• Title/Summary/Keyword: External combustion engine

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A Study on the Application of the Lean Boosting in a Hydrogen-fueled Engine with the SI and the External Mixture (흡기관 분사식 수소 SI기관의 희박과급 적용에 관한 연구)

  • Lee, Kwangju;Lee, Jonggoo;Lee, Jongtai
    • Transactions of the Korean hydrogen and new energy society
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    • v.24 no.2
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    • pp.136-141
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    • 2013
  • In order to achieve simultaneously the ultra-low NOx, the high power and the high efficiency in a hydrogen-fueled engine with SI and the external mixture, the effects of low temperature combustion, performance and exhaust are compared and analyzed by the application of the lean boosting. As the results, the decrease rate of the high temperature in the hydrogen is less decreased than the other fuels by high constant-volume specific heat. However, when the conditions of 1.7bar and ${\Phi}=0.33$ are reached by the lean boosting, the maximum gas temperature of hydrogen is decreased under the temperature of NOx formation and it is possible to stabilize combustion below 2% of COVimep. Also, at that condition, it is feasible to achieve simultaneously NOx-free and the power of gasoline level. Therefore, it is found that the lean boosting is useful in the hydrogen-fueled engine.

Stability Rating Tests for Optimization of Axial Baffle Length (배플 길이의 최적화를 위한 연소 안정성 평가 시험)

  • Kim, Hong-Jip;Lee, Kwang-Jin;Seo, Seong-Hyeon;Kim, Seung-Han;Han, Yeoung-Min;Seol, Woo-Seok
    • Journal of the Korean Society for Aeronautical & Space Sciences
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    • v.33 no.1
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    • pp.69-77
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    • 2005
  • To optimize and limit the axial length of the baffle of the KSR-III engine, stability rating tests using pulse gun as one of artificial disturbance devices have been done. Generally a rocket engine can be considered to be dynamically stable if a certain imposed external perturbation or pressure oscillation in rocket combustion chamber could be suppressed within a short time period. Decay time and other parameters for the evaluation of stabilization ability of an engine to external perturbation have been analyzed to quantify stabilization capacity of engine, in other words, dynamic stability margin. Baffle not covering flame zone enough which can be considered as collision region of injector wasn't be able to suppress external perturbation sufficiently. The limit of combustion stability margin of engine is assumed to be 50 mm length baffle of the KSR-III engine.

Stability Rating of KSR-III Rocket Engine (KSR-III 로켓엔진의 연소 안정성 평가)

  • Sohn, Chae-Hoon;Kim, Young-Mog
    • Journal of the Korean Society for Aeronautical & Space Sciences
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    • v.32 no.3
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    • pp.95-101
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    • 2004
  • Stability rating of KSR-III rocket engine is conducted based on stability rating tests in the course of development of KSR-III rocket engine. Rocket engine is approved to have combustion stabilization ability when it can suppress the external perturbation or pressure oscillation with finite amplitude and recover the original stable combustion. Rocket engine in flight may be perturbed by unexpectedly large-amplitude pressure oscillation and thus a designer should not only assure combustion stabilization ability of the engine but also quantify the stabilization capacity. For this, principal quantitative parameters and their evaluation are introduced. To verify dynamic stability of KSR-III rocket engine, six stability rating tests have been conducted. Based on these test results, such parameters are quantified and thereby, the stabilization capacity of KSR-III rocket engine is evaluated.

The Realization of High Performance in a Hydrogen-Fueled Engine with External Mixture by Retarding Valve Timing and Super Charging (밸브 타이밍 지각과 과급에 의한 흡기관 분사식 수소기관의 고성능 실현)

  • Lee, Kwang-Ju;Hur, Sang-Hoon;Lee, Jong-Tae
    • Transactions of the Korean hydrogen and new energy society
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    • v.20 no.6
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    • pp.464-470
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    • 2009
  • In order to analysis the possibility of high expansion and performance without backfire in a hydrogenfueled engine using external mixture injection, combustion characteristics and performance enhancement were analyzed in terms of retarding valve timing and increasing the boosting pressure. As the results, it was found that thermal efficiency increased by retarding intake valve timing with the same level of supplied energy is over 6.6% by the effect of high expansion including effect of combustion enhancement due to supercharging. It was also shown that the achievement of high power (equal to that of a gasoline engine), low brake specific fuel consumption and low emission (NOx of less than 16 ppm) without backfire in a hydrogen-fueled engine is possible around a boosting pressure of 1.5 bar, intake valve opening time of TDC and $\Phi$=0.35 in fuel-air equivalence ratio.

연소 안정성 평가 시험을 통한 배플 길이의 안정성 여분 평가

  • Kim, Hong-Jip;Lee, Kwang-Jin;Seo, Seong-Hyeon;Kim, Seung-Han;Han, Yeoung-Min;Seol, Woo-Seok
    • Aerospace Engineering and Technology
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    • v.3 no.1
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    • pp.188-196
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    • 2004
  • To optimize and limit the axial length of baffle in KSR-III engine, stability rating tests using pulse gun as one of artificial disturbance devices have been done. Decay time and other parameters for the evaluation of stabilization ability of engine to external perturbation have been analyzed to quantify stabilization capacity of engine, in other words, dynamic stability margin. If baffle does not cover flame zone enough which can be considered as collision region of injector, it wasn't be able to suppress external perturbation sufficiently. The limit of combustion stability margin of engine is assumed to be 50 mm length baffle.

