• 제목/요약/키워드: Motor Bearing

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Vibration Analysis of Rotor System for Rotary Compressor Considering Hydrodynamic Force between Motor Rotor and Stator (전동기 공극부 냉매의 유막력을 고려한 로터리 압축기용 회전축계의 진동해석)

  • Kim, Yong-Han;Yang, Bo-Suk;Ahn, Byoung-Ha;Lee, Jang-Woo
    • Proceedings of the Korean Society for Noise and Vibration Engineering Conference
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    • 2000.06a
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    • pp.1058-1064
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    • 2000
  • The analysis of dynamic behaviour of rotor system for the rolling piston type rotary compressor considering hydrodynamic force between motor rotor and stator is presented. In addition to considering other dynamic, loads such as large unbalance forces, gas force and bearing force, we consider the hydrodynamic force induced by the compressed fluid flow through the air gap between motor rotor and stator, and improve the analysis of vibration in rotary compressor. The Childs' method which based on Bulk-now and Hirs' turbulent lubrication model is used to calculate the rotordynamic coefficients due to hydrodynamic force of annular clearance in motor air gap.

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DEVELOPMENT OF AN ACCELERATED LIFE TEST PROCEDURE FOR COOLING FAN MOTORS

  • Shin, W.G.;Lee, S.H.;Song, Y.S.
    • International Journal of Automotive Technology
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    • v.7 no.6
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    • pp.757-762
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    • 2006
  • Reliability of automotive parts has been one of the most interesting fields in the automotive industry. Especially, a small DC motor was issued because of the increasing adoption for passengers' safety and convenience. For several years, small DC motors have been studied and some problems of a life test method were found out. The field condition was not considered enough in the old life test method. It also needed a lot of test time. For precise life estimation and accelerated life test, new life test procedure was developed based on measured field condition. The vibration condition on vehicle and latent force on fan motor shaft were measured and correlated with each other. We converted the acceleration data into the load data and calculated the equivalent load from integrated value. We found the relationship which can be used for accelerated life test without changing the severity by using different loading factors.

Development of Air Blower for Air Management Module of PEMFC System (고분자전해질 연료전지 연료공급모듈용 Air Blower 개발)

  • Hur, Jin;Jung, In-Soung
    • The Transactions of The Korean Institute of Electrical Engineers
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    • v.58 no.9
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    • pp.1735-1740
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    • 2009
  • This study presents a brushless DC (BLDC) motor for air management system of fuel cell modules. Magnetic equivalent circuit model and finite element analysis are used to design the motor, and an improved structure is considered to reduce a mechanical loss induced from bearing units. Finally, air blower system combined with the motor and an impeller is manufactured and output properties, such as an air pressure and an amount of flowing air, are measured. Through the experimental results, a validity of the simulated one is confirmed.

The Effect of Stator`s Slot on the Torque in the Windmill Type Ultrasonic Motor (풍차형 초음파 전동기의 고정자 슬롯이 토크에 미치는 영향)

  • 김영균;김진수
    • Proceedings of the Korean Institute of Electrical and Electronic Material Engineers Conference
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    • 1999.11a
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    • pp.323-326
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    • 1999
  • In this paper, a windmill type ultrasonic motor operated by single-Phase AC electric field was fabricated, and then torque characteristics were investigated. A metal-ceramic composite component was used as the stator\`s vibrator to generate ultrasonic vibrations. The windmill type ultrasonic motors has only three components; a stator element with two wind-mill shape slotted metal endcaps, a rotor and a bearing. In this parer we measured torque, when stator\`s slot was changed Iron 4, 6, 8. Brass metal was pressed with umbrella-type using metal molt then slot of 3 kind was manufactured. The maximum revolution speed was 388(rpm) in the case of a small ultrasonic motor of 11.35 mm diameter, 8 slot and 1.01 mm thickness. The maximum torque of 0.17 mNm was obtained at a speed of 131 rpm.

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A Study on the Characteristic of Noise and Vibration in 3-Phase Induction Motor for the Forklift (전동 지게차용 3 상 유도 모터의 소음 진동 특성에 대한 연구)

  • Kim, Woo-Hyung;Chung, Jin-Tai
    • Proceedings of the Korean Society for Noise and Vibration Engineering Conference
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    • 2007.11a
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    • pp.764-769
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    • 2007
  • This paper is studied the noise and vibration characteristics analysis of the three-phase induction AC motor of the electrical forklift. And we suggest the method which the reduction orders the noise and vibration to be the mechanical. In other to investigate these characteristics, we considered the mechanical characteristics, the electromagnetic effects, and these interactions. In mechanical, we studied the characteristic of the stator, the bearing supported condition of the rotor, and the sound radiation. In electronically, this paper is considered the harmonic effect which is related the magnetic motive force (mmf) with respect to the characteristic of the slot number of the rotor and the stator and the pole number of the motor. Finally we investigated the overall noise and vibration of the induction motor by relations between the electronically harmonic and the mechanical resonance of the stator. By the analysis of the generally three-phase induction motor, we suggest the design methodology to low noise and vibration.

