• 제목/요약/키워드: Feeding-rotating rate

검색결과 17건 처리시간 0.03초

박피 마늘의 품위판정 기술개발에 관한 기초연구(I) -영상식 마늘 선별기용 반전장치 개발- (Basic Study on Quality Evaluation Technique for Peeled Garlics(I) -Rotation sytem for vision-based garlic sorter-)

  • 이종환;이성범;안청운
    • Journal of Biosystems Engineering
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    • 제26권3호
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    • pp.271-278
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    • 2001
  • Many workers in the garlic peeling factory are separating the sound peeled garlics from the unpeeled and defective ones in a manual way. In order to reduce the seasonal labor requirement and operating cost, the mechanized garlic sorting system such as the vision-based garlic sorter should be developed. This study was conducted as one of basic studies on developing quality evaluation technique for peeled garlics, especially to developed the system for acquiring the whole surface images of garlics with a CCD camera. The following results were obtained from this study. 1. The belt-type garlic rotation system was devised to apply for the vision-based garlic sorter and was tested to decide the criteria of design and optimum conveying speed. 2. To evaluate the performance of the developed garlic rotation system, feeding rate and rotating rate were measured under the conditions of four experimental factors such as the inclined angle of rotating belt, the inclined angle of feeding belt, the height of plate arrays on feeding belt and the conveying speed of belts. And the capacity of the system according to mixture ratios of peeled garlics and unpeeled garlics was analyzed as a feasibility test. 3. For the inclined angle of rotating belt 20°and height of plate array on feeding belt 22㎜, the maximum rotating rate for garlic samples including unpeeled ones was 81.1% at the conveying speed of 4.2 garlic/sec. And under these condition, the maximum feeding rate was 85% at the inclined angle of feeding belt 6.5°. 4. The capacity of the developed garlic rotation system was almost constant regardless of mixture ratio of peeled garlics and unpeeled garlics and its range was 2.95∼3.92 garlic/sec. At the conveying speed of 4.2 garlic/sec, the capacity of the garlic rotation system was calculated ad 58∼64 kg/hr. 5. To improve performance of the garlic rotation system, it is recommended to develop a device to slide garlics into feeding belt.

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회전원판 반응조에 고정화시킨 Aspergillus sojae B-10에 의한 반응성 염료의 탈색 (Biodergradation of Reactive Dyes Using Multistage Rotating Disc Contactor Immobilized by Aspergillus sojae B-10)

  • 류병호;김동석;진승록;정종순;원용돈
    • 한국환경보건학회지
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    • 제21권4호
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    • pp.49-55
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    • 1995
  • Dyes are released into the environment as industrial wasterwater. Dyes are considered to be a pollution problem because of the wide spread into environment with a variety of colors. Continuous biodegradation of reactive dyes such as Rifacion Red H-3EB, Rifazol Blue BT, Rifacion Yellow P4G and Rifacion Brown RT were demonstrated using multistage rotating disc contactor immobilized by Aspergillus sojae B-10. Aspergillus sojae B-10 was cultivated the optimal medium containing 2.0% glucose, 0.08% $NaNO_3$, 0.1% $KH_2PO_4$ and 0.5% $MgSO_4\cdot 7H_2O$, pH 5 at 32$\circ$C. Mycelium of Aspergillus sojae B-10 were guck to the rotating disc for 10 days until steady state. For continuous biodegradation of reactive dyes by using rotating disc contactor, it was most effective biodegradation in the medium containing 1,000 ppm each dyes at the medium feeding rate of 20 ml per hour. Under the conditions biodegradation of each dyes on 2, 4 and 6 days were 20~50%, 75% and 96%, respectively. Therefore, practical application of reactive dyes were carried out at the feeding rate of 20 ml/h as synthetic wasterwater containing 500 ppm of mixture reactive dyes. It was found the highest levels of 94% biodegradation during 20 days.

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양돈 급여에 적합한 원형베일 사일리지 해체·세절·연화 일관시스템 연구 (I) (A Study on the Integrated Unrolling, Cutting, and Softening System of Round Bale Silage for Pig Feeding (I))

  • 홍종태;김혁주;유병기;현창식;김성기;유지수;홍영신;서형덕
    • 한국축산시설환경학회지
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    • 제19권1호
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    • pp.9-18
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    • 2013
  • Currently, there was no producing system of TMR for pig feeding in Korea. In this study, we examined unrolling, cutting, and softening for the round bale silage. We designed and developed the prototype system of round bale silage for pig feeding. Unroll method were lower chain conveying and upper belt conveying which includes an hydraulic vertical fodder knife. Gathering and cutting method were rotating auger and flywheel which have 10 cutters, input roller of 280 rpm, and cutter rotating speed of 1,750 rpm. Softening device was rotating hammer in inclined cylinder adjustable to $25^{\circ}C$ and rotating speed up to 1,300 rpm. The prototype system was integrated working for unrolling, cutting, and softening. We found that when the round bale silage in unrolling apparatus cut length of 20 cm to input cutting apparatus, the cutting performance was well in continuous working up to input rate of 1,000 kg/h, the softening apparatus was working well.

