• Title/Summary