• 제목/요약/키워드: Gear accuracy

검색결과 147건 처리시간 0.027초

호이스트 기어박스의 소음불량률 저감을 위한 실험적 연구 (An Experimental Study to Reduce the Fraction of Noise Defect of Hoist Gear Boxes)

  • 이희원;손병진;신용하
    • 대한기계학회논문집
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    • 제18권5호
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    • pp.1347-1354
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    • 1994
  • This paper deals with the experimental research, including measurement and analysis and field survey, on the causes of occurring noise defective gear boxes in hoist production plant in order to reduce the fraction of their occurrence. In this reserch following investigations are performed : measurement and gear-boxes, examination of each machining process of production, measurement and analysis of dimensional accuracy of each part, comparative vibration test with exchanging inaccurate parts. From these investigations, it is found that the machining accuracy of pinion gear tooth thickness is the most sensitive factor of noise problem. By maintaining the tooth thickness error within 0.05 mm tolerance in the gear cutting process, the fraction of noise defective gear-boxes are greatly reduced to less than 2%, where the usual rate of it has been 20-50%.

산업용 취출로봇의 소음 저감에 대한 연구 (Study on Noise Reduction of an Industrial Take-out Robot)

  • 조재연;김덕수;정진태
    • 한국소음진동공학회논문집
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    • 제21권1호
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    • pp.41-46
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    • 2011
  • In this paper, we experimentally investigate factors that decrease in noise of a industrial take-out robot at driving state. For this, we analyse change in the noise of the take-out robot with gear machining accuracy and clearance. In order to calculate the noise related to gear machining accuracy that is based upon the Japanese Industrial Standard(JIS), we equally increase motor speed from 0 rpm to 1250 rpm. In addition, to investigate influence of clearance on noise, we evenly change clearance from 0.5 mm to 1.2 mm. These experiments show that clearance is more effective factor than gear machining accuracy to reduce the noise of the take-out robot.

엔진용 백래쉬 방지 기어의 Fp Z/8에 관한 연구 (A Study on Fp Z/8 of Anti-Backlash Gear in an Engine)

  • 종흥;려건화;로호;주서;곽검우;개랑;진진;장기;류성기
    • 한국기계가공학회지
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    • 제19권10호
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    • pp.24-30
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    • 2020
  • The high speed of an engine balance box may cause significant additional gear noise. Gear accuracy is the most useful key to reduce gear noise, but the small tooth width and thin-walled anti-backlash gear introduce challenges to the manufacturing process. In order to reduce the gear noise caused by gear pitch error, this paper investigates the correlation between influencing factors and gear pitch error by analyzing the processing technology, tooling fixture, and equipment accuracy. By improving the process and optimizing the gear design, the gear machining accuracy was improved and the processing cost was saved.

Development of the Sub Gear for the Scissors Gear System for Automobile Engines

  • Nakazawa, Katsuhito;Nagata, Toshihiko;Motooka, Naoki
    • 한국분말야금학회:학술대회논문집
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    • 한국분말야금학회 2006년도 Extended Abstracts of 2006 POWDER METALLURGY World Congress Part2
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    • pp.756-757
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    • 2006
  • P/M enables the economical production of components for many kinds of gears. Functionally, the sub gear requires high tooth accuracy and bending fatigue strength. The whole tooth profile was sized after sintering to satisfy the gear tooth accuracy specification. The part was redesigned to reduce machining requirements. The required bending fatigue strength was achieved through appropriate material choice and induction of compressive residual stress by shotpeening after carburizing. The P/M sub gear replaced a forged steel gear, satisfied performance requirements, expanded the use of P/M applications and provided over 30% cost reduction.

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합금강을 이용한 스퍼기어의 정밀 냉간 단조 (Precision Cold Forging of Spur Gear Using the Alloy Steel)

  • 최재찬;최영
    • 소성∙가공
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    • 제6권6호
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    • pp.500-507
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    • 1997
  • The conventional closed-die forgings had been applied to the forging of spur gears. But the forgings require high forging-pressure. In this paper, new precision forging technology have been developed. The developed technology is two steps forging process. Good shaped products are forged successfully with lower forging-pressure than those of conventional forging. The accuracy of the forged spur gear obtained by new precision forging technology is set nearly equal to that of cut spur gear of fourth and fifth class in Korean industrial standard.