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Multivariable Control System Design for Magnetic Bearing (자기베어링에 대한 다변수 제어계 설계)

  • Choung, K.G.;Yang, J.H.;Kim, C.H.
    • Journal of Power System Engineering
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    • v.15 no.1
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    • pp.78-85
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    • 2011
  • In order to design the control system of the magnetic bearing for the high speed 3 phase induction motor, the mathematical modeling was conducted and LQ regulator system was designed. When the plant is controllable and detectable, the nominal stability of LQ regulator could be guaranteed. However, LQ regulator doesn't ensure the robustness of stability and performance for the real system because LQ control is the mathematical optimal theory. In this paper to ensure the robustness of stability and performance for the real system, the control systems are designed by the simulation to the variation system parameters and this method was confirmed as an effective means.

Vibration Reduction of Electric-powered Hand Grinder (전동 핸드그라인더의 진동 저감)

  • 조성진
    • Proceedings of the Korean Society for Noise and Vibration Engineering Conference
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    • 2004.05a
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    • pp.831-836
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    • 2004
  • Vibration of electric-powered hand grinder comes from the parts of motor, gear, bearing, and fan. Excessive vibration can be harmful to workers. To reduce vibration of a hand grinder we analyzed the frequency components from the routing electric-powered grinder and did modal test to find the natural frequencies of the each part. It shows that the vibration is due to the resonance of the case. To remove the resonance, the case structure is modified and the bearing cap is replaced on a basis of the results from the rotor dynamic analysis using SAMCEF. As a result the vibration of the hand grinder is reduced greatly.

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A Comparison of Separated and Combined Winding Concepts for Bearingless Centrifugal Pumps

  • Raggl, Klaus;Nussbaumer, Thomas;Kolar, Johann W.
    • Journal of Power Electronics
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    • v.9 no.2
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    • pp.243-258
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    • 2009
  • Bearingless centrifugal pump systems are employed in the semiconductor, pharmaceutical and medical industries due to their facility for pumping high purity fluids without particle contamination. Two types of forces have to be generated by the stator units, namely bearing forces for achieving magnetic levitation, and drive forces for producing the needed pump torque. The generation of these forces requires bearing and drive windings, which can be realized as separate bearing and drive coils or as identical, combined coils on the stator claws. In this paper, a detailed comparison between these two winding concepts is undertaken, whereby the copper losses, the power electronics losses, and the achievable pump output pressure are evaluated for both concepts. For each criterion a ratio of improvement is calculated analytically which allows evaluation of the performance of the two winding concepts for any given pump operating point and design. Finally, also practical features such as control complexity, cabling effort and manufacturability are discussed and measurements on prototype systems are carried out to validate the considerations.

Development of a hard bearing type balancing machine (강성 베어링형 밸런실 장치의 개발)

  • 권이석;이동환;박중윤;홍성욱
    • Proceedings of the Korean Society of Precision Engineering Conference
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    • 1994.10a
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    • pp.773-777
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    • 1994
  • This paper is devoted to the development and performance evaluation of a hard bearing type balancing machine for rigid rotors. The pedestals of the balancing machine are designed to be rigid to be rigid enough to enable the balancing to operate far below the fundamental critical speed. The force measuring method is implemented to the balancing machine. The forces due to unbalance are measured through load cell that are attached to the pedestals. A helical coupling is used for transmitting the driving force from an AC servo motor to the rotor to be balanced. The experimental results show that the current hard bearing type balancing machine can indicate the presence of unbalance beyond 1 .mu. m in specific unbalance unit. The limitation of the current balancing machine is due to the coupling that is likely to make inconsistent offset errors everytime the rotor is connected to the machine.

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Vibration Reduction of Electric Hand Grinder (전동 핸드그라인더의 진동 저감#)

  • 조성진;최연선
    • Transactions of the Korean Society for Noise and Vibration Engineering
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    • v.14 no.10
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    • pp.1035-1040
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    • 2004
  • The vibration of an electric hand grinder originates from the motor, gear, bearing, and fan. Its excessive vibration can be harmful to workers. To reduce the vibration of an electric hand grinder. frequency analysis for the vibration signals of a running electric hand grinder and modal test for the each part were done. The results show that the vibration is due to the resonance of the case. To remove the resonance, the case structure was modified and the bearing cap was replaced on a basis of the results of the rotor dynamic analysis using SAMCEF. As a result, the vibration of the electric hand grinder was reduced greatly.