• Title/Summary/Keyword: Exhaust Pipe

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Heat Recovery Characteristics of the Exhaust Heat Recovery System with Heat Pipe Unit Attached to the Hot Air Heater in the Greenhouse (히트파이프를 이용한 온풍난방기 배기열회수 시스템의 열회수 특성)

  • Kang, K. C.;Kim, Y. J.;Ryou, Y. S.;Baek, Y.;Rhee, K. J.
    • Journal of Biosystems Engineering
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    • v.26 no.5
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    • pp.441-448
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    • 2001
  • Hot air heater with light oil combustion is used as the most common heater for greenhouse heating in the winter season. However, exhaust gas heat discharged to atmosphere through chimney reaches up to 10~20% of total heat capacity of the oil burred. In order to recover the heat of this exhaust gas and to use for greenhouse heating, the heat pipe type exhaust heat recovery system was manufactured and tested in this experiment. The system consisted of a heat exchanger made of heat pipes, ø15.88${\times}$600mm located in the rectangular box of 675(L)${\times}$425(W)${\times}$370(H)mm, an air suction fan and air ducts. The number of heat pipe was 60, calculated considering the heat exchange amount between exhaust gas and air and heat transfer capacity of a heat pipe. The working fluid of heat pipe was acetone because acetone is known for its excellent heat transfer capacity. The system was attached to the exhaust gas path. According to the performance test it could recover 53,809 to 74,613kJ/h depending on the inlet air temperature of 12 to -12˚at air flow rate of 1.100㎥/h. The temperature of the exhaust gas left the heat exchanger dropped to 100$^{\circ}C$ from 270$^{\circ}C$ after the heat exchange between the suction air and the exhaust gas.

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An Experimental Study on the Characteristics of Back Pressure in Automotive Exhaust System (자동차 배기계의 배압특성에 관한 실험적연구)

  • Shin, D.Y.;Lee, J.S.;Kim, B.G.;Cha, K.O.
    • Proceedings of the KSME Conference
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    • 2000.11b
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    • pp.751-756
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    • 2000
  • Based on Experimental analysis, the characteristics of back pressure in automotive exhaust system is tested for 4-stroke gasoline engine. The back pressure in automotive exhaust system is generated by resistance working of exhaust system, i.e. exhaust manifold, pipe length, pipe banding, difference system pressure with atmospheric pressure. This paper contains experimental results which are tested for the change of exhaust pipe length and torque change are tested under experimental conditions.

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Pressure Predictions in Exhaust Pipe of a Single Cylinder Gasoline Engine (단기통 가솔린 기관의 배기단의 압력 예측)

  • Choi, S.C.;Lee, H.J.;Kim, S.H.;Koh, D.K.;Jeong, H.M.;Chung, H.S.
    • Journal of Power System Engineering
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    • v.8 no.1
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    • pp.24-29
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    • 2004
  • In this study, a computer analysis has been developed for predicting the pipe pressure of the intake and exhaust manifold. To obtain the boundary conditions for a numerical analysis, one dimensional and non-steady gas dynamic calculation is performed by using the MOC(Method Of Characteristic). The main numerical parameters are the variation of the engine revolution to calculate the pulsating flow which the intake and exhaust valves arc working. The comparison of exhaust pressure in case of numerical results is quite matched with in case of experimental results. When engine revaluation is increased, the pressure amplitude showed a high value, but the pressure frequency was decreased.

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A Study on the Fluid Dynamic of Catalytic Converter in Exhaust Pipe

  • Wangwenhai, Wangwenhai;Cho, Haeng Muk
    • Journal of Energy Engineering
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    • v.23 no.2
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    • pp.114-118
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    • 2014
  • The need to maximize the exhaust pipe inside surface and to minimize exhaust resistance And Find the best point between the exhaust and the duration of contact between the two surfaces. Exhaust gas mass flow On the whole cross section of catalytic converters more uniform distribution will contribute to its usability. Based on the flow rate of fluid traces given color, Exhaust fluid resistance in the porous catalyst can be estimated, from the efficiency of the catalytic converter that is very important.

