• Title/Summary/Keyword: Gas pipe

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Comprehensive Consideration on the Discharge of Gases from Pressurized Vessels through Pressure Relief Devices (압력용기로부터 압력방출장치를 통한 가스 방출에 관한 포괄적 고찰)

  • Chung, Chang-Bock
    • Journal of the Korean Society of Safety
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    • v.35 no.6
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    • pp.32-45
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    • 2020
  • The problem of determining the discharge rates of gases from pressurized vessels through pressure relief devices was dealt with comprehensively. First, starting from basic fluid flow equations, detailed modeling procedures were presented for isentropic nozzle flows and frictional flows in a pipe, respectively. Meanwhile, physical explanations were given to choking phenomena in terms of the acoustic velocity, elucidating the widespread use of Mach numbers in gas flow models. Frictional flows in a pipe were classified into adiabatic, isothermal, and general flows according to the heat transfer situation around the pipe, but the adiabatic flow model was recommended suitable for gas discharge through pressure relief devices. Next, for the isentropic nozzle flow followed by adiabatic frictional flow in the pipe, two equations were established for two unknowns that consist of the Mach numbers at the inlet and outlet of the pipe, respectively. The relationship among the ratio of downstream reservoir pressure to upstream pressure, mass flux, and total frictional loss coefficient was shown in various forms of MATLAB 2-D plot, 3-D surface plot and contour plot. Then, the profiles of gas properties and velocity in the pipe section were traced. A method to quantify the relationship among the pressure head, velocity head, and total friction loss was presented, and was used in inferring that the rapid increase in gas velocity in the region approaching the choked flow at the pipe outlet is attributed to the conversion of internal energy to kinetic energy. Finally, the Levenspiel chart reproduced in this work was compared with the Lapple chart used in API 521 Standatd.

Thermal and Flow Analysis of Organic Rankine Cycle System Pipe Line for 250 kW Grade Waste Gas Heat Recovery (250kW급 폐열회수 시스템용 유기랭킨사이클 배관 열유동해석에 관한 연구)

  • Kim, Kyoung Su;Bang, Se Kyoung;Seo, In Ho;Lee, Sang Yun;Yi, Chung Seob
    • Journal of the Korean Society of Manufacturing Process Engineers
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    • v.18 no.4
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    • pp.26-33
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    • 2019
  • This study is a thermal and flow analysis of Organic Rankine Cycle (ORC) pipe line for 250 kW grade waste gas heat recovery. We attempted to obtain the boundary condition data through the process design of the ORC, which can produce an electric power of 250 kW through the recovery of waste heat. Then, we conducted a simulation by using STAR-CCM+ to verify the model for the pipe line stream of the 250 kW class waste heat recovery system. Based on the results of the thermal and flow analyses of each pipe line applied to the ORC system, we gained the following conclusion. The pressure was relatively increased at the pipe outside the refracted part due to the pipe shape. Moreover, the heat transfer amount of the refrigerant gas line is relatively higher than that of the liquid line.

Validation of diesel engine gas flow one-dimensional numerical analysis using the method of characteristics (특성곡선법을 이용한 디젤엔진 가스유동 1차원 수치해석의 타당성 평가)

  • KIM, Kyong-Hyon;KONG, Kyeong-Ju
    • Journal of the Korean Society of Fisheries and Ocean Technology
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    • v.56 no.3
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    • pp.230-237
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    • 2020
  • In order to design a diesel engine system and predict its performance, it is necessary to analyze the gas flow of the intake and exhaust system. A gas flow analysis in three-dimensional (3D) format needs a high-resolution workstation and enormous time for analysis. Therefore, the method of characteristics (MOC) was used for a gas flow analysis with a fast calculation time and a low-resolution workstation. An experiment was conducted on a single cylinder diesel engine to measure pressure in cylinder, intake pipe and exhaust pipe. The one-dimensional (1D) gas flow was analyzed under the same conditions as the experiment. The engine speed, valve timing and compression ratio were the same conditions and the intake pressure was inputted as the experimental results. Bent pipe such as an exhaust port that cannot be realized in 1D was omitted. As results of validation, the cylinder pressure showed accuracy, but the exhaust pipe pressure exhibited inaccuracy. This is considered as an error caused by the failure to implement a bent pipe such as an exhaust port. When analyzed in 3D, calculation time required 61 hours more based on a model of this study. In the future, we intend to implement a bent pipe that cannot be realized in 1D using 3D and prepare a method to supplement reliability by using 1D-3D coupling.

