• Title/Summary/Keyword: Combustion Liner

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Predictions of the deteriorating performance for the marine diesel engines (선박용 디젤기관의 열화성능 예측에 관한 연구)

  • Jung, Chan-Ho;Rho, Beom-Seuk;Lee, Ji-Woong;Choi, Jae-Sung
    • Journal of Advanced Marine Engineering and Technology
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    • v.37 no.1
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    • pp.47-52
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    • 2013
  • The higher energy efficiency for ship and the lower pollution for global environment are required strictly. However the performance of marine diesel engine is gradually deteriorated with time. And also the operation condition is varied with sea conditions. Hence the optimization for operating condition of marine engines is needed for energy saving and environment kindly. In this paper, it was attempted to investigate the influence of aging for marine diesel engine. The deterioration of engine performance is assessed by the calculation results of the simulation program for two-stroke marine diesel engine developed by author which was reported before. And three parameters for deterioration of engine performance were considered such as lower efficiency of turbocharger by fouling, increase of blow-by gas due to wear of cylinder liner and getting worse of combustion by poor injection. By the results, it was shown that the influence of engine performance by aging was relatively not so small - 10.4 bar low in Pmax and 3.2% decrease in Pmi.

Experimental Study on Firing Test of LPI Engine Using Gasoline Fuel for Improving the Production Process at End of line (엔진 착화 라인의 생산성 향상을 위한 LPI 엔진 가솔린 연료 적용성에 대한 실험적 연구)

  • Hwang, In-Goo;Choi, Seong-Won;Myung, Cha-Lee;Park, Sim-Soo;Lee, Jong-Soo
    • Transactions of the Korean Society of Automotive Engineers
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    • v.15 no.3
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    • pp.133-140
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    • 2007
  • The purpose of this study was to evaluate the effects of gasoline fuel to the LPI engine. Firing test bench was used in order to assess the effect on gasoline-injected LPI engine. Gasoline fuel was supplied into the reverse direction(3-4-2-1 cylinder) at 3.0 bar with commercial gasoline fuel pump. Engine test was performed using the firing test mode at end of line. The deviations of excess air ratio of each cylinder and maximum combustion pressure using gasoline fuel were within 0.1 and $1{\sim}2\;bar$. Engine start time was measured with changing coolant temperature at $20^{\circ}C,\;40^{\circ}C,\;80^{\circ}C$, respectively. Residual gasoline volume in the fuel line was measured about 32 cc after firing test and it was less than 2 cc within 10 seconds purging. To simulate the end of line, the residual gasoline in the fuel line was purged during 5 and 10 seconds. Start time of LPI engine with LPG fuel were 0.61 and 0.58 seconds. This work showed that severe problems such as misfiring and liner scuffing were not occurred applying gasoline fuel to LPI engine.

Development of 2-ton thrust-level sub-scale calorimeter (추력 2톤급 축소형 칼로리미터 개발)

  • Cho, Won-Kook;Ryu, Chul-Sung;Chung, Yong-Hyun;Lee, Kwang-Jin;Kim, Seung-Han;Lee, Soo-Yong
    • Journal of the Korean Society for Aeronautical & Space Sciences
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    • v.33 no.3
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    • pp.107-113
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    • 2005
  • A calorimeter of 2-ton thrust level rocket engine chamber has been developed to measure the wall heat flux. The liner of the chamber is made of copper-chromium alloy to maximize the heat transfer performance and structural strength. 1-D design code based on empirical correlations has been used for the prediction of the global thermal characteristics while 3-D CFD has been applied for the verification of local cooling performance. The predicted average wall heat flux at the throat is 43 $MW/m^{2}$ for the combustion chamber pressure of 53 bar. The chamber structure is confirmed to be safe at the pressure of 150 bar through 2-D stress analysis and measurement of the strain of the test species. Finally, the test of pressurizing the calorimeter chamber has been performed with water at the pressure of 150 bar in room temperature environment. No thermal damage has been detected after the hot-fire test in the test nozzle of same cooling performance with the developed calorimeter though the measured throat heat flux is higher than the design value by 10%.

