex shedding from the cylinder is suppressed and the vortex formation region is hardly distinguished. Around the center of the wake, the mean velocity for the FC located in atmospheric boundary layer has large velocity deficit compared to that of uniform flow.

Prediction of Fluid-borne Noise Transmission Using AcuSolve and OptiStruct

  • Barton, Michael;Corson, David;Mandal, Dilip;Han, Kyeong-Hee
    • 한국소음진동공학회:학술대회논문집
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    • 한국소음진동공학회 2014년도 추계학술대회 논문집
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    • pp.557-561
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    • 2014
  • In this work, Altair Engineering's vibroacoustic modeling approach is used to simulate the acoustic signature of a simplified automobile in a wind tunnel. The modeling approach relies on a two step procedure involving simulation and extraction of acoustic sources using a high fidelity Computational Fluid Dynamics (CFD) simulation followed by propagation of the acoustic energy within the structure and passenger compartment using a structural dynamics solver. The tools necessary to complete this process are contained within Altair's HyperWorks CAE software suite. The CFD simulations are performed using AcuSolve and the structural simulations are performed using OptiStruct. This vibroacoustics simulation methodology relies on calculation of the acoustic sources from the flow solution computed by AcuSolve. The sources are based on Lighthill's analogy and are sampled directly on the acoustic mesh. Once the acoustic sources have been computed, they are transformed into the frequency domain using a Fast Fourier Transform (FFT) with advanced sampling and are subsequently used in the structural acoustics model. Although this approach does require the CFD solver to have knowledge of the acoustic simulation domain a priori, it avoids modeling errors introduced by evaluation of the acoustic source terms using dissimilar meshes and numerical methods. The aforementioned modeling approach is demonstrated on the Hyundai Simplified Model (HSM) geometry in this work. This geometry contains flow features that are representative of the dominant noise sources in a typical automobile design; namely vortex shedding from the passenger compartment A-pillar and bluff body shedding from the side view mirrors. The geometry also contains a thick poroelastic material on the interior that acts to reduce the acoustic noise. This material is modeled using a Biot material formulation during the structural acoustic simulation. Successful prediction of the acoustic noise within the HSM geometry serves to validate the vibroacoustic modeling approach for automotive applications.

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질량분사가 있는 덕트 난류유동의 LES 해석 (LES for Turbulent Duct Flow with Surface Mass Injection)

  • 김보훈;나양;이창진
    • 한국항공우주학회지
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    • 제39권3호
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    • pp.232-241
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    • 2011
  • 하이브리드 로켓은 난류 산화제 유동과 고체 추진제의 기화로 인한 분사 유동 사이의 상호 작용에 의해 복잡한 형태의 혼합 전단층이 존재한다는 특별한 성질을 가지고 있다. 본 논문에서는 유동 간섭에 의해 표면에서 발생하는 진동 유동의 물리적 특성을 연구하기 위하여 압축성 효과를 고려한 질량분사가 있는 덕트 유동의 LES(Large Eddy Simulation) 해석을 수행하였다. 계산 결과에 따르면, 기화 질량이 분출됨에 따라 주유동방향 와류의 특성이 강해지고 국부적으로 발생하는 역류 현상을 근거로 벽면 근방에서 원주방향 와류가 생성됨을 확인하였다. 그리고 시간 특성을 갖고 나타나는 와류 흘림 현상은 혼합 전단층에 기인한 유동 불안정성에 의해 촉진되었으며, 분출유동에 의해 발달한 고유 진동 유동을 의미하는 압력 섭동의 특정 진동수가 $\omega$=8.8에서 검출됨을 확인하였다.

Mechanism on suppression in vortex-induced vibration of bridge deck with long projecting slab with countermeasures

  • Zhou, Zhiyong;Yang, Ting;Ding, Quanshun;Ge, Yaojun
    • Wind and Structures
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    • 제20권5호
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    • pp.643-660
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    • 2015
  • The wind tunnel test of large-scale sectional model and computational fluid dynamics (CFD) are employed for the purpose of studying the aerodynamic appendices and mechanism on suppression for the vortex-induced vibration (VIV). This paper takes the HongKong-Zhuhai-Macao Bridge as an example to conduct the wind tunnel test of large-scale sectional model. The results of wind tunnel test show that it is the crash barrier that induces the vertical VIV. CFD numerical simulation results show that the distance between the curb and crash barrier is not long enough to accelerate the flow velocity between them, resulting in an approximate stagnation region forming behind those two, where the continuous vortex-shedding occurs, giving rise to the vertical VIV in the end. According to the above, 3 types of wind fairing (trapezoidal, airfoil and smaller airfoil) are proposed to accelerate the flow velocity between the crash barrier and curb in order to avoid the continuous vortex-shedding. Both of the CFD numerical simulation and the velocity field measurement show that the flow velocity of all the measuring points in case of the section with airfoil wind fairing, can be increased greatly compared to the results of original section, and the energy is reduced considerably at the natural frequency, indicating that the wind fairing do accelerate the flow velocity behind the crash barrier. Wind tunnel tests in case of the sections with three different countermeasures mentioned above are conducted and the results compared with the original section show that all the three different countermeasures can be used to control VIV to varying degrees.

Strouhal number of bridge cables with ice accretion at low flow turbulence

  • Gorski, Piotr;Pospisil, Stanislav;Kuznetsov, Sergej;Tatara, Marcin;Marusic, Ante
    • Wind and Structures
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    • 제22권2호
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    • pp.253-272
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    • 2016
  • The paper concerns with the method and results of wind tunnel investigations of the Strouhal number (St) of a stationary iced cable model of cable-supported bridges with respect to different angles of wind attack. The investigations were conducted in the Climatic Wind Tunnel Laboratory of the Czech Academy of Sciences in $Tel{\check{c}}$. The methodology leading to the experimental icing of the inclined cable model was prepared in a climatic section of the laboratory. The shape of the ice on the cable was registered by a photogrammetry method. A section of an iced cable model with a smaller scale was reproduced with a 3D printing procedure for subsequent aerodynamic investigations. The St values were determined within the range of the Reynolds number (Re) between $2.4{\cdot}10^4$ and $16.5{\cdot}10^4$, based on the dominant vortex shedding frequencies measured in the wake of the model. The model was oriented at three principal angles of wind attack for each of selected Re values. The flow regimes were distinguished for each model configuration. In order to recognize the tunnel blockage effect the St of a circular smooth cylinder was also tested. Good agreement with the reported values in the subcritical Re range of a circular cylinder was obtained. The knowledge of the flow regimes of the airflow around an iced cable and the associated St values could constitute a basis to formulate a mathematical description of the vortex-induced force acting on the iced cable of a cable-supported bridge and could allow predicting the cable response due to the vortex excitation phenomenon.