Heat Recovery Characteristics of the Exhaust Heat Recovery System with Heat Pipe Unit Attached to the Hot Air Heater in the Greenhouse (히트파이프를 이용한 온풍난방기 배기열회수 시스템의 열회수 특성)

  • Kang, K. C.;Kim, Y. J.;Ryou, Y. S.;Baek, Y.;Rhee, K. J.
    • Journal of Biosystems Engineering
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    • v.26 no.5
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    • pp.441-448
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    • 2001
  • Hot air heater with light oil combustion is used as the most common heater for greenhouse heating in the winter season. However, exhaust gas heat discharged to atmosphere through chimney reaches up to 10~20% of total heat capacity of the oil burred. In order to recover the heat of this exhaust gas and to use for greenhouse heating, the heat pipe type exhaust heat recovery system was manufactured and tested in this experiment. The system consisted of a heat exchanger made of heat pipes, ø15.88${\times}$600mm located in the rectangular box of 675(L)${\times}$425(W)${\times}$370(H)mm, an air suction fan and air ducts. The number of heat pipe was 60, calculated considering the heat exchange amount between exhaust gas and air and heat transfer capacity of a heat pipe. The working fluid of heat pipe was acetone because acetone is known for its excellent heat transfer capacity. The system was attached to the exhaust gas path. According to the performance test it could recover 53,809 to 74,613kJ/h depending on the inlet air temperature of 12 to -12˚at air flow rate of 1.100㎥/h. The temperature of the exhaust gas left the heat exchanger dropped to 100$^{\circ}C$ from 270$^{\circ}C$ after the heat exchange between the suction air and the exhaust gas.

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Analysis of Transient Thermal Characteristics in a Gas-Loaded Heat Pipe (가스내장 히트파이프의 과도 열특성 해석)

  • 박병규;김근오;김무근
    • Korean Journal of Air-Conditioning and Refrigeration Engineering
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    • v.13 no.6
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    • pp.514-523
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    • 2001
  • The thermal performance characteristics of gas-loaded heat pipe(GLHP) were investigated by using transient diffuse-front model. Numerical evaluation of the GLHP is made with water as a working fluid and Nitrogen as control gas in the stainless steel tube. The transient vapor temperature and wall temperature were obtained. It is found that the temperature profiles and gas mole fraction distribution have been mainly influence by the diffusion between working fluid and noncondensable control gas in the condenser of GLHP. It is also found that he large power input make the diffusion region smaller.

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Application of a Large Scale Heat Pipe System to Preheating the Fuel Gas of Low Heating Value (분리형 히트파이프의 저발열량 연료가스 예열시스템에 대한 적용연구)

  • Park, Heung Soo;Riu, Kap Jong;Lee, Jin Ho;Lee, Yong Kuk
    • Transactions of the Korean Society of Mechanical Engineers B
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    • v.23 no.9
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    • pp.1085-1097
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    • 1999
  • A separate heat pipe system capacity of 3,700kW has been developed and applied to preheating the blast furnace gas for recovery of the waste heat from boiler. The system is designed to preheat the blast furnace gas up to $126^{\circ}C$ by using tho boiler exhaust gas of which temperature is $180^{\circ}C{\sim}220^{\circ}C$. The arrangement of the fin tubes as well as the shape of the fin has been carefully determined to minimize the fouling problems. The heat pipe system was found to be stable in circulation of the working fluid and the range of the temperature variation of the preheated blast furnace gas was within $10^{\circ}C$. It was proved through a long-term test that the selected tube arrangement and the shape of the fins are proper to prevent the fouling problems and that the pay-back period of the system Is within one year.