Analysis of Boundary Layer in Solid Rocket Nozzle and Numerical Analysis of Thermal Response of Carbon/Phenolic using Finite Difference Method (고체 로켓 노즐의 경계층 해석과 유한차분법을 이용한 탄소/페놀릭의 열반응 해석 연구)

  • Seo, Sang Kyu;Hahm, Hee Cheol;Kang, Yoon Goo
    • Journal of the Korean Society of Propulsion Engineers
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    • v.22 no.1
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    • pp.36-44
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    • 2018
  • The thermal response of carbon/phenolic used in a solid rocket nozzle liner was analyzed. In this paper, the numerical analysis of the thermal response of carbon/phenolic consists of (1) the integration equation of the boundary layer to obtain the convective heat transfer coefficient of the combustion gas on the rocket nozzle wall and (2) 1-D finite difference method for heat conduction of carbon/phenolic to calculate the ablation, char, and temperature. The calculated result was compared with the result of a blast-tube-type test motor. It is found that the calculated result shows good agreement with the thermal response of the test motor, except at the vicinity of the throat insert.

Analysis of cause of engine failure during power generation using biogas in sewage treatment plant (하수처리장 바이오가스를 이용한 발전시 가스엔진의 고장원인 분석)

  • Kim, Gill Jung;Kim, Lae Hyun
    • Journal of Energy Engineering
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    • v.25 no.4
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    • pp.13-29
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    • 2016
  • In this study, we analyzed the causes of major faults in the biogas plant through the case of gas engine failure when cogenerating electricity and heat using biogas as a fuel in the actual sewage treatment plant and suggested countermeasures. Hydrogen sulfide in the biogas entering the biogas engine and water caused by intermittent malfunction of the water removal system caused intercooler corrosion in the biogas engine. In addition, the siloxane in the biogas forms a silicate compound with silicon dioxide, which causes scratches and wear of the piston surface and the inner wall of the cylinder liner. The substances attached to the combustion chamber and the exhaust system were analyzed to be combined with hydrogen sulfide and other impurities. It is believed that hydrogen sulfide was supplied to the desulfurization plant for a long period of time because of the high content of hydrogen sulfide (more than 50ppm) in the biogas and the hydrogen sulfide was introduced into the engine due to the decrease of the removal efficiency due to the breakthrough point of the activated carbon in the desulfurization plant. In addition, the hydrogen sulfide degrades the function of the activated carbon for siloxane removal of the adsorption column, which is considered to be caused by the introduction of unremoved siloxane waste into the engine, resulting in various types of engine failure. Therefore, hydrogen sulfide, siloxane, and water can be regarded as the main causes of the failure of the biogas engine. Among them, hydrogen sulfide reacts with other materials causing failure and can be regarded as a substance having a great influence on the pretreatment process. As a result, optimization of $H_2S$ removal method seems to be an essential measure for stable operation of the biogas engine.

Air Fuel Ratio Determination Method for Alternative Fuel Based on Carbon Balance and Linear Equation (탄소 균형과 1차식에 의한 대체 연료의 공연비 산정법)

  • Lee, Jae-Won;Kwon, Soon-Tae;Park, Chan-Jun;Ohm, In-Young
    • Journal of Energy Engineering
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    • v.17 no.4
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    • pp.182-188
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    • 2008
  • This paper is to compare the carbon-balanced and liner air-fuel ratio determination methods for alternative fuels. In the previous work, expansion of Eltinge chart, unburned hydrocarbon compensation, comparison of the results from various methods were discussed. It has been also concluded that Eltinge method might be regarded as the most general equation of AFR determination among the existing ones. In the recent years, however, increasing demand for the environmental preservation, including global warming-up protection, and energy conservation lead to introduce the alternative fuel to the internal combustion engine. Therefore, the exact calculations of AFR for these fuels are needed. Especially, for the fuel that contains oxygen, all AFR calculation equations except Eltinge have to be re-formulated. In this paper, the AFR for alternative fuel were calculated by re-formulated carbon balance, accuracy of which was already confirmed, and linear equations, which are newly proposed by statistical method for each fuel. The results show that AFRs based on carbon balance have a little more error compared with gasoline, however, the accuracy is enough for this formula to apply to various fuel. The proposed linear equation also have excellent accuracy below $\lambda=1.2$.