Factors Affecting Performance of Rotary Impact-Type Threshers for Sesame and Perilla Harvesting

  • Pang, Yeoun Gyu;Kim, Sang Hun;Jun, Hyeon-Jong
    • Journal of Biosystems Engineering
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    • 제43권3호
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    • pp.185-193
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    • 2018
  • Purpose: The purpose of this study was to analyze the performance factors of a rotary impact-type thresher to develop a sesame and perilla thresher, specifically to analyze the cut length of the stems and the threshing rates based on the relationship between the blade velocity and feeding speed. Methods: The materials were dried within a range of 12.3-13.0% to test the impact cut by bending. The cut lengths of the perilla and sesame stems were categorized in 6 ranges (~7.0, 7.1-10.0, 10.1-13.0, 13.1-16.0, 16.1-20.0, 20.1- (cm)). For testing the cut length and threshing rate, the upward-rotating blade velocity was varied as 11.0 m/s, 13.5 m/s, and 22.3 m/s. Feeding speeds were changed from 0.1 m/s to 2.2 m/s by the inverter connected to the feed motor. The feed rate and threshing rates without cover-casing were evaluated with the factors of thresher testing. Results: The mean cut length of the stem decreased as the blade velocity increased and/or the feeding speed decreased. As the feed rate increased up to 17.5 g/s, the cut length distributions showed no significant difference. The threshing rate was 98.9% for sesame, and flexible according to the blade velocity and feeding speed of the perilla. Conclusion: Feeding material too fast could produce longer cut stem segments, therefore, a feeding speed less than 2.2 m/s is recommended. A blade velocity of 13.5 m/s is preferable for both sesame and perilla with regard to cut length and threshing rate.

급액속도가 원심식 박막증발기의 운전 특성에 미치는 영향 (Effect of Feeding Rate for Operation Properties of Centrifugal Thin Film Evaporator)

  • 김병삼;박노현;박무현;한봉호
    • 한국식품과학회지
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    • 제23권4호
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    • pp.437-441
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    • 1991
  • 원심식 박막증발기를 이용해 마늘착즙을 증발 농축하면서 급액속도가 증발표면에서의 액의 흐름상태와 운전 특성에 미치는 영향에 대해서 조사하였다. 급액속도 $25{\sim}125kg/h$의 운전 조건하에서 증발표면에서의 이론적인 박막의 두께는 $0.52{\sim}0.89mm$ 그리고 체류시간은 $1.77{\sim}6.75$초로 계산되었다. 한편 Reynolds number로 판단해 볼 때 증발표면에서의 마늘착즙의 흐름은 대체로 층류로 여겨졌다. 일정한 증기 및 증발온도 조건하에서 농축비는 급액속도가 증가함에 따라 감소한 반면 증발속도와 총괄열전달계수는 어느 일정한 값까지 증가하다가 감소하는 경향을 나타내었다. 그리고 급액속도 $25{\sim}125kg/h$(증발온도 $40^{\circ}C$, 증기온도 $95{\sim}120^{\circ}C$, 급액의 초기농도 $32^{\circ}Brix$)에서 농축비는 $1.04{\sim}2.04$, 총괄열전달계수는 $3,074.33{\sim}17,614.70kJ/m^{2}{\cdot}h{\cdot}^{\circ}C$ 였다.

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칩마운터의 직진 테이프 피더 설계 및 평가 (Mechanical Design and Evaluation of Linear Tape Feeder for Chip Mounter)

  • 이수진;강성민;이창희;김용연
    • 한국정밀공학회지
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    • 제23권5호
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    • pp.155-161
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    • 2006
  • This paper introduces a new type of mechanical tape feeder for chip mounter. The mechanical feeder is composed of a pneumatic linear actuator and a linear feeding module with the application of a cam-slider. As semiconductor chips are getting smaller, PCB assembly makers require the feeder to position the chip with high accuracy. The linear feeding system improves the positioning accuracy of the chip by getting rid of the index error, which brings into existence on the sprocket rotating feeder. It also can make greatly reduce the dumping rate. The dumping error is caused by the impact occurred as the pawl to interrupt ratchet wheel rotation. The paper discusses its mechanism and mechanical performance. The positioning accuracy and the dynamic characteristic were measured for long time operation and analyzed. As a result, the feeder showed very good performance. However, the feeding system was dynamically unstable due to the cover film eliminator that is required to be modified

영상처리식 온라인 품위판정을 위한 현미의 정렬공급장치 (Echelon Feeder of Brown Rice for On-line Inspection Using Image Processing)