Safety Assessment of By-product Gas Piping after Design Change (부생가스 연료배관의 설계변경에 따른 안전성 평가)

  • Yoon, Kee Bong;Nguyen, Van Giang;Nguyen, Tuan Son;Jeong, Seong Yong;Lee, Joo Young;Kim, Ji Yoon
    • Journal of the Korean Institute of Gas
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    • v.17 no.2
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    • pp.50-58
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    • 2013
  • Various process piping usually carries out high flammable and explosible gas under high pressure and high temperature. Due to frequent change of design and structure it becomes more complicated and compactly located. The safety management level is relatively low since it is considered as simply designed component. In this study a safety assessment procedure is proposed for complicated piping system around a mixing drum in which natural gas and by-product gases were mixed. According to ASME code, pipe stress analysis was conducted for determining design margin at some key locations of the piping. These high stress locations can be used as major inspection points for managing the pipe integrity. Sensitivity analysis with outside temperature of the pipe and support constraint condition. Possible effect of hydroen gas to the pipe steel during the previous use of the by-product gas was also discussed.

RFID Applicability Study to Prevent the Third Party Accident of LNG Pipe Line (가스관 굴착사고 예방을 위한 RFID 인식기술의 적용성 연구)

  • Han, Sang-Wook;Park, Su-Ri;Kim, Byung-Jick
    • Journal of the Korean Institute of Gas
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    • v.16 no.2
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    • pp.1-8
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    • 2012
  • According to the last 5 year statistics of KGS, there occurred 22 under ground gas pipe accidents per year in Korea. And about 5 accidents per year were caused from the third party digging. IT recognition technique could reduce such underground gas accidents. Among IT recognition technique, RFID is most poplar. In the air, RFID were applied to various fields including the distribution industry, but underground condition, the research and application cases of RFID were little This research was undertaken to see the applicability of RFID to underground gas pipe safety. By use of 900 MHz RFID reader and commercial metal tag, the stable recognition distance was measured in the similar underground condition of LNG pipe. Stable recognition depth of RFID tag were measured to be 50, 45, 25 cm in the medium of soil, 5 cm-thick-concrete+soil, and water respectively. The measured distances were considered to be the meaningful distance to prevent the gas pipe accidents Also the efficient ways to input the required gas pipe data to the 24 byte metal tag were proposed. Application of RFID to underground LNG supply system will not only reduce the gas accidents due to third party digging but also improve the gas line maintenance efficiency.

Effect of Refrigerant Pipe Length on Sea Water Cooling System Performance (해수냉각시스템 성능에 미치는 냉매배관길이의 영향)

  • Yun, Jeong-In;Jo, Yeong-Je
    • Journal of the Korean Society of Fisheries and Ocean Technology
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    • v.34 no.3
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    • pp.346-351
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    • 1998
  • The purpose of this study is analyzing the performance of sea water cooling system under various refrigerant pipe length. In sea water cooling system, the increase of refrigerant pipe length cause increases of pressure drops. These pressure drops cause fresh gas in liquid pipe and increase specific volume in gas pipe outlet, so sea water cooling system capacity is decreased by decrease of refrigerant mass flow rate. Sea water cooling system capacity in refrigerant pipe length 70m is decreased more than 30% when compared with pipe length 10m and the decrease of the coefficient of performance is nearly 20%.

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Experimental Study on Naphthalene Heat Pipe Heat Exchanger for Middle-high Temperature Heat Recovery (중고온 범위 폐열회수용 나프탈렌 히트파이프 열교환기에 대한 실험적 연구)

  • Chung, Won-Bok;Park, Soo-Yong;Hwang, Seon-Hong
    • Proceedings of the SAREK Conference
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    • 2007.11a
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    • pp.64-69
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    • 2007
  • This study is to develop heat recovery system using high performance heat pipe heat exchanger for Middle-high temperature range industrial exhaust gas. The naphthalene is used as working fluid of heat pipe in this study. Single naphthalene heat pipe could transport over 2,000 watts with $0.05^{\circ}C/W$. The heat pipe heat exchanger consist of 50 naphthalene heat pipes recovered 62 kW when over $400^{\circ}C$ gas exhausted and the maximum recovered heat rate was 173 kW in this study.

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