• Title/Summary/Keyword: Mist Blower

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Atomizing Mechanism for a Mist Blower (동력살분무기의 무화기구에 관한 연구)

  • 이상우
    • Journal of Biosystems Engineering
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    • v.21 no.2
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    • pp.117-122
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    • 1996
  • Droplet sizes produced from a mist blower should be adequate to get highly biological effects with a reasonable level of work performance. However the droplet sizes from the conventional nozzles of the mist blower were around VMD 95 to 469$\mu$ which were relatively large as compared with the recommended droplet sizes in liquid flow rate of 17.2 m$/ell$s with air flow rate of 16660$m^3$/s on the maximum travel distance of about 4.0 m. The velocity of air stream at the point where two fluids, air and liquid, impact each other, was tried to maximize as much as possible in order to enhance the atomization performance of a newly designed twin fluid nozzles with the same or better level of performance of the conventional mist blower, The configuration of nozzle orifice should be designed to enlarge the contact area between air and liquid to enhance the atomization.

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Presumption on the Failures, the Causes and the Reliability of the Mist and Dust Blower (미스트기 부품의 고장실태조사에 의한 신뢰성의 예측)

  • 금동혁;최재갑
    • Magazine of the Korean Society of Agricultural Engineers
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    • v.17 no.1
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    • pp.3702-3711
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    • 1975
  • This study was originated to investigate the imparired parts of the mist and dust blowers and intended to analyze the causes of their failures by the use of the Weibull probability paper. By the use of the paper, the parts which were needed to change the design, the force of the urgency, the mean time between failures of the parts and the basic causes of the troubles could be predicted. The survey showed that the following parts got out of order: (A) flexible rubber hose, (B) blowing fan, (C) lead valve, (D) piston ring. (E) crank main bearing, (F) coil in magneto and (G) needle valve in carburettor. The analysis of the survey indicated that the parts G, C, E and D were belonged to "wear-out failure", and that the mean time between failures became shorter in order as indicated above. To insure longer lives of those parts, it would be necessary to change the design and the material and to upgrade operators mechanical technique of the mist and dust blower. The failure of the parts A, B and F was classified as "randomfailure", and they did not seem to be the "wear-out" at that time. The parts B and F was evaluated as "initial failure". Quality controls and operating tests by the producer. and the operational training for users should be strengthened so as to eliminate these failures. Were the failures only in the parts A, C, D, E, F and G, it could be said that the "reliability" of the mist and dust blower would fall to 10 percent in the second year, and 50 percent of the mist and dust blowers would fail in all parts A, C, D, E, F and G before the blower would have control insect and disease in 58.2 hectares. The use of the Weibull probability paper for analyzing failures of the mist and dust blowers was effective in that it analyzed failure in the relationship between strength of the parts and users actual circumstanoes.

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Development of Defogger Equipped with a Roller Horsehair Brush

  • Ma, Chang-Jin;Kasahara, Mikio;Cao, Renqiu
    • Asian Journal of Atmospheric Environment
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    • v.10 no.4
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    • pp.226-231
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    • 2016
  • In order to remove fog often causes various troubles in our daily lives, the novel defog blower equipped the roller brush made of recycled horse's mane hair was developed. This work presents the overview of new defog devices and the experimental data obtained at two different kinds of defogging experiments. In the model experiment carried out at the enclosed cleanroom ($W5.9m{\times}L5.1m{\times}H2.4m$) targeted a vinyl house, fog was dissipated in less than 30 seconds in case with wind entrainment and two minutes 45 seconds in case without wind entrainment after running of the newly designed defog blower. When the demisting blower was run in a duct, it has an excellent mist sweeping qualities as well as a great removal effect for the background particles (89.5% and 65.4% scavenging rates for fine and coarse particles, respectively). It can be therefore said that the mist eliminator presented in this paper is ideal for use in the sealing space like a vinyl house and the industrial sites where required to remove both harmful mist and particle.

Fire Suppression Effect of PPV with Water Mist System (미세물분무를 이용한 PPV의 화재진압효과)

  • Kim, Sung-Won;Shin, Chang-Sub
    • Journal of the Korean Society of Safety
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    • v.18 no.4
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    • pp.71-77
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    • 2003
  • To inject fresh air into a fire room, Positive Pressure Ventilation (PPV) can be used and the blower of PPV increases inside pressure of the room. It makes high flow rate of products of combustion, smoke and heat from the structure, and it is very helpful to fireman on the fire extinguishing work. The flame moves to the direction of airflow and the temperature of flame can be decreased rapidly. In this experiment, a water mist system is applied to PPV to increase the effectiveness, and various effective factors are studied. n-Heptane and pine wood stick were used as fuel. Temperatures at the above and behind the combustion pan were strongly reduced by the water mist system and by the convective cooling with airflow. The smoke density was also decreased by PPV with water mist system and it can be explained by the absorption of smoke particles on the water mist droplet and by the strong exhausting effects of mobile fan.

Full-scale Fire Suppression Test for Application of Water Mist System in Road Tunnel (미분무수 소화시스템의 도로터널 적용을 위한 실물 화재 실험)

  • Han, Yong-Shik;Choi, Byung-Il;Kim, Myung-Bae;Lee, Yu-Whan;So, Soo-Hyun
    • Fire Science and Engineering
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    • v.25 no.3
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    • pp.51-56
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    • 2011
  • The full-scale experiments are carried out to investigate the fire suppression characteristics of water-based fire fighting systems in a road tunnel. Applied systems are the low-pressure water spray system at 3.5 bar and the high-pressure water mist system at 60 bar. The water flow rate of the high-pressure system is one sixth only of the water spray system. A passenger car and a heptane fuel pan with area of $1.4m^2$ are used as fire sources. A blower system is installed at the tunnel exit to realize the longitudinal ventilation conditions (0.9~3.8 m/s) in the tunnel. Temperatures from the fire source to the down-stream direction are measured by K-type thermocouple trees. The experimental results show that the cooling effect of the high pressure water mist system in the test conditions were equivalent to that of the low pressure water spray system for B-class fire.

A Study on Performance Evaluation for Oil Mist Removal using a High-speed Centrifugal Cyclone (고속원심분리 사이클론을 이용한 오일 미스트 제거 성능 연구)

  • Kim, SooYeon;Kim, Jin-Seon;Sung, Jin-Ho;Han, Bangwoo;Kim, Yong-Jin;Kim, Hak-Joon
    • Particle and aerosol research
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    • v.15 no.4
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    • pp.139-148
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    • 2019
  • This study was performed for the application of a high-speed centrifugal cyclone to shale gas mining process. This device uses the centrifugal force to control particles similar to typical cyclones, and the disk located inside the cyclone is forced to rotate using a motor. The pressure difference occurred during the rotating of disk. Hence, inflow rate was generated without a blower fan. In addition, flow rate increased with elevating rpm of motor. The installing the disk in multiple stages on the inner rotor increased the instantaneous disk outlet flow. Hence, the control efficiency of oil particle increased from 1.05% to 31.2%. By modifying the structure of the disk so that the air flow to the opposite direction of the cyclone, the control efficiency of oil particles increased to 81.5%. By increasing the capacity of the motor and the size of the disk, the flow rate was increased to 2.5 ㎥/min because the rpm of motor and pressure difference increased. As rpm of motor increased, the cut-off diameter (dpc) became smaller. Unlike the Lapple's equation, dpc was inversely proportional to the effective number of rotations (Ne). The control efficiency was maintained even if the concentration of oil particles increased, for this reason, the higher the oil concentration, the more particles were accumulated and controlled.