• Title/Summary/Keyword: Propulsion motor

Search Result 678, Processing Time 0.026 seconds

Development of Somaloy Components for a BLDC Motor in a Scroll Compressor Application

  • Persson, Mats;Nord, Goran;Pennander, Lars-Olov;Atkinson, Glynn;Jack, Alan
    • Proceedings of the Korean Powder Metallurgy Institute Conference
    • /
    • 2006.09b
    • /
    • pp.804-805
    • /
    • 2006
  • Electric scroll-compressor drives are commonly used for e.g. home appliance cooling units. The recent development of hybrid cars with internal combustion engine in combination with electrical propulsion requires new solutions to be able to cool the passenger compartment of cars at stand-still. Both application areas demand efficient motor drives to reach good economy and efficient use of limited battery power as well as competitive volume/weight for a given output. The BLDC motor is a controllable and efficient solution. A major part of the motor is the soft-magnetic core. The powder based $Somaloy^{(R)}$ material shows high resistivity and induction as the result of engineered iron particles with in-organic coating. The unique features of compacted $Somaloy^{(R)}$ components can be utilized to enhance the shape and total volume of the BLDC motor with at least maintained efficiency compared to the use of traditional laminated steel sheet cores. A careful design of the $Somaloy^{(R)}$ components can also simplify assembly and positively influence the coil configuration. This study shows a comparison between a typical laminated BLDC motor and a redesigned, $Somaloy^{(R)}$ based version adapted for a scroll-compressor application.

  • PDF

Spatial and Temporal Features of Motor Modules in an individual with Hemiparesis During the Curvilinear Gait: A Pilot Single-Case Study

  • LEE, Jae-Hyuk
    • Journal of Wellbeing Management and Applied Psychology
    • /
    • v.5 no.1
    • /
    • pp.1-7
    • /
    • 2022
  • Purpose: This study aimed to investigate spatial and temporal features of motor control in an individual with hemiparesis during the curvilinear gait (CG) and proposed an exercise guideline. Research design, data and methodology: An individual aged 63 with hemiparesis by stroke disease was participated in the study. Autoencoder (AE) was used to extract four motor modules from eight muscle activities of the paretic leg during CG. After extraction, each module of four modules was operationally defined by numbering from M1 to M4 according to spatial and temporal features and compared with results reported in a previous study. Results: As a result, an individual with hemiparesis had motor module problems related to difficulty of weight acceptance (module 1), compensation for the weakness of ankle plantar flexor (module 2), a spastic synergistic pattern (module 3) and difficulty with transition from the swing to stance phase (module 4) in terms of spatial features. Also, a delayed activation timing of temporal motor module (module 2) related to the forward propulsion during CG was observed. Conclusions: Gait rehabilitation for the stroke will need to consider clinical significances in respect of the deterioration of motor module and provide the tailored approaches for each gait phase.

Analysis on the Internal Flow of the Hydraulic Dual Chambers Applying Various Orifice (다양한 오리피스를 이용한 연결형 공압 챔버 내부 유동 해석)

  • Cho, Kihong;Park, Jungho;Kim, Euiyong
    • Journal of the Korean Society of Propulsion Engineers
    • /
    • v.18 no.1
    • /
    • pp.58-64
    • /
    • 2014
  • Hydraulic dual chamber, as the simulator for a dual pulse rocket motor, was tested by a high pressure device with various orifice-hole size being applied. Pressure difference occurs between 1st chamber and 2nd chamber depending on area ratio of the orifice to nozzle throat. Studying a design configuration of the orifice is essential to the motor development because pressure difference severely affects the rocket motor performance. It is noticed in this study that energy dissipation is caused by the vortex flow originating from the orifice as the 2nd chamber is operated. The flow field is simulated by a commercial computational fluid dynamics program, ANSYS FLUENT V14.5.

