• Title/Summary/Keyword: Plant Engineering Program

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Implementation Status of Performance Demonstration Program for Steam Generator Tubing Analysts in Korea

  • Cho, Chan-Hee;Lee, Hee-Jong;Yoo, Hyun-Ju;Nam, Min-Woo;Hong, Sung-Yull
    • Journal of the Korean Society for Nondestructive Testing
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    • v.33 no.1
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    • pp.63-68
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    • 2013
  • Some essential components in nuclear power plants are periodically inspected using non-destructive examinations, for example ultrasonic, eddy current and radiographic examinations, in order to determine their integrity. These components include nuclear power plant items such as vessels, containments, piping systems, pumps, valves, tubes and core support structure. Steam generator tubes have an important safety role because they constitute one of the primary barriers between the radioactive and non-radioactive sides of the nuclear power plant. There is potential that if a tube bursts while a plant is operating, radioactivity from the primary coolant system could escape directly to the atmosphere. Therefore, in-service inspections are critical in maintaining steam generator tube integrity. In general, the eddy current testing is widely used for the inspection of steam generator tubes due to its high inspection speed and flaw detectability on non-magnetic tubes. However, it is not easy to analyze correctly eddy current signals because they are influenced by many factors. Therefore, the performance of eddy current data analysts for steam generator tubing should be demonstrated comprehensively. In Korea, the performance of steam generator tubing analysts has been demonstrated using the Qualified Data Analyst program. This paper describes the performance demonstration program for steam generator tubing analysts and its implementation results in Korea. The pass rate of domestic analysts for this program was 71.4%.

Process Simulation of the BOG Re-Liquefaction system for a Floating LNG Power Plant using Commercial Process Simulation Program (상용 공정시뮬레이션 프로그램을 이용한 부유식 LNG 발전설비의 BOG 회수시스템 공정모사)

  • Seo, Ju-Wan;Yoo, Seung-Yeol;Lee, Jae-Chul;Kim, Young-Hun;Lee, Soon-Sup
    • Journal of the Korean Society of Marine Environment & Safety
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    • v.26 no.6
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    • pp.732-741
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    • 2020
  • Environmental regulations have recently been strengthened. Consequently, floating LNG(Liquefied Natural Gas) power plants are being developed, which are new power generation plants that generate electricity by utilizing LNG. A floating LNG power plant generates BOG(Boil-Off Gas) during its operation, and the system design of such a plant should be capable of removing or re-liquefying BOG. However, the design of an offshore plant differs according to the marine requirements. Hence, a process simulation model of the BOG re-liquefaction system is needed, which can be continuously modified to avoid designing the floating LNG power plant through trial and error. In this paper, to develop a model appropriate for the floating LNG power plant, a commercial process simulation program was employed. Depending on the presence of refrigerants, various BOG re-liquefaction systems were modeled for comparing and analyzing the re-liquefaction rates and liquid points of BOG. Consequently, the BOG re-liquefaction system model incorporating nitrogen refrigerants is proposed as the re-liquefaction system model for the floating LNG power plant.

A Development of the Performance Analysis Program Package of the Automatic Temperature Control System for Heating (난방용 자동온도조절기 성능분석용 프로그램 및 패키지 개발)

  • Kim, Yong-Ki;Woo, Nam-Sub;Lee, Tae-Won;Ahn, Byung-Cheon
    • Proceedings of the SAREK Conference
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    • 2009.06a
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    • pp.1209-1214
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    • 2009
  • Various automatic temperature control systems have been used widely in Korea for the conservation of heating energy and the enhancement of thermal comfort in residential buildings. But the heating control performance for automatic temperature control systems extensively vary with the design and operational conditions of the heating system, the climate condition and others. It was introduced in this study a numerical calculation program package to analyze heating control characteristics of the automatic temperature control system. This package is able to analyze the room air temperature, return water temperature, supplied heating flux and flow rate, and so on. One the other hand, the simulation results were verified by comparing with the field test results.

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Development of a Leading Performance Indicator from Operational Experience and Resilience in a Nuclear Power Plant

  • Nelson, Pamela F.;Martin-Del-Campo, Cecilia;Hallbert, Bruce;Mosleh, Ali
    • Nuclear Engineering and Technology
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    • v.48 no.1
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    • pp.114-128
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    • 2016
  • The development of operational performance indicators is of utmost importance for nuclear power plants, since they measure, track, and trend plant operation. Leading indicators are ideal for reducing the likelihood of consequential events. This paper describes the operational data analysis of the information contained in the Corrective Action Program. The methodology considers human error and organizational factors because of their large contribution to consequential events. The results include a tool developed from the data to be used for the identification, prediction, and reduction of the likelihood of significant consequential events. This tool is based on the resilience curve that was built from the plant's operational data. The stress is described by the number of unresolved condition reports. The strain is represented by the number of preventive maintenance tasks and other periodic work activities (i.e., baseline activities), as well as, closing open corrective actions assigned to different departments to resolve the condition reports (i.e., corrective action workload). Beyond the identified resilience threshold, the stress exceeds the station's ability to operate successfully and there is an increased likelihood that a consequential event will occur. A performance indicator is proposed to reduce the likelihood of consequential events at nuclear power plants.

