• Title/Summary/Keyword: Conventional circular duct

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Numerical and experimental investigation of conventional and un-conventional preswirl duct for VLCC

  • Shin, Hyun-Joon;Lee, Jong-Seung;Lee, Kang-Hoon;Han, Myung-Ryun;Hur, Eui-Beom;Shin, Sung-Chul
    • International Journal of Naval Architecture and Ocean Engineering
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    • v.5 no.3
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    • pp.414-430
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    • 2013
  • This paper shows the study of preswirl duct as an effective energy saving devices that have been devised and reviewed to support the propeller performance, especially for the ship of VLCC with large block coefficients. From the bare hull wake measurements, typical upper/lower asymmetry of hull wake at the propeller disk was found. The 2 kinds of pre-swirl duct, Unconventional half circular duct and Conventional circular pre-swirl duct have been designed and reviewed to recover the loss of propeller running in that condition. The general function of the pre-swirl duct was set to work against this asymmetry of wake and generate pre-swirled flow into the propeller against the propeller rotating direction. The optimum self propulsion tests with various angle configurations were carried out and the best configuration was decided. Accordingly, cavitation test was carried out with best configuration of unconventional half circular duct. The blade surface and tip vortex cavitation behaved smoother when the duct was mounted. The hull pressure amplitudes reflected this difference, so the hull pressure amplitude with duct was smaller than that of without duct.

Active Noise Control in a Circular Duct Using Smart Foam (원형 덕트 내에서 스마트 폼을 이용한 능동 소음 제어)

  • Han, Je-Heon;Kim, Pyo-Jae;Kang, Yeon-June
    • Proceedings of the KSME Conference
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    • 2001.06b
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    • pp.641-645
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    • 2001
  • In this paper, it is discussed that active noise control in a circular duct using smart foam. Firstly, it is demonstrated that the potential of the conventional smart foam, proposed by Fuller, for active noise control in a duct. Conventional smart foam is not applicable to active noise control in a duct having flow. Thus, this paper presents a ring-type smart foam as an alternative. The ring-type smart foam consists of polyurethane acoustic foam of lining shape and PVDF film embedded in the foam. The embedded PVDF element acts as an actuator to reduce noise at lower frequencies and the foam absorbs noise at higher frequencies. A filtered-x LMS controller is used to minimize the signal from the error microphone. Experiments are executed to reduce broadband and tonal noise.

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Heat transfer characteristics around a circular combustion chamber of kerosene fan heater (석유 팬 히터의 연소실 주변 열전달 특성)

  • Kim, Jang-Gwon
    • Transactions of the Korean Society of Mechanical Engineers B
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    • v.22 no.4
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    • pp.551-561
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    • 1998
  • This paper was studied to understand the characteristics of heat transfer coefficients and surface temperature distributions around a circular combustion chamber within the heat-intercept duct of kerosene fan heater. The experiment was carried out in the heat-intercept duct of kerosene fan heater attached to the blow-down-type subsonic wind tunnel with a test section of 240 mm * 240 mm * 1200 mm. The purpose of this paper was to obtain the basic data related with normal combustion for new design from conventional kerosene fan heater, and to investigate the effect of surface temperature, local and mean heat transfer coefficients versus flow-rate of convection axial fan according to the variations of heat release conditions from kerosene fan heater during normal combustion. Consequently it was found that (i) the revolution of convection axial fan during combustion had a smaller value than that of non-combustion because of the thermal resistance due to the high temperature in the heat-intercept duct, (ii) the pressure ratio P$_{2}$/P$_{1}$ had a comparatively constant value of 0.844 according to the revolution increase of turbo fan and the heating performance of kerosene fan heater had a range of 1,494 ~ 3,852 kcal/hr, (iii) the local heat transfer coefficient around a circular combustion chamber had a comparatively larger scale in the range of 315 deg. < .theta. < 45 deg. than that in the range of 90 deg. < .theta. < 270 deg. as a result of heat transfer difference between front and back of a circular combustion chamber, and (iv) the mean heat transfer coefficient around a circular combustion chamber increased linearly like a H$_{m}$=95.196Q+104.019 in condition of high heat release according to the increase of flow-rate of axial fan.n.

Effects of Ventilation Systems on Interior Environment of the Growing-finishing Pig House in Korea (육성$\cdot$비육돈사 내에서 환기형태별 환경조사 연구)

  • Song J. I.;Yoo Y. H.;Jeong J. W.;Kim T. I.;Choi H. C.;Kang H. S.;Yang C. B.;Lee Y. Y.
    • Journal of Animal Environmental Science
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    • v.10 no.2
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    • pp.93-100
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    • 2004
  • An experiment was conducted to establish comparison of ventilation efficiency in an enclosed and conventional growing-finishing pig house. The experimental pigs were in winter and summer. The main results of the experiment are as follows : Then the air from planar slot inlet the pig house flow out through the sidewall outlet operated by exhaust fan(Gl). The second structure has an air input through the circular duct inlet are plated side the juncture of the entering wall and the air into the pig house flow out through the chimney and pit outlet are operated by exhaust fan(G2). Through the air into relay fan the pig house flow out through the curtains in sidewall(G3). Similarly, air comes in through the circular duct inlet are placed the air into the pig house flow out through the curtains in sidewall (G4). Air flow rate on the floor level which is the low part of pen and the living area of pigs in the G2 and G4 system during winter was measured at 0.2 to 0.3 m/s at the 0.5 to 0.6 m/s at the maximum ventilation efficiency. As for the results of detrimental gas(ammonia) concentration ratio analysis, while G2 and G4 system sustained of summer 13.3 $\~$ 16.6 ppm, winter 14.0 $\~$ 14.6 ppm level, Gl and G3 system sustained of summer 14.6 $\~$ 20.3 ppm, winter 20.3 $\~$ 25.0 ppm, and the latter one is lower than that of the G1 and G3 system.

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