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Stability Rating of Liquid Propellant Rocket Engine (액체 로켓엔진의 연소 안정성 평가)

  • 손채훈;김영목
    • Proceedings of the Korean Society of Propulsion Engineers Conference
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    • 2003.10a
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    • pp.73-77
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    • 2003
  • Stability rating of KSR-III rocket engine is conducted based on stability rating tests in the course of development of KSR-III rocket engine. Rocket engine is approved to have combustion stabilization ability when it can suppress the external perturbation or pressure oscillation with finite amplitude and recover the original stable combustion. Rocket engine in flight nay be perturbed with unexpectedly large amplitude and thus a designer should not only assure combustion stabilization ability of the engine but also quantify the stabilization capacity. For this, several quantitative parameters and their evaluation are introduced. To verify dynamic stability of KSR-III rocket engine, five stability rating tests have been conducted. Based on these test results, such parameters are quantified and thereby, the stabilization capacity of KSR-III rocket engine is evaluated.

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Analysis of Journal Locus in a Connecting Rod Bearing (엔진 연결봉 베어링의 운동 궤적 해석)

  • 조명래;정진영;한동철
    • Proceedings of the Korean Society of Tribologists and Lubrication Engineers Conference
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    • 1997.04a
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    • pp.183-189
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    • 1997
  • This paper presents the motion of dynamically loaded journal in the connecting rod bearing of reciprocating internal combustion engine. Journal motions in engine bearings have been composed of two components, which was rotational and translational motion. Early study of journal locus in engine bearing had been performed on each motion. This paper has been considered two motions simultaneously. Reynolds equation including the squeeze effect has been analyzed using the ADI method, and real engine bearing and crankshaft system has been considered to calculate the cyclic external force. The equations of journal motion have been derived and then the numerical integration of these equations performed by 4th order Runge-Kutta method. This paper gives various journal orbits in connecting rod bearing depending on cyclic external forces, rotating speeds, and bearing parameters.

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Analysis of Journal Locus in a Connecting Rod Bearing (엔진 연결봉 베어링의 운동 궤적 해석)

  • 조명래;정진영;한동철
    • Transactions of the Korean Society of Automotive Engineers
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    • v.6 no.4
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    • pp.17-23
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    • 1998
  • This paper presents the motion of dynamically loaded journal in the connecting rod bearing of reciprocation internal combustion engine. Journal motions in engine bearings have been composed of two components, which was rotational and translational motion. Early study of journal locus in engine bearing had been performed on each motion. This paper has been considered two motions simultaneously. Reynolds equation including the squeeze effect has been analyzed using the ADI method, and real engine bearing and crankshaft system has been considered to calculate the cyclic external force. The equations are performed by 4th order Runge-Kutta method. This paper gives various journal orbits in connecting rod bearing depending on cyclic external forces, rotation speeds, and bearing parameters.

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Development of Sub-scale Combustor for a Liquid Rocket Engine Using Swirl Injector with External Mixing (외부혼합 와류분사기를 장착한 액체로켓엔진용 축소형 연소기 개발)

  • Han, Yeoung-Min;Kim, Seung-Han;Seo, Seong-Hyeon;Lee, Kwang-Jin;Kim, Jong-Gyu;Seol, Woo-Seok
    • Journal of the Korean Society for Aeronautical & Space Sciences
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    • v.32 no.10
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    • pp.102-111
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    • 2004
  • The procedure of design and manufacture of sub-scale combustor using bipropellant swirl injector with external mixing for a liquid rocket engine are described. The results of cold flow test, ignition test and combustion test of the sub-scale combustor are also given in this paper. The sub-scale combustor uses liquid oxygen(LOx) and kerosene as propellants and has a injector head, an ablative material combustor wall and a water cooled nozzle. The injector head has LOx manifold, fuel manifold, fire face plate, one center swirl injector and 18 main swirl injectors. The cold flow, ignition and combustion tests were successfully performed without damage of combustor. Results of hot firing tests show that combustion efficiency meets the target of design and operations of start and stop cyclogram are stable and high frequency combustion instability does not occur.

The Effect of T90 Temperature on Exhaust Emissions in Low-temperature Diesel Combustion (저온 디젤 연소에서 T90 온도가 배기가스에 미치는 영향)

  • Han, Man-Bae
    • Transactions of the Korean Society of Automotive Engineers
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    • v.19 no.4
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    • pp.72-77
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    • 2011
  • This study is to investigate the effect of the distillation temperature in ultra low sulfur diesel fuel on exhaust emissions in the low-temperature diesel combustion with 1.9L common rail direct injection diesel engine. Low temperature diesel combustion was achieved by adopting an external high EGR rate with a strategic injection control. The engine was operated at 1500 rpm 2.6 bar BMEP. The 90% distillation recovery temperature (T90) was $270^{\circ}C$ and $340^{\circ}C$ for the respective cetane number (CN) 30 and 55. It was found that there exists no distinctive discrepancy on exhaust emissions with regards to the different T90s. The high CN (CN55) fuels follow the similar trend of exhaust emissions as observed in CN30 fuels' except that high T90 fuel (CN55-T340) produced higher PM compared to low T90 fuel (CN55-T270). This may come from that high T90 plays an active role in aggravating the degree of fuel-air mixture preparedness before ignition.