• Title/Summary/Keyword: Scheduled Speed

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Technical Study on Possibility of an Express Service Wide Area Railway (광역철도 노선의 급행화 가능성에 대한 기술적 검토)

  • Park, Jung Hyun
    • Journal of the Korean Society for Railway
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    • v.20 no.5
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    • pp.612-624
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    • 2017
  • As the existing metropolitan area metropolitan railway operates on a one-to-one basis, which leads to long travel times, its competitiveness with other means of transportation is deteriorating. Since there is a limit to attracting road traffic by rail, there is a continuing societal demand to expand express train service. Especially in the northern and the southwestern parts of the metropolitan area, a public transportation network system with express function, connecting to the city center of Seoul, is needed because of the social cost of the increase of traffic congestion and the increase of the travel time. The most efficient express service in Korea is Seoul Subway Line 9, which runs in 27 minutes from Gimpo Airport to the high speed terminal; this is a 40% shorter time compared to 44 minutes by car; the congestion in this area is up to 240%, so the preference for this train is quite high. The technical results of this study are expected to contribute to the implementation of an express service metropolitan railway.

Experimental investigation of dynamic trim control devices in fast speed vessel (고속선의 트림제어 장치가 항주 자세 및 저항 성능에 미치는 영향)

  • Seo, Kwang-Cheol;Gopakumar, Nithin;Atlar, Mehmet
    • Journal of Navigation and Port Research
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    • v.37 no.2
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    • pp.137-142
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    • 2013
  • The displacement Deep-V catamaran concept was developed in Newcastle University(UNEW) through development of the systematic Deep-V catamaran series. One of the most important Deep-V catamaran launched to date is Newcastle University's own multi-purpose research vessel, The Princess Royal. The vessel was launched in 2011 and enhanced the Deep-V catamaran concept further with the successful adoption of a novel anti-slamming bulbous bow and tunnel stern for improved efficiency. It was however identified that the vessel has substantial amount of dynamic trim that limited the visibility of the captain. The dynamic trim also increased the wave-making resistance thereby preventing the vessel from attaining its maximum speed in certain sea states. This paper therefore presents the application of devices such as Trim Tabs, Interceptors, Transom Wedges and Integrated Transom Wedges-Tabs to control the dynamic trim and improvement of fuel efficiency of the vessel. All of these energy saving devices were fitted into a model for tests in Newcastle University's Towing Tank. Model test verification confirmed that the optimum appendage was the interceptors, they produced a 5% power saving and 1.2 degree trim reduction at 15 knots, and investigations of full scale trials will be scheduled with and without application of device to compare the improvement of performance.

Delay and Doppler Profiler based Channel Transfer Function Estimation for 2×2 MIMO Receivers in 5G System Targeting a 500km/h Linear Motor Car

  • Suguru Kuniyoshi;Rie Saotome;Shiho Oshiro;Tomohisa Wada
    • International Journal of Computer Science & Network Security
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    • v.23 no.9
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    • pp.8-16
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    • 2023
  • In Japan, high-speed ground transportation service using linear motors at speeds of 500 km/h is scheduled to begin in 2027. To accommodate 5G services in trains, a subcarrier spacing frequency of 30 kHz will be used instead of the typical 15 kHz subcarrier spacing to mitigate Doppler effects in such high-speed transport. Furthermore, to increase the cell size of the 5G mobile system, multiple base station antennas will transmit identical downlink (DL) signals to form an expanded cell size along the train rails. In this situation, the forward and backward antenna signals are Doppler-shifted in opposite directions, respectively, so the receiver in the train may suffer from estimating the exact Channel Transfer Function (CTF) for demodulation. In a previously published paper, we proposed a channel estimator based on Delay and Doppler Profiler (DDP) in a 5G SISO (Single Input Single Output) environment and successfully implemented it in a signal processing simulation system. In this paper, we extend it to 2×2 MIMO (Multiple Input Multiple Output) with spatial multiplexing environment and confirm that the delay and DDP based channel estimator is also effective in 2×2 MIMO environment. Its simulation performance is compared with that of a conventional time-domain linear interpolation estimator. The simulation results show that in a 2×2 MIMO environment, the conventional channel estimator can barely achieve QPSK modulation at speeds below 100 km/h and has poor CNR performance versus SISO. The performance degradation of CNR against DDP SISO is only 6dB to 7dB. And even under severe channel conditions such as 500km/h and 8-path inverse Doppler shift environment, the error rate can be reduced by combining the error with LDPC to reduce the error rate and improve the performance in 2×2 MIMO. QPSK modulation scheme in 2×2 MIMO can be used under severe channel conditions such as 500 km/h and 8-path inverse Doppler shift environment.

