• Title/Summary/Keyword: Effluent rate

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A Study on the Growth Characteristics of Commercially Developed Nitrifying Bacteria and its Application to Activated Sludge Process (상업용 질산화 박테리아의 성장특성과 활성슬러지 공정에서의 적용 방법에 따른 연구)

  • Whang, Gyu-Dae;Lee, Bong-Hee
    • Journal of Korean Society of Water and Wastewater
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    • v.20 no.4
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    • pp.595-604
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    • 2006
  • The growth characteristics of Commercially Developed Nitrifying Bacteria (CDNB) were studied in laboratoryscale. CDNB, a pure, artificially isolated bacterium, was cultivated to produce Cultivated Nitrifying Bacterium Group (CNBG). The average ammonia removal rate of CDNB was 0.0234g $NH_4^+-N/g$ MLSS/hr. CNBG was produced in the batch reactor and Specific Nitrification Rate (SNR) was determined at 0.0107g $NH_4^+-N/g$ MLSS/hr. The SNR of CNBG was lower than the SNR of CDNB because the diverse and multi-cultured microbial growth took place during cultivation. The effect of the temperatures and the mixing ratios of sewage and culture solution on the SNR of CNBG was studied. The SNR of CNBG, 0.0107g $NH_4^+-N/g$ MLSS/hr at $27^{\circ}C$, decreased to 0.0048g $NH_4^+-N/g$ MLSS/hr at $15^{\circ}C$, and temperature coefficient (${\Theta}$) was calculated to be 1.07. With the varied sewage mixing ratios, the SNR of CNBG remained unchanged. Activated sludge reactors maintaining an MLSS of 2,000mg/L at HRT of 4 h were operated under conditions in which dosage of Concentrated CNBG Solution (CCNBGS, 10,000mg MLSS/L) and application method of CNBG were varied. The reactor with 20mL of CCNBGS took shorter time to oxidize $NH_4^+-N$ reaching 1mg/L than the reactor with 5mL of CCNBGS showing that higher dosages were associated with greater mass removal of $NH_4^+-N$. However, the total removal was not great. In terms of different methods of CNBG application, reactor seeded with 20mL of CCNBGS took 3days to reach 1mg/L of effluent ammonia concentration while reactor dosed with 20% (v/v) CNBG implanted media took 2days. Both the control reactor and the reactor dosed with 20% (v/v) media only did not reach 1mg $NH_4^+-N/L$ after operating 18days. The reactor with CNBG implanted media had the highest $NH_4^+-N$ removal rate because of maintaining high concentration of Nitrifying Oxidizing Bacteria (NOM), and is regarded as an appropriate method for the activated sludge process.

A Study on Clogging and Water Quality Improvement in Floodplain Filtration with Flood/rest Raw-water Supply (범람/휴지식 홍수터여과에서 폐색현상 및 수질개선도 연구)

  • Kim, Hoh-Seok;Kim, Seung-Hyun
    • Journal of Korean Society of Environmental Engineers
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    • v.33 no.2
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    • pp.120-131
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    • 2011
  • A pilot-scale experiment of floodplain filtration with a filtration depth of 3.6m was performed employing flood/rest type raw-water supply system in an effort to find ways to improve river water quality by additional treatments of discharged effluent from sewage treatment plant. Soil samples were taken from 3 sites including Gumi, Daegu and Gimhae along the Nakdong river. Reductions of infiltration rates following increases in operating time was investigated in each soil sample, along with the analysis of removal efficiencies of various pollutants according to different depths and infiltration rates. The results show incremental development of clogging on the soil surface with increases in operation time, and illustrate exponential decrease in the infiltration rate. The time required for the removal of the clog from the soil surface was longer than 2 weeks for all soil samples analyzed. The stable infiltration rates for soils were 5 m/day for Gumi and for Daegu and Gimhae was 1 m/day. In unsaturated soils dissolved oxygen levels increased following the increase of filtration depth, suggesting that alternating application of flood and rest for raw-water supply effectively keeps the soil environment aerobic. For all soils, the nature of pollutant removal depending on the depth of filtration remained the same regardless of the infiltration rate. Most of the BOD and turbidity were removed within 1.2 m, about 30% of COD was removed within 3.6m and was expected to be removed further with increases in filtration depth. Nitrification occurred near the surface of all soils; however there was no significant removal of nitrogen in the filtration depths tested in this study. Although removal rate of phosphorus was low for Gumi's soil, it was high enough for other soils, suggesting that the method developed in this study could significantly improve river water quality.