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냉간 단조 스퍼어 기어의 금형과 단조품의 인볼류트 곡선 변화 연구 (A study on the changes of involute-curve of spur gear die for cold forging and forged part)

  • 천세환;이정환;이영선;배원병
    • 한국소성가공학회:학술대회논문집
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    • 한국소성가공학회 2003년도 춘계학술대회논문집
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    • pp.44-48
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    • 2003
  • In metal working, cold forging that has profit to satisfy dimension accuracy is using in various manufacturing products. Recently, most of the interest thing is precision forging of gear, Gear forging product is more strength than broaching gear, and it has many advantages with reduction of factory expenses. The reason of difficulty to improve accuracy of gear dimension compare to another products is the dimension accuracy is very high, approximately 10$\mu\textrm{m}$, and because die of involute teeth and elastic strain of forged tool differ from standard curve. This paper represent quantitative analysis of die and teeth of forged tool, namely difference of curves, with experiments and analyze the factor of dimension gap, finally, will design compensated involute curve.

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베벨기어 제조 공정에서 베벨기어의 정도 및 급수에 미치는 인자 (Factors affecting accuracy or grade of bevel gears during manufacturing)

  • 전병윤;엄재근;박정휘;전만수
    • 한국소성가공학회:학술대회논문집
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    • 한국소성가공학회 2008년도 추계학술대회 논문집
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    • pp.405-409
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    • 2008
  • In this paper, factors affecting accuracy or grade of forged bevel gears are investigated in the experimental way. Two materials of SKD-11 and copper. two machining conditions and two machines of WIA-V50 and Roders-RFM600 are particularly investigated to reveal their effects on the grade of bevel gear forging dies in this study. It has been shown that the bevel gear grades are much affected by all the factors tested, revealing that it is of great significance to find the optimal machining process of die making to develop or manufacture a high precision bevel gear and that the bevel gear is degraded by one from the grade of its related die during forging.

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냉간 단조시 인볼류트 곡선 변화 예측을 위한 유한요소 해석 (FE Analysis to predict the changes of involute-curve during cold-forging)

  • 천세환;이정환;이영선;배원병
    • 한국소성가공학회:학술대회논문집
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    • 한국소성가공학회 2003년도 추계학술대회논문집
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    • pp.34-38
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    • 2003
  • In metal working, cold forging that has profit to satisfy dimension accuracy is using in various manufacturing products. Recently, most of the interest thing is precision forging of gear. Gear forging product is more strength than broaching gear, and it has many advantages with reduction of factory expenses. The reason of difficulty to improve accuracy of gear dimension compare to another products is the dimension accuracy is very high, approximately 10$\mu\textrm{m}$, and because die of involute teeth and elastic strain of forged tool differ from standard curve. This paper represent quantitative analysis of die and teeth of forged tool, namely difference of curves, with experiments and analyze the factor of dimension gap, finally, will design compensated involute curve.

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자동차용 고정밀 시트 리클라이너의 기어성형 공정에 관한 연구 (A Study on Gear Forming Process for High Precision Automotive Seat Recliner)

  • 강길석;박민제;장명진;김병민;고대철
    • 소성∙가공
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    • 제25권4호
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    • pp.268-274
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    • 2016
  • In the automotive seat industry, the use of a fine blanking press is important for manufacturing of high precision products. Among them, a gear part which is a main component of an automotive seat recliner is generally manufactured by fine blanking press. However, the use of conventional mechanical press has been increasing in manufacture of gear part because of low productivity of fine blanking press. In this study, new forming process is suggested to fabricate the gear part with high precision by using mechanical press. The effect of flow restriction die (FRD) which has the restriction of blank edge on dimensional accuracy is investigated by FE-analysis. FE-analysis results for different conditions of FRD indicated that FRD has high dimensional accuracy with the lowest roll-over and the highest perpendicularity of gear part. After application to fabrication of the gear part using mechanical press, the measured dimensional characteristic was compared with the required specification of final product. In addition, results of the performance test showed that the product fabricated by developed process satisfied the required strength and durability. The results show that the suggested forming process by using FRD and mechanical press can replace fine blanking on the viewpoint of dimensional accuracy and productivity.