Effects of The Home Physical Therapy on Recovery of Muscle Strength and Gait for Discharged Patients Who Underwent Total Knee Replacement

  • Jang, Yong Su;Kim, Moo Ki;Kim, Ji Sung;Koo, Ja Pung;Park, Si Eun;Choi, Wan Suk;Kim, Bo Kyoung;Kim, Yong Youn;Kim, Soon Hee
    • Journal of International Academy of Physical Therapy Research
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    • v.5 no.2
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    • pp.743-751
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    • 2014
  • This study aims to identify the effect of home physical therapy on patients who left the hospital after total knee arthroplasty, compared to the Daily living group, when it was applied to them, under the guidance of physical therapists. As research subjects, 20 patients that were scheduled to leave the hospital after unilateral total knee arthroplasty, were chosen, and they were randomly divided into a home physical therapy group(10 patients) and an Daily living group(10 patients) in order to conduct an experiment. During the 4-week research, home physical therapy was offered for 40 mins once for 5 days a week, and muscular strength, gait components were measured. For muscular strength, quadriceps muscle strength, hamstring muscle strength were measured, and as gait components, endurance, speed, step time, single-limb support were analysed. For this experiment, pre- and post-measurement were performed, and collected data were analyzed using SPSS ver. 18.0 statistical program. From the analysis of data, the following study results were obtained. Home physical therapy group and Daily living group both showed significant improvements in quadriceps muscle strength, hamstring muscle strength, and quadriceps muscle strength, hamstring muscle strength of home physical therapy group more significantly improved than Daily living group's. In relation to gait components, gait endurance, gait speed, step time significantly improved in both of home physical therapy group and Daily living group, whereas home physical therapy group only showed significant improvements in single-limp support. According to the comparison between two groups, gait speed, single-limp support and step time improved more significantly in the home physical therapy group than in the Daily living group. In conclusion, positive results were revealed in both home physical therapy group and Daily living group, with regard to muscular recovery of lower limbs of patients discharged from the hospital after total knee arthroplasty and walking, but considering the comparison results between two groups, it seems that applying home physical therapy is more effective than maintaining a daily life.

Statistical Qualitative Analysis on Chemical Mechanical Polishing Process and Equipment Characterization

  • Hong, Sang-Jeen;Hwang, Jong-Ha;Seo, Dong-Sun
    • Transactions on Electrical and Electronic Materials
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    • v.12 no.2
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    • pp.56-59
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    • 2011
  • The characterization of the chemical mechanical polishing (CMP) process for undensified phophosilicate glass (PSG) film is reported using design of experiments (DOE). DOE has been used by experimenters to understand the relationship between the input variables and responses of interest in a simple and efficient way, and it typically is beneficial for determining the appropriatesize of experiments with multiple process variables and making statistical inferences for the responses of interest. The equipment controllable parameters used to operate the machine consist of the down force of the wafer carrier, pressure on the back side wafer, table and spindle speeds (SS), slurry flow (SF) rate, pad condition, etc. None of these are independent ofeach other and, thus, the interaction between the parameters also needs to be understoodfor improved process characterization in CMP. In this study, we selected the five controllable equipment parameters the most recommendedby process engineers, viz. the down force (DF), back pressure (BP), table speed (TS), SS, and SF, for the characterization of the CMP process with respect to the material removal rate and film uniformity in percentage terms. The polished material is undensified PSG which is widely used for the plananization of multi-layered metal interconnects. By statistical modeling and the analysis of the metrology data acquired from a series of $2^{5-1}$ fractional factorial designs with two center points, we showed that the DF, BP and TS have the greatest effect on both the removal rate and film uniformity, as expected. It is revealed that the film uniformity of the polished PSG film contains two and three-way interactions. Therefore, one can easily infer that process control based on a better understanding of the process is the key to success in current semiconductor manufacturing, in which the size of the wafer is approaching 300 mm and is scheduled to continuously increase up to 450 mm in or slightly after 2012.

Tethered Hover Test for Small Scaled Tilt-rotor UAV (축소형 틸트로터 무인기의 안전줄 호버 시험)

  • Park, Bum-Jin;Yoo, Chang-Sun;Chang, Sung-Ho;Choi, Seong-Wook;Koo, Sam-Ok;Kang, Young-Shin
    • Journal of the Korean Society for Aviation and Aeronautics
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    • v.15 no.4
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    • pp.9-16
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    • 2007
  • Tilt rotor aircraft can take off and land vertically and cruise faster than any other helicopter. A scaled flight demonstration model of a tilt rotor aircraft has been developed by KARI. Because the flight characteristics of tilt rotor are not well known, the developed scaled model would be helpful to evaluate flight control algorithm of a full scale aircraft. The tethered hover test has been performed in order to improve hover flight characteristics of tilt rotor aircraft prior to flight test of the small scaled model. During the tethered hover test, the performance of rotor speed governor, rate SAS (Stability Augmentation System) and control surface mixers have been evaluated. We expect that the results of real flight hover test would be quite same as tethered hover test. Therefore the tethered hover test results will reduce the risk of flight test properly by fixing some of hidden problems which might occur during the flight test. This paper presents the results of tethered hover test in detail and shows how it could be final ground test before flight test. The control mixer gain and rate SAS feedback gains were modified in order to get higher controllability and stability during the tethered hover flight. The rotor governor showed that it could keep rotor RPM constant with very small deviation even during severe pilot collective input change. The tethered hover test results gave pilot and engineers confirmation and experience about the scheduled flight test.