Effect of Microbubble Ozonation Process on Performance of Biological Reactor System for Excess Sludge Solubilisation (마이크로버블오존을 이용한 잉여슬러지 가용화 처리가 생물반응조의 성능에 미치는 영향)

  • Lee, Shun-Hwa;Jung, Kye-Ju;Kwon, Jin-Ha;Lee, Se-Han
    • Journal of Korean Society of Environmental Engineers
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    • v.33 no.2
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    • pp.113-119
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    • 2011
  • The study purpose was to examine an effect of zero emission of excess sludge on biological reactor and treated water quality within the biological reactor in the process of biological treatment combined with excess sludge reduction system with ozone. Under an ozone injection rate 0.03 g $O_3/g$ SS, Sludge Disintegration Number (SDN) 3 and less than pH 4 as pre-treatment process, it was possible to maintain a stable biological treatment process without sludge disintegration. In the test of $OUR_{max}$, of sludge, its value was hardly under the condition of ozone injection rate 0.03 g $O_3/g$ SS. There were almost no changes of MLVSS/MLSS within biological reactor followed by a solubilization of excess sludge. Accumulation of microorganism within biological reactor was also not observed. After solubilization of excess sludge, an increase for organic matter and SS concentrations of an effluent was not observed and T-N concentration was reduced by increasing nitrification and denitrification rate within biological reactor. Most of T-P was not removed by zero emission of excess sludge and was leaked by being included in effluents.

Characteristics of Microbial Distribution of Nitrifiers and Nitrogen Removal in Membrane Bioreactor by Fluorescence in situ Hybridization (막/생물반응기에서 Fluorescence in situ Hybridization 기법을 이용한 질산화 미생물 분포특성 및 질소제거 연구)

  • Lim Kyoung-Jo;Kim Sun-Hee;Kim Dong-Jin;Cha Gi-Cheol;Yoo Ik-Keun
    • Microbiology and Biotechnology Letters
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    • v.34 no.3
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    • pp.257-264
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    • 2006
  • An aerobic submerged membrane bioreactor (MBR) treating ammonium wastewater was studied in respect of nitrification characteristics and distribution of nitrification bacteria over a period of 350 days. MBR was fed with ammonium concentration of 500-1000 mg $NH_4-N/L$ at a nitrogen load of $1-2kg\;N/m^3{\cdot}d$. Overall ammonium oxidation rate increased with dissolved oxygen (DO) concentration, temperature, and sludge retention time (SRT). Under a higher concentration of free ammonia ($NH_3-N$) due to the decrease of ammonium oxidation rate, the nitrite ratio ($NO_2-N/NO_x-N$) in the effluent increased. The sudden collapse of nitrification efficiency accompanied by sludge foaming and the increase of sludge volume index (SVI) was observed unexpectedly during the operation. At the later stage of operation, additional carbon source was fed to the MBR and resulted in twice higher value of SVI and the decrease of ammonium oxidation rate. In fluorescence in situ hybridization (FISH) analysis, genus Nitrosomonas which is specifically hybridized with probe NSM156 was initially the dominant ammonia oxidizing bacteria and the amount of Nitrosospira gradually increased. Nitrospira was the dominant nitrite oxidizing bacteria during whole operational period. Significant amount of Nitrobacter was also detected which might due to the high concentration of nitrite maintained in the reactor.