Shape Design of Construction Equipment Tailpipe for Noise Reduction and Engine Room Cooling (소음 및 엔진룸 냉각개선을 위한 건설기계테일파이프의 형상설계)

  • Kim, Seong-Jae;Yang, Ji-Hae;Kim, Nag-In;Kim, Jou-Sik
    • Proceedings of the Korean Society for Noise and Vibration Engineering Conference
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    • 2004.11a
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    • pp.737-740
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    • 2004
  • The interior noise reduction of construction equipment is concerned for improving the driver comfort in this study. From the baseline test, the exhaust noise gives a big contribution to the interior noise of construction equipment. And the detail noise contribution analysis of the exhaust system, the tail pipe, which is for ventilation an engine room hot air to outside, amplify the exhaust noise around operating engine RPM associated with tail pipe structural and cavity resonances. To remove the noise amplifying effects, the tail pipe has to be shorted its length. Even the noise can be attenuated the ventilation flux when using the redesigned tail pipe is reduced than the original one. Thus, a shape change of the tail pipe is additionally needed for increasing the ventilation flux and attenuating the exhaust noise using CFD technique. The CFD results of the tail pipe give a meaning full information what obstructs the ventilation flex in the current design and how changes the tail pipe.

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A Basic Study on the Utilization of Kitchen and Bathroom Exhaust Wind Velocity in High-Rise Apartment (초고층 공동주택의 주방.욕실 배기풍속 활용을 위한 기초연구)

  • Kim, Seong-Yong;Lee, Yong-Ho;Park, Jin-Chul;Hwang, Jung-Ha
    • 한국태양에너지학회:학술대회논문집
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    • 2011.11a
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    • pp.226-231
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    • 2011
  • This study set out to review the air current fluidity in exhaust common ducts by installing an inlet pipe at a leisure space in the PS(Pipe Shaft)room for the sake of wind power generation with kitchen and bathroom exhaust common ducts of all the equipment and air conditioning shafts in high-rise apartment. The air current functionality of kitchen and bathroom exhaust common ducts was reviewed by analyzing wind velocity changes according to changes to the area of exhaust common ducts through a simulation, changes to the wind velocity of the kitchen hood by applying an external inlet pipe, changes to the usage factor of exhaust common ducts, and changes to wind velocity by altering the form of the ventilator at the bottom of the old exhaust common duct. It was a basic study on the utilization of exhaust wind velocity in exhaust common ducts.

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HEAT PIPE TYPE EXHAUST HEAT RECOVERY SYSTEM FOR HOT AIR HEATER

  • Kang, G.C.;Kim, Y.J.;Ryou, Y.S.;Rhee, K.J.
    • Proceedings of the Korean Society for Agricultural Machinery Conference
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    • 2000.11c
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    • pp.654-661
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    • 2000
  • Area of greenhouse increases rapidly up to 45,265ha by the year of 1998 in Korea. Hot air heater with light oil combustion is the most common heater for greenhouse heating in the winter season. However, exhaust gas heat discharged to atmosphere through chimney reaches up to 10~20% of total heat of the oil combusted in the furnace. In order to recapture the heat of this exhaust gas and to recycle for greenhouse heating, the heat pipe type exhaust heat recovery system was manufactured and tested in this experiment. The exhaust heat recovery system was made for space heating in the greenhouse. The system consisted of a heat exchanger made of heat pipes, ${\emptyset}15.88{\times}600mm$ located in the rectangular box of $600{\times}550{\times}330mm$, a blower and air ducts. The rectangular box was divided by two compartments where hot chamber exposed to exhaust gas in which heat pipes could pick up the heat of exhaust gas, and by evaporation of the heat transfer medium in the pipes it carries the heat to the cold compartment, then the blower moves the heat to greenhouse. The number of heat pipe was 60, calculated considering the heat exchange amount between flue gas and heat transfer capacity of heat pipe. The working fluid of heat pipe was acetone because acetone is known for its excellent heat transfer capacity. The system was attached to the exhaust gas path. According to the performance test it could recover 53,809 to 74,613kJ/hr depending on the inlet air temperature of 12 to $-12^{circ}C$ respectively when air flow rate $1,100\textrm{m}^3/hr$. The exhaust gas temperature left the heat exchanger dropped to $100^{circ}C$ from $270^{circ}C$ by the heat exchange between the air and the flue gas, the temperature difference was collected by the air and the warm air temperature was about $60^{circ}C$ at the air flow rate of $1,100\textrm{m}^3/hr$. This heat pipe type exhaust heat recovery system can reduce fuel cost by 10% annually according to the economic analysis.