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A Numerical Study on Transient Performance Behavior of a Turbofan Engine with Variable Inlet Guide Vane and Bleed Air Schedules (가변 입구 안내익과 블리드 공기 스케줄에 따른 터보팬 엔진에서의 천이 성능특성에 관한 수치연구)

  • Kim, Sangjo;Son, Changmin;Kim, Kuisoon;Kim, Myungho;Min, Seongki
    • Journal of the Korean Society of Propulsion Engineers
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    • v.19 no.5
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    • pp.52-61
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    • 2015
  • This paper performed a numerical study to analyse the transient performance behavior of a turbofan engine with variable inlet guide vane (IGV) and bleed air schedules. The low bypass ratio mixed flow turbofan engine was considered in this study. For modeling the compressor performance with IGV, the performance maps were generated by using a one-dimensional meanline analysis and feed to the engine simulation program. The IGV and bleed air according to the rotating speed were scheduled to satisfy 10% of surge margin at steady-state condition. The transient engine performance analysis was conducted with the schedules. The engine with IGV schedule showed a higher surge margin and lower turbine inlet temperature than the engine with bleed air schedule during the transient period.

On/Off-Design/Transient Analysis of a 50KW Turbogenerator Gas Turbine Engine (50KW 터보제너레이터용 가스터빈 엔진의 설계점/ 탈설계/과도성능해석)

  • Kim, Su-Yong;Park, Mu-Ryong;Jo, Su-Yong
    • 연구논문집
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    • s.27
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    • pp.87-99
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    • 1997
  • Present paper describes on/off design performance of a 50KW turbogenerator gas turbine engine for hybrid vehicle application. For optimum design point selection, relevant parameter study is carried out. The turbogenerator gas turbine engine for a hybrid vehicle is expected to be designed for maximum fuel economy, ultra low emissions, and very low cost. Compressor, combustor, turbine, and permanent-magnet generator will be mounted on a single high speed (82,000 rpm) shaft that will be supported on air bearings. As the generator is built into the shaft, gearbox and other moving parts become unnecessary and thus will increase the system's reliability and reduce the manufacturing cost. The engine has a radial compressor and turbine with design point pressure ratio of 4.0. This pressure ratio was set based on calculation of specific fuel consumption and specific power variation with pressure ratio. For the given turbine inlet temperature, a rather conservative value of $1100^\circK$ was selected. Designed mass flow rate was 0.5 kg/sec. Parametric study of the cycle indicates that specific work and efficiency increase at a given pressure ratio and turbine inlet temperature. Off design analysis shows that the gas turbine system reaches self operating condition at N/$N_{DP}$ = 0.53. Bleeding air for turbine stator cooling is omitted considering low TIT and for a simple geometric structure. Various engine performance simulations including, ambient temperature influence, surging at part load condition. Transient analysis were performed to secure the optimum engine operating characteristics. Surge margin throughout the performance analysis were maintained to be over 80% approximately. Validation of present results are yet to be seen as the performance tests are scheduled by the end of 1998 for comparison.

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The Study of the Robustness Analysis of the autopilot for the UAV (무인항공기 자동조종장치의 강건성 해석에 관한 연구)

  • Lim, Ho;Kim, Ki-Yeol;Kim, Ho
    • The Journal of Information Technology
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    • v.4 no.3
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    • pp.165-170
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    • 2001
  • In this paper, we proposed an autopilot of the unmanned piloted vehicle to guide to the specific position and analyzed robustness of the designed autopilot. We divide an aircraft velocity into the three case which are low, crusing and high speed, and designed autopilot gains are gain scheduled. We generated the turbulence for the operational altitudes and analyzed performance of the autopilot about it. We proved robustness of the designed autopilot for the turbulence and gust using simulation.

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A Study for the Express Railway of Seoul Metropolitan Area(Kangnam$\sim$Ilsan) (수도권(강남$\sim$일산) 급행철도 도입에 관한 연구)

  • Park, Kwang-Bok
    • Proceedings of the KSR Conference
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    • 2009.05a
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    • pp.1269-1278
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    • 2009
  • The Seoul metropolitan area is generated the transportation problems of traffic congestion, delay of travel time, etc due to the increase of traffic demand at Seongnam area, Koyang/Paju area, Incheon/Bucheon area, etc, because that have not provided the urban surrounding railway network and live to be concentrated about 49% of the population of Korea. The Koyang/Paju route axis is required the urban surrounding railway network because the share percentage of public transportation is 51%, the automobiles is 48.8% and the subway is 27.3% and the housing development plan for 530,000 persons have provided. According to the result of the study for the introduction of the express railway between Kangnam to Ilsan of 37.8Km, in case of operation of 150Kmm at express railway, the scheduled speed between Kangnam to Ilsan is 103Km/h, the running time is about 23 minutes. The demand of traffic of this project was forecasted about 237,000persons by traffic analysis. This project which was analysed B/C of 1.08 by the result of the feasibility study have a economic feasibility.

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