• Title/Summary/Keyword: A/A Reactor System

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A Study on Chaining Threat Analysis of Cybersecurity against Reactor Protection Systems (원자로보호계통 사이버보안 연계 위협 분석 연구)

  • Jung, Sungmin;Kim, Taekyung
    • Journal of Korea Society of Digital Industry and Information Management
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    • v.18 no.2
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    • pp.39-48
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    • 2022
  • The application of digital technology to instrumentation and control systems in nuclear power plants has overcome many shortcomings of analog technology, but the threat of cybersecurity has increased. Along with other systems, the reactor protection system also uses digital-based equipment, so responding to cybersecurity threats is essential. We generally determine cybersecurity threats according to the role and function of the system. However, since the instrumentation and control system has various systems linked to each other, it is essential to analyze cybersecurity threats together between the connected systems. In this paper, we analyze the cybersecurity threat of the reactor protection system with the associated facilities. To this end, we quantitatively identified the risk of the reactor protection system by considering safety functions, a communication type, the use of analog or digital-based equipment of the associated systems, and the software vulnerability of the configuration module of the reactor protection system.

SAFETY STUDIES ON HYDROGEN PRODUCTION SYSTEM WITH A HIGH TEMPERATURE GAS-COOLED REACTOR

  • TAKEDA TETSUAKI
    • Nuclear Engineering and Technology
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    • v.37 no.6
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    • pp.537-556
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    • 2005
  • A primary-pipe rupture accident is one of the design-basis accidents of a High-Temperature Gas-cooled Reactor (HTGR). When the primary-pipe rupture accident occurs, air is expected to enter the reactor core from the breach and oxidize in-core graphite structures. This paper describes an experiment and analysis of the air ingress phenomena and the method fur the prevention of air ingress into the reactor during the primary-pipe rupture accident. The numerical results are in good agreement with the experimental ones regarding the density of the gas mixture, the concentration of each gas species produced by the graphite oxidation reaction and the onset time of the natural circulation of air. A hydrogen production system connected to the High-Temperature Engineering Test Reactor (HTTR) Is being designed to be able to produce hydrogen by themo-chemical iodine-Sulfur process, using a nuclear heat of 10 MW supplied by the HTTR. The HTTR hydrogen production system is first connected to a nuclear reactor in the world; hence a permeation test of hydrogen isotopes through heat exchanger is carried out to obtain detailed data for safety review and development of analytical codes. This paper also describes an overview of the hydrogen permeation test and permeability of hydrogen and deuterium of Hastelloy XR.

Design Considerations on the Standby Cooling System for the integrity of the CNS-IPA

  • Choi, Jungwoon;Kim, Young-ki
    • Proceedings of the Korean Vacuum Society Conference
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    • 2015.08a
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    • pp.104-104
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    • 2015
  • Due to the demand of the cold neutron flux in the neutron science and beam utilization technology, the cold neutron source (CNS) has been constructed and operating in the nuclear research reactor all over the world. The majority of the heat load removal scheme in the CNS is two-phase thermosiphon using the liquid hydrogen as a moderator. The CNS moderates thermal neutrons through a cryogenic moderator, liquid hydrogen, into cold neutrons with the generation of the nuclear heat load. The liquid hydrogen in a moderator cell is evaporated for the removal of the generated heat load from the neutron moderation and flows upward into a heat exchanger, where the hydrogen gas is liquefied by the cryogenic helium gas supplied from a helium refrigeration system. The liquefied hydrogen flows down to the moderator cell. To keep the required liquid hydrogen stable in the moderator cell, the CNS consists of an in-pool assembly (IPA) connected with the hydrogen system to handle the required hydrogen gas, the vacuum system to create the thermal insulation, and the helium refrigeration system to provide the cooling capacity. If one of systems is running out of order, the operating research reactor shall be tripped because the integrity of the CNS-IPA is not secured under the full power operation of the reactor. To prevent unscheduled reactor shutdown during a long time because the research reactor has been operating with the multi-purposes, the introduction of the standby cooling system (STS) can be a solution. In this presentation, the design considerations are considered how to design the STS satisfied with the following objectives: (a) to keep the moderator cell less than 350 K during the full power operation of the reactor under loss of the vacuum, loss of the cooling power, loss of common electrical power, or loss of instrument air cases; (b) to circulate smoothly helium gas in the STS circulation loop; (c) to re-start-up the reactor within 1 hour after its trip to avoid the Xenon build-up because more than certain concentration of Xenon makes that the reactor cannot start-up again; (d) to minimize the possibility of the hydrogen-oxygen reaction in the hydrogen boundary.