CRISPR base editor-based targeted random mutagenesis (BE-TRM) toolbox for directed evolution

  • Rahul Mahadev Shelake;Dibyajyoti Pramanik;Jae-Yean Kim
    • BMB Reports
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    • v.57 no.1
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    • pp.30-39
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    • 2024
  • Directed evolution (DE) of desired locus by targeted random mutagenesis (TRM) tools is a powerful approach for generating genetic variations with novel or improved functions, particularly in complex genomes. TRM-based DE involves developing a mutant library of targeted DNA sequences and screening the variants for the desired properties. However, DE methods have for a long time been confined to bacteria and yeasts. Lately, CRISPR/Cas and DNA deaminase-based tools that circumvent enduring barriers such as longer life cycle, small library sizes, and low mutation rates have been developed to facilitate DE in native genetic environments of multicellular organisms. Notably, deaminase-based base editing-TRM (BE-TRM) tools have greatly expanded the scope and efficiency of DE schemes by enabling base substitutions and randomization of targeted DNA sequences. BE-TRM tools provide a robust platform for the continuous molecular evolution of desired proteins, metabolic pathway engineering, creation of a mutant library of desired locus to evolve novel functions, and other applications, such as predicting mutants conferring antibiotic resistance. This review provides timely updates on the recent advances in BE-TRM tools for DE, their applications in biology, and future directions for further improvements.

A Study on the Optimum Capacity of Combind Heat & Power Plant Related to Size of District Heating System (지역난방 규모에 따른 열병합발전플랜트의 경제적 최적용량 선정에 관한 연구)

  • Chung, Cahn-Kyo;Kim, Hoon
    • Journal of Energy Engineering
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    • v.9 no.2
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    • pp.95-101
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    • 2000
  • The purpose of this study is to find plant utilities capacity for economical operation of combined heat & power by reducing energy expenditure. Using a numerical simulation program CHPSIM, a comparative analysis of additional heat expenditure (AHE) of combined heat & power plant in relation to size of district heating has been performed within the comparison of the difference capacity of gas turbine and steam turbine . As a results, if a 105.2MW gas turbine (exhaust gas temp ; 540$^{\circ}C$) installed in CHP plant can reduced 17-18% yearly the AHE than 75MW gas turbine (520$^{\circ}C$) installed. If a 130-150MW gas turbine (560-580$^{\circ}C$) installed, can reduced 34.7-35.8% of the yearly AHE.

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Noise Map Modeling and Analysis of Thermal Power Plant (화력발전소의 소음지도 모델링 및 해석)

  • Kim, Won-Jin;Yun, Jun-Ho
    • Proceedings of the Korean Society for Noise and Vibration Engineering Conference
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    • 2013.10a
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    • pp.605-610
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    • 2013
  • This study proposes an analysis model to simulate a noise map and estimate noise distribution for a location and its surroundings of a power plant. The noise map analysis was executed by using ENPro that is a commercial program for environmental noise prediction. Experimental evaluation for the proposed analysis model was carried out by comparing the results from noise analysis and measurement at several major points of the power plant and residential areas.

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TECHNICAL EVALUATION OF THE CONTINUED OPERATION OF NPP

  • Kim, Tae-Ryong;Jin, Tae-Eun
    • Nuclear Engineering and Technology
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    • v.40 no.4
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    • pp.277-284
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    • 2008
  • Recently, the long-term operation of a nuclear power plant beyond its licensed term has become a worldwide trend as long as the safety of the plant is maintained in the extended period. Kori Unit 1, the oldest PWR in Korea, is the foremost example of this type of long-term operation in Korea. Comprehensive technical evaluation of the long-term operation of this plant was completed to confirm the overall safety of the plant. The technical evaluation included a review of PSR results, an assessment on aging management programs and time limited aging analyses, and a statement of radiological impact on the environment. Based on all of the results of the technical evaluation activities, Kori Unit 1 was approved to operate for an additional 10 years beyond its original design life of 30 years.

Computer Based Core Monitoring System for an Operating CANDU Reactor

  • Yoon Moon Young;Kwon Hwan O.;Kim Kyung Hwa;Yeom Choong Sub
    • Nuclear Engineering and Technology
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    • v.36 no.1
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    • pp.53-63
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    • 2004
  • The research was performed to develop a CANDU-6 Core Monitoring System(CCMS) that enables operators to have efficient core management by monitoring core power distribution, burnup distribution, and the other important core variables and managing the past core history for Wolsong nuclear power plant unit 1. The CCMS uses Reactor Fueling Simulation Program(RFSP, developed by AECL) for continuous core calculation by integrating the algorithm and assumptions validated and uses the information taken from Digital Control Computer(DCC) for the purpose of producing basic input data. The CCMS has two modules; CCMS server program and CCMS client program. The CCMS server program performs automatic and continuous core calculation and manages overall output controlled by DataBase Management System. The CCMS client program enables users to monitor current and past core status in the predefined GUI(Graphic-User Interface) environment. For the purpose of verifying the effectiveness of CCMS, we compared field-test data with the data used for Wolsong unit 1 operation. In the verification the mean percent differences of both cases were the same($0.008\%$), which showed that the CCMS could monitor core behaviors well.

Program Development for the Prediction of Cooling Tower Performance (냉각탑 성능 예측을 위한 프로그램 개발)

  • Jung, Jaehyung;Jung, Jaihyun;Choi, Young Ki
    • Korean Journal of Air-Conditioning and Refrigeration Engineering
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    • v.26 no.3
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    • pp.130-136
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    • 2014
  • The present study is performed to set up the framework of cooling tower performance predictions. The performance of mechanical forced draft cooling tower is directly related to the state of a nuclear power plant system, such as the condenser and evaporator. The main parameters related to the state of systems are as follows : wet bulb temperature, dry bulb temperature and absolute humidity. The performance evaluation of cooling tower must be considered at the power plant design. In this study, the toolkit developed by the American Cooling Tower Industry association (CTI) has been used for the framework construction. In order to validate the framework, it is being applied to the cooling tower constructed for the U.S. Nuclear Power Plant. The test results have shown good agreements with the cold water temperature on the cooling tower performance curves provided by manufacturers.