Investigation of the High Temperature Shift for a Generation of High Purity Hydrogen (고순도 수소생산을 위한 고온전이 반응 연구)

  • Lim, Mun Sup;Chun, Young Nam
    • Applied Chemistry for Engineering
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    • v.19 no.2
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    • pp.157-160
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    • 2008
  • The generation of high-purity hydrogen from hydrocarbon fuels is essential for efficient operation of fuel cell. In general, most feasible strategies to generate hydrogen from hydrocarbon fuels consist of a reforming step to generate a mixture of $H_2$, CO, $CO_2$ and $H_2O$ (steam) followed by water gas shift (WGS) and CO clean-up steps. The WGS reaction that shifts CO to $CO_2$ and simultaneously produces another mole of $H_2$ was carried out in a two-stage catalytic conversion process involving a high temperature shift (HTS) and a low temperature shift (LTS). In a typical operation, gas emerges from the reformer is taken through a high temperature shift catalyst to reduce the CO concentration to about 3~5%. The HTS reactor was designed and tested in this study to produce hydrogen-rich gas with CO to a range of 2~4%. The iron based catalysts (G-3C) was used for the HTS to convert the most of CO in the effluent from the partial oxidation (POX) to $H_2$ and $CO_2$ at a relatively high rate. Parametric screening studies were carried out for variations of the following variables: reaction temperature, steam flow rate, components ratio ($H_2/CO$), and reforming gas flow rate.

Effect of the Addition of Granular Activated Carbon and Granular Sludge on the Performance of Upflow Anaerobic Sludge Blanket Reactors for Treating Leachate (상향류 혐기성 슬러지 블랭킷 반응조를 이용한 침출수 처리시 입상 활성탄 및 입상슬러지 첨가의 영향)

  • Lee, Chae-Young
    • Journal of the Korea Organic Resources Recycling Association
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    • v.16 no.4
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    • pp.91-97
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    • 2008
  • The objective of this research is to investigate the effect of the addition of granular activated carbon (GAC) and granular sludge on the performance of upflow anaerobic sludge blanket (UASB) reactors for treating leachate. For the control reactor, sludge obtained from an anaerobic digester was used as a seed material. On the other hand, GAC and granular sludge were incorporated with the seed sludge in the GAC reactor and the Granule reactor, respectively. The shortest acclimation period was observed in the Granule reactor. The GAC reactor also gave comparable performance to the Granule reactor at the beginning of operation. However, as the adsorptive capacity of GAC was exhausted, the effluent COD concentration increased gradually. Once the systems were stabilized, the GAC reactor showed slightly better results than the other two reactors in terms of chemical oxygen demand (COD) removal. COD removal in all reactors was more than 90% at hydraulic retention time of 1.0 day. Furthermore, GAC reactor showed little variation in COD removal rate and remained at 95% with organic loading rate (OLR) of 4.0 to $8.2kg\;COD/m^3.d$. Initial operating period was reduced by the addition of granular sludge, while the treatment efficiency was enhanced by the addition of GAC.

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Recycled packed-bed reactor for efficient denitrification (재순환 충전탑식 반응기를 이용한 효율적 탈질)

  • 김성홍;송승훈;박재연;유영제
    • KSBB Journal
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    • v.19 no.2
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    • pp.154-158
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    • 2004
  • Recycled packed-bed reactor emploring immobilized microorganism was suggested in this paper for efficient denitrification. In the batch reactor, the effects of initial oxidation-reduction potential and nitrate concentration on denitrification were investigated. As the initial oxidation-reduction potential was decresed to -70 mV from +40 mV, the removal rate of nitrate was increased to 3.33 from 1.25 m9 NO$_3$$\^$-/-N/min under the experimental conditions. As the initial nitrate-N concentraion was increased to 200 mg/l, the removal rate of nitrate was proportional to the concentration of nitrate. When the concentration of nitrate-N was 400 mg/min, nitrite was detected, and when the initial nitrate-N concentration was reached at 1,000 mg/l, it took longer time for the complete nitrate removal. In order to decrease the initial oxidation-reduction potential and the nitrate-N concentration in the feed stream, the effluent was recycled to the influent stream in the packed-bed reactor. In the case of recycling, the initial oxidation-reduction potential was decreased to 30 mV from 150 mV, and the initial nitrate concentration could be decreased to 85 from 120 mg NO$_3$$\^$-/-N/l. As the result of recycling, the removal rate of nitrate was increased to 91.7% from 49.2%.