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Analysis on the Interactions of Harmonics in Exhaust Pipes of Automotive Engines

  • Lee, Min-Ho;Lee, Joon-Seo;Cha, Kyung-Ok
    • Journal of Mechanical Science and Technology
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    • v.17 no.12
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    • pp.1867-1875
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    • 2003
  • In exhaust pipes of automotive engines, the pulsating pressure waves are composed of fundamental frequency and high order harmonics. The nonlinearities in the exhaust pipe is caused by their interactions. The error between prediction and measurement is induced by the nonlinearities. We can not explain this phenomenon using linear acoustics theory. So power spectrum, which is used in linear theory, is not useful. This paper is concerned with the development of useful engineering techniques to detect and analyze nonlinearity in exhaust pipe of automotive engines. The study of higher order statistics has been dominated by work on the bispectrum. The bispectrum can be viewed as a decomposition of the third moment (skewness) of a signal over frequency and as such is blind to symmetric nonlinearities. The phenomenon of quadratic phase coupling (QPC) can be analyzed by the bicoherence function. Finally the application of these techniques to data from actual exhaust pipe systems is performed.

Cabin Noise Reduction of wheel Loader through the Shape Optimization of Tail-Pipe (테일 파이프 형상 개선을 통한 휠로더 캐빈 소음 저감 연구)

  • Ko, Kyung-Eun;Joo, Won-Ho;Kim, Dong-Hae;Bae, Jong-Gug
    • Proceedings of the Korean Society for Noise and Vibration Engineering Conference
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    • 2006.11a
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    • pp.686-689
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    • 2006
  • In a wheel loader, the tail-pipe is installed at the exhaust tube of muffler for the reduction of exhaust noise and the cooling of engine room however, the cabin noise level can be largely increased due to the tail-pipe. In this paper, to grasp and reduce the cabin noise, a series of noise and vibration tests were carried out in addition to numerical simulations. As a result, the transmission path of exhaust noise toward the cabin was exactly identified and the improved shape of tail pipe, that can reduce the cabin noise, was derived through various numerical simulations and real tests.

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Cabin Noise Reduction of Wheel Loader through the Shape Optimization of Tail-Pipe (테일 파이프 형상 개선을 통한 휠로더 캐빈 소음 저감 연구)

  • Ko, Kyung-Eun;Joo, Won-Ho;Kim, Dong-Hae;Bae, Jong-Gug
    • Transactions of the Korean Society for Noise and Vibration Engineering
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    • v.16 no.12 s.117
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    • pp.1238-1243
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    • 2006
  • In a wheel loader, the tail-pipe is installed at the exhaust tube of muffler for the reduction of exhaust noise and the cooling of engine room, however, the cabin noise level can be largely increased due to the tail-pipe. In this paper, to grasp and reduce the cabin noise, a series of noise and vibration tests were carried out in addition to numerical simulations. As a result, the transmission path of exhaust noise toward the cabin was exactly identified and the improved shape of tail pipe, that can reduce the cabin noise, was derived through various numerical simulations and real tests.