Analysis of Unsteady Combustion Performance in Solid Rocket Motor with Pintle (핀틀을 장착한 고체추진기관의 비정상 연소 성능 분석)

  • Ki, Taeseok;Ha, Dongsung;Jin, Jungkun;Lee, Hosung;Yoon, Hyungull
    • Journal of the Korean Society of Propulsion Engineers
    • /
    • v.19 no.1
    • /
    • pp.68-75
    • /
    • 2015
  • In this paper, unsteady characteristics of pressure in solid rocket motor were analyzed by using response of pintle actuation, pressure and thrust data from ground test. Pressure and thrust in solid rocket motor can be controlled in real time by varying nozzle throat area with pintle, installed in the valve. Unsteady characteristics of pressure can be observed in this system occurred by various reasons. Two critical reasons, error of pintle actuation and ablation of center tube, are found and effects of each reason can be analyzed individually by re-prediction of pressure with response of pintle actuation and analyzing thrust to pressure ratio.

Firing Test for Hybrid Rocket Motor with 650 kgf Thrust Level (추력 650 kgf 급 하이브리드 로켓 모터의 연소시험)

  • Lee, Jung-Pyo;Kim, Soo-Jong;Kim, Gi-Hun;Cho, Jung-Tae;Kim, Hak-Chul;Woo, Kyong-Jin;Do, Gyu-Sung;So, Jung-Soo;Oh, Jung-Soo;Cho, Min-Gyung;Moon, Hee-Jang;Sung, Hong-Gye;Kim, Jin-Kon
    • Proceedings of the Korean Society of Propulsion Engineers Conference
    • /
    • 2009.11a
    • /
    • pp.503-506
    • /
    • 2009
  • In this study, we presented the results of static firing tests on the PE/LN2O hybrid rocket motor, which has a thrust of 650 kgf level. Through the early tests, we found that the combustion chamber pressure and the thrust were lower than design values because an actual oxidizer flow rate was less than that expected. In order to complement this result, the methods of decrease of nozzle throat and the increase of oxidizer mass flow rate were conducted in the next experiment, and we studied the combustion phenomena with the experimental results. Also we compared and analyzed a difference of combustion characteristics on scale effect. It show that a sub-scale motor regression rate was a little less than that of a lab-scale motor with the same oxidizer mass flux. Results of this study might be used as a basic data for development of hybrid sounding rocket.

  • PDF

Combustion Characteristics and Performance Prediction of PE-GOX Hybrid Rocket Motor Part II : Internal Ballistic Performance (PE-GOX 하이브리드 모터의 연소특성 및 성능 예측 기법 Part II : 내탄도 성능)

  • Yoon, Chang-Jin;Song, Na-Young;Yoo, Woo-Jun;Jeon, Chang-Soo;Kim, Jin-Kon;Moon, Hee-Jang;Sung, Hong-Gye
    • Journal of the Korean Society of Propulsion Engineers
    • /
    • v.11 no.2
    • /
    • pp.79-85
    • /
    • 2007
  • An internal ballistic model to predict the performance of a Polyethylene-GOX (PE-GOX) hybrid motor was proposed and evaluated. A theoretical treatment of the model was followed by detail discussion of each of the factors affecting the overall performance. The present model consists of the governing equations by considering the unsteady burn-back rate of the fuel grain and on-off response characteristics of a oxygen-supply valve. The numerical results using the 4th order Runge-Kutta scheme with temporal physicochemical properties showed good agreements with test results and the global effects of the performance parameters, such as the burning area of the fuel grain, O/F ratio, and etc., on the performance of the motor were analyzed.