  • 김태민;노상하
    • Journal of Biosystems Engineering
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    • 제35권3호
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    • pp.197-205
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    • 2010
  • An automatic echelon feeder of brown rice was presented for quality inspection system using color image processing. A echelon feeder was developed with vibratory feeder and cylindrical indent singulator having oblique light. The vibratory feeder consisted of a hopper, electromagnetic vibrator and multichannel grooves and supply the grain sample to the singulator. The feeding performance such as feed rate, blocking frequency of the channel was dependent on the size of groove and vibration pattern. A cylindrical indent singulator consisted of a rotating cylinder, prisms and a tungsten-halogen light source. It delivered grain kernels under the camera in a echelon form and illuminate the kernels with oblique ray and ambient light. The size of the indents installed on the surface of the rotating cylinder was determined by the dimensions of the paddy and a small triangular prism was placed in each indent to apply $ 20^{\circ}$ oblique light to the grain kernel.

네오디뮴 영구자석을 이용한 컨베이어벨트 구동형 미세칩 포집장치의 성능 평가 (Performance Evaluation of Microchip Removal Device Rotating by Conveyor Belt with Neodymium Permanent Magnet)

  • 최성윤;왕준형;왕덕현
    • 한국기계가공학회지
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    • 제20권1호
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    • pp.103-109
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    • 2021
  • Fine chips generated by machining have an impact on machine failure and quality of machined products, it is necessary to remove the chips, so the microchip collection and removal device by rotating conveyor belt with neodymium permanent magnets was developed. In this research, to solve the problem for reducing the existing microchips in the tank, a micro-chip removal device by rotating conveyor belt with neodymium permanent magnets developed. In the development of micro-chip removal device, 3D CATIA modeling was used, and the flow analysis and the electromagnetic force analysis were performed with COMSOL Multiphysics program. To evaluate the performance of the prototypes produced, design of experiments (DOE) is used to obtain the effect of neodymium conveyor movement speed on chip removal for the ANOVA analysis of recovered powders. An experiment was conducted to investigate the effect of the conveyor feed rate on the chip removal performance in detail. As a result of the experiment, it was confirmed that the slower the feeding speed of the fine chip removing device, the more efficient the chip removal.

회전원판 반응조를 이용한 Pseudomonas sp. KS-96에 의한 gallic acid로부터 Pyrogallol의 전환 (Bioconversion of Pytogallo from Gallic Acid by Pseudomonas sp. KS-96 using Rotating Disc Contactor)

  • 안성만;김동석;정영기;임복규;이홍수;류병호
    • 생명과학회지
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    • 제7권2호
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    • pp.112-118
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    • 1997
  • Gallic acid로부터 pyrogallol로 전환하는 균주를 토양에서 분리 동정하여 얻는 Pseudomonas sp. KS-96의 균체를 회전원판 반응조에 고정화시킨 후 연속전환을 시도하여 다음과 같은 결과를 얻었다. Gallate decarboxylase의 활성은 배양 24시간에서 가장 좋았다. 반응조의 원판에 gallic acid가 함유된 액체 배양액을 시간당 20m${\ell}$씩 공급하면서 균체막의 두께가 steady state에 도달할때까지 공급하였다. 균체를 고정화 시킨 후 시간 경과에 따른 전환율은 18시간부터 36시간에서 전환율이 높았다. 균체 고정화 후에 gallic acid를 15g/${\ell}$ 함유하는 기질을 시간당 30m${\ell}$씩 주입했을 때 pyrogallol의 전환율이 가장 좋았으며 회전원판 반응조에 의한 연속적 전환은 6일에서 8일까지가 각각 81%, 80%로서 가장 높았다.

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원추형(圓錐型) 탈곡기(脱糓機)에 관(關)한 연구(硏究) (Study on Cone Type Thresher (I))

  • 이승규
    • Journal of Biosystems Engineering
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    • 제6권1호
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    • pp.48-59
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    • 1981
  • The major limiting factor on the determination of combine capacity is the frequent occurence of clogging over the some parts of machine when the crop is wet in the case of Japanese self-feeding type combine. And in the case of American conventional combine having big separating parts, the great grain loss and damage occur when the machine is used for rice harvesting. This experiment was carried out to develop the new type threshing and separating equipment. Proto-type thresher which consist of a conical threshing drum and a conical separating sieve rotating around the threshing cone was constructed and tested. In the case of 800 rpm of threshing cone speed, average threshing loss was below 1 percent, separating loss was about 1 percent, grain damage was about 0.4 percent, and average total power required was about 2.6 PS. This design has some problems such as higher power required or wrapping problems under the conditions of feeding long damp straw. But, compared with the conventional combine or thresher, this machine certainly has some potentials for this approach to combine development. The crop feed rate must be increased through improvement of the feeding portion of the threshing cone. And it is required to investigate further about some parameters causing wrapping phenomena.

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