Estimation of Pollution Loads flowing into Mokpo Harbour - Centering on Pollution Loads from Land in Dry Case - (목포항에 유입하는 오염부하량 산정 - 비강우시 육상오염부하를 중심으로 -)

  • Kim Kwang-Soo;Lee Nam-Il
    • Journal of the Korean Society for Marine Environment & Energy
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    • v.6 no.1
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    • pp.11-20
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    • 2003
  • The pollution loads flowing into Mokpo harbour from land in dry case were estimated on the bases of the seasonal flow rates and the seasonal water qualities of streams and effluents located around Mokpo harbour. Average daily amount of fresh water Stowing into Mokpo harbour obtained by the inflow rate data of 4 seasons was found to be about 5.5×10/sup 6/㎥/day and annual inflow rate to be about 2×10/sup 9/㎥/year. The seasonal flow rates of effluents iron Yongsan lake were above 90% of total flow rates of all inflows in 4 seasons. The concentrations of COD, TSS, TIN and TP at 9 inflow stations Iron streams and effluents in 4 seasons were shown to be in the ranges of 2.87~42.69㎎/ℓ, 3.65~1080.32㎎/ℓ, 0.083~89.744㎎/ℓ and 0.028~6.926㎎/ℓ, respectively. The average loads of COD, TSS, TIN and TP into Mokpo harbour estimated by the data of 4 seasons were found to be about 37 ton/day, 64 ton/day, 13 ton/day and 1.2 ton/day, respectively. The loads of COD, TSS, TIN and TP into Mokpo harbour in summer were shown to be about 82 ton/day, 159 ton/day, 14 ton/day and 2 ton/day, respectively. The main source of pollution loads into Mokpo harbour was found to be the effluent of Yongsan lake.

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Analysis study on substances subject to management using long-term water quality monitoring data in tributaries of the Nakdong River basin (낙동강유역 지류에서의 장기 수질모니터링 자료를 이용한 관리 대상물질 분석 연구)

  • Byungseok Kal;Jaebeom Park;Seongmin Kim;Sangmin Shin;Soonja Jang;Minjae Jeon;Donghyun Lee
    • Journal of Wetlands Research
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    • v.25 no.4
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    • pp.326-334
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    • 2023
  • The purpose of this study is to use long-term water quality monitoring data from tributaries of the Nakdong River system to identify problematic substances in tributaries by examining the rate of exceedance and increase in water quality targets. In the Nakdong River system, monitoring is conducted once a month for 38 tributaries that require intensive management, and this data was used to analyze trends in exceeding and increasing target water quality at each point. The analysis items are eight items that can be evaluated based on river water quality standards: DO, BOD, COD, TOC, SS, total phosphorus, fecal coliform, and total coliform. As a result of the analysis, the target water quality exceedance rate was more than 50%, and the items with an increasing trend were TOC, fecal coliform and total E. coli counts, and the items with an exceedance rate of less than 50% but an increasing trend were SS. TOC is believed to be caused by an increase in non-degradable substances, and the continued increase in Total Coliform will require management of Total ColiformTotal Coliform in effluent water from sewage treatment facilities in the future.

Ensuring Stability in Accordance with the Secondary sedimentation tank Surface Loading rate Increase (장방향 이차침전지에서 이중정류벽 설치를 통한 침강속도 증대에 따른안정성 확보 분석)

  • Choi, Dongkyu;Im, Jiyeol;Gil, Kyungik
    • Journal of Wetlands Research
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    • v.18 no.4
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    • pp.357-362
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    • 2016
  • Improvement of the solid-liquid separation efficiency in the secondary sedimentation tank of the biological treatment process, is known to be increasing effectiveness of the overall system operation. Sewage treatment plant effluent SS is composed of most organic substances. In order to reduce the SS component in the secondary sedimentation tank discharge, fine SS components constituting the heterogeneous should be increased by its own aggregation (self flocculation), so that can be deleted through their precipitation. So, it is improved through using the installation of double rectification wall in this secondary tank. In case, sewage is rapidly increased due to the daily change of the influent water, it was confirmed that suspended solids caused by the impact load are processed stably. Therefore, there is a need for a facility installation which can be its own aggregation for reduction suspended solids in secondary sedimentation tank.