Development of Nozzleless Booster casted to Solid Propellant with Al as a Metal Fuel (알루미늄(Al) 금속연료 조성의 추진제를 이용한 무노즐 부스터 개발)

  • Khil, Taeock;Jung, Eunhee;Lee, Kiyeon;Ryu, Taeha;Lee, Hyoungjin
    • Journal of the Korean Society of Propulsion Engineers
    • /
    • v.21 no.4
    • /
    • pp.52-62
    • /
    • 2017
  • The study for the performance characteristics of the nozzleless booster used in ramjet booster was carried out. Performances related to pressure and thrust for nozzleless booster are lower than classical motor those because of absence of convergent and divergent sections of nozzle. To solve this problem, it developed a high-performance propellant with maximum impulse density included Al as metal fuel. Using the nozzleless booster casted the propellant, ground test of it was carried out by varying the length-to-diameter ratio (L/D ratio) of the propellant. Specific impulse of nozzleless booster was limited to about 75 percents of its value compared with that of classical motor adapted nozzle in the same propellant and propellant length and will be estimated approximately 85 percents of its value compared with that of classical motor at same average pressure in terms of the curve fitting by our test results.

Shape Optimization of the Metal Boss for a Composite Motor Case (복합재 연소관의 금속 보스 형상 최적설계)

  • Jeong, Seungmin;Kim, Hyounggeun;Hwang, Taekyung
    • Journal of the Korean Society of Propulsion Engineers
    • /
    • v.20 no.6
    • /
    • pp.29-37
    • /
    • 2016
  • This paper proposes a shape optimization of the metal boss for a composite motor case using finite element analysis. For the structural safety and the weight reduction of the composite motor case, under the internal pressure, the fiber stress in the dome area and the tightening bolt stress are constrained and the boss weight is set to objective function, respectively. The response surface models are constructed for the performance characteristics by using response surface method. The significance of the design variables about the performance characteristics is evaluated through the ANOVA(analysis of variance) and the goodness of fit test for the constructed model is performed through the regression analysis. The SQP(sequential quadratic programming) algorithm is used for the optimization and the proposed method is verified by performing structural analysis for the optimum shape.

Scale Effect on Combustion Characteristics of N2O/PE Hybrid Rocket (N2O/PE 하이브리드 로켓의 스케일 변화에 따른 연소특성 연구)

  • Han, Seongjoo;Moon, Keunhwan;Kim, Jinkon;Moon, Heejang
    • Proceedings of the Korean Society of Propulsion Engineers Conference
    • /
    • 2017.05a
    • /
    • pp.797-802
    • /
    • 2017
  • This paper describes the scale effect of hybrid rocket motor which has blow-down oxidizer supply system. ResuIts show that the scale effect on regression rate is negligible using presently accessible scaling relation for $LN_2O$/PE propellant combination amid the absence of exactly proven scaling relation. It was also found that the characteristic velocity efficiency increases as motor scale increases. However, the characteristic velocity efficiency includes complicated parameters such as post-chamber configuration or geometry which can affect the entire flow field. It is therefore hard to conclude that the increase of efficiency is solely due to the enlargement of motor scale nor draw any conclusion on the scale effect which require a profound understanding of hybrid rocket scaling rules.

  • PDF

Development of an Integrated Design System for Solid Rocket Motors (고체 추진기관 통합 설계 시스템 개발)

  • Lee, Kang-Soo;Kim, Won-Hoon;Hwang, Tae-Kyung;Bae, Joo-Chan;Yang, June-Seo;Lee, Do-Hyeong;Seok, Jung-Ho;Choi, Byeong-Wook;Kwon, Hyuk-Sun
    • Proceedings of the Korean Society of Propulsion Engineers Conference
    • /
    • 2008.11a
    • /
    • pp.207-210
    • /
    • 2008
  • We developed an integrated design system for a solid rocket motors. We can do a conceptual design of a solid rocket motor easily and quickly with this system. It consists of four modules, or, size design, structure design, grain design and performance analysis module. Size design module determines the lengths and diameters of some major parts, which results in fixing the whole size of a motor. Structure design module has many master models, which enables a designer can do a conceptual design of almost parts of motor structures. Grain design module can design a solid fuel according to the result of structure design. Finally performance analysis module verifies the proposed design with the output from grain design module.

  • PDF