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Software Verification & Validation for Digital Reactor Protection System (디지털 원자로 보호계통의 소프트웨어 확인 및 검증)

  • Park, Gee-Yong;Kwon, Kee-Choon
    • Proceedings of the KIEE Conference
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    • 2005.05a
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    • pp.185-187
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    • 2005
  • The reactor protection system is the most important function for the safe operation of nuclear powerplants (NPPs) in that such system protects a nuclear reactor tore whose damage can cause an enormous disaster to the nuclear facility and the public. A digital reactor protection system (DRPS) is being developed in KAERI for use in the newly-constructed NPPs and also for replacing the existing analog-type reactor Protection systems. In this paper, an software verification and validation (V&V) activities for DRPS, which are independent of the DRPS development processes, are described according to the software development life cycle. The main activities of DRPS V&V processes are the software planning documentations, the verification of software requirements specification (SRS) and software design specification (SDS), the verification of codes, the tests of the integrated software and system. Moreover, the software safety analysis and the software configuration management are involved in the DRPS V&V processes. All of the V&V activities are described, in detail, in this paper.

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Development of Self-Actuated Shutdown System Using Curie Point Electromagnet

  • Kim, Tae-Ryong;Park, Jin-Ho
    • Nuclear Engineering and Technology
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    • v.31 no.6
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    • pp.1-7
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    • 1999
  • An innovative concept for a passive reactor shutdown system, so called self-actuated shutdown system(SASS), is inevitably required for the inherent safety in liquid metal reactor, which is designed with the totally different concept from the usual reactor shutdown system in LWR. SASS using Curie point electromagnet(CPEM) was selected as the passive reactor shutdown system for KALIMER (Korea Advanced Liquid MEtal Reactor). A mock-up of the SASS was designed, fabricated and tested. From the test it was confirmed that the mockup was self-actuated at the Curie point of the temperature sensing material used in the mockup. An articulated control rod was also fabricated and assembled with the CPEM to confirm that the control rod can be inserted into core even when the control rod guide tube is deformed due to earthquake. The operability of SASS in the actual sodium environment should be confirmed in the future. All the design and test data will be applied to the KALIMER design.

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Monte Carlo Analysis of the Accelerator-Driven System at Kyoto University Research Reactor Institute

  • Kim, Wonkyeong;Lee, Hyun Chul;Pyeon, Cheol Ho;Shin, Ho Cheol;Lee, Deokjung
    • Nuclear Engineering and Technology
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    • v.48 no.2
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    • pp.304-317
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    • 2016
  • An accelerator-driven system consists of a subcritical reactor and a controllable external neutron source. The reactor in an accelerator-driven system can sustain fission reactions in a subcritical state using an external neutron source, which is an intrinsic safety feature of the system. The system can provide efficient transmutations of nuclear wastes such as minor actinides and long-lived fission products and generate electricity. Recently at Kyoto University Research Reactor Institute (KURRI; Kyoto, Japan), a series of reactor physics experiments was conducted with the Kyoto University Critical Assembly and a Cockcrofte-Walton type accelerator, which generates the external neutron source by deuteriu-metritium reactions. In this paper, neutronic analyses of a series of experiments have been re-estimated by using the latest Monte Carlo code and nuclear data libraries. This feasibility study is presented through the comparison of Monte Carlo simulation results with measurements.

Biological Fixation of $CO_2$ by Chlorella sp. HA-1 in a Semi-Continuous and Series Reactor System

  • LEE JAE-YOUNG;KWON TAE-SOON;BAEK KITAE;YANG JI-WON
    • Journal of Microbiology and Biotechnology
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    • v.15 no.3
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    • pp.461-465
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    • 2005
  • Characteristics of biological $CO_2$ fixation by Chlorella sp. HA-1 were investigated in a semi-continuous and series reactor system using an internally illuminated photobioreactor to overcome shortcomings of physicochemical technologies such as adsorption and membrane separation. High $CO_2$ fixation rate was achieved in the semi-continuous reactor system, in which the dilution ratios of the culture medium were controlled. The average $CO_2$ fixation rate was maintained almost constantly when the dilution ratio increased by 0.1 increment from the initial value of 0.5. The total removal efficiency of $CO_2$ was enhanced by employing a series reactor system. The average $CO_2$ fixation rate increased until 4.013 g $CO_2\;day^{-1}$ in a series operation of four reactors, compared to 0.986 g $CO_2\;day^{-1}$ in a batch operation mode. The total $CO_2$ fixation rate was proportional to the number of reactors used in the series reactor system. In the series reactor system of semi-continuous operation, a large amount of $CO_2$ was removed continuously for 30 days. These results showed that the present reactor systems are efficient and economically feasible for a biological $CO_2$ fixation.

Thermal-hydraulic behavior simulations of the reactor cavity cooling system (RCCS) experimental facility using Flownex

  • Marcos S. Sena;Yassin A. Hassan
    • Nuclear Engineering and Technology
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    • v.55 no.9
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    • pp.3320-3325
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    • 2023
  • The scaled water-cooled Reactor Cavity Cooling System (RCCS) experimental facility reproduces a passive safety feature to be implemented in Generation IV nuclear reactors. It keeps the reactor cavity and other internal structures in operational conditions by removing heat leakage from the reactor pressure vessel. The present work uses Flownex one-dimensional thermal-fluid code to model the facility and predict the experimental thermal-hydraulic behavior. Two representative steady-state cases defined by the bulk volumetric flow rate are simulated (Re = 2,409 and Re = 11,524). Results of the cavity outlet temperature, risers' temperature profile, and volumetric flow split in the cooling panel are also compared with the experimental data and RELAP system code simulations. The comparisons are in reasonable agreement with the previous studies, demonstrating the ability of Flownex to simulate the RCCS behavior. It is found that the low Re case of 2,409, temperature and flow split are evenly distributed across the risers. On the contrary, there's an asymmetry trend in both temperature and flow split distributions for the high Re case of 11,524.

FMEA for CNS Facility and Cause Analysis of Shutdown Events to Improve Reactor Availability (원자로 이용률 향상을 위한 냉중성자원 시설의 고장모드영향분석 및 정지이력의 원인분석)

  • Lee, Yoon-Hwan;Hwang, Jeong Sik
    • Journal of the Korean Society of Safety
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    • v.35 no.5
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    • pp.115-120
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    • 2020
  • From 2009 when the CNS facility was installed, the number of reactor failures due to abnormal CNS facility system has increased significantly. Of the total of 19 nuclear reactor shutdowns over the six years from 2009 to 2019, there were 10 nuclear reactor shutdowns associated with the CNS facility, which are very numerous. Therefore, this report intends to analyze the history of nuclear reactor shutdowns due to CNS facility system failure in detail, and to present the root cause and solution to problems. As a result of FMEA implementation of CNS facility system, a total of 76 SPVs were selected. In addition, 10 cases of reactor shutdown history due to CNS facility system abnormalities were analyzed in detailed, and improvement plans for solving the root cause and problem were suggested for each trip history. The results of this study are expected to be able to operate the domestic research reactor and CNS facilities more stably by providing effective measures to prevent recurrence of CNS facilities and reactor trips.

Dechlorination of High Concentrations of Tetrachloroethylene Using a Fixed-bed Reactor

  • Chang, Young-C.;Park, Chan-Koo;Jung, Kweon;Kikuchi, Shintaro
    • Journal of Environmental Health Sciences
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    • v.36 no.4
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    • pp.323-336
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    • 2010
  • We evaluated the properties of a fixed-bed column reactor for high-concentration tetrachloroethylene (PCE) removal. The anaerobic bacterium Clostridium bifermentans DPH-1 was able to dechlorinate PCE to cis-1,2-dichloroethylene (cDCE) via trichloroethylene (TCE) at high rates in the monoculture biofilm of an upflow fixed-bed column reactor. The first-order reaction rate of C. bifermentans DPH-1 was relatively high at $0.006\;mg\;protein^{-1}{\cdot}l{\cdot}h^{-1}$, and comparable to rates obtained by others. When we gradually raised the influent PCE concentration from $30\;{\mu}M$ to $905\;{\mu}M$, the degree of PCE dechlorination rose to over 99% during the operation period of 2,000 h. In order to maintain efficiency of transformation of PCE in this reactor system, more than 6 h hydraulic retention time (HRT) is required. The maximum volumetric dechlorination rate of PCE was determined to be $1,100\;{\mu}mol{\cdot}d^{-1}l$ of reactor $volume^{-1}$, which is relatively high compared to rates reported previously. The results of this study indicate that the PCE removal performance of this fixed-bed reactor immobilized mono-culture is comparable to that of a fixed-bed reactor mixture culture system. Furthermore, our system has the major advantage of a rapid (5 days) start-up time for the reactor. The flow characteristics of this reactor are intermediate between those of the plug-flow and complete-mix systems. Biotransformation of PCE into innocuous compounds is desirable; however, unfortunately cDCE, which is itself toxic, was the main product of PCE dechlorination in this reactor system. In order to establish a system for complete detoxification of PCE, co-immobilization of C. bifermentans DPH-1 with other bacteria that degrade cDCE aerobically or anaerobically to ethene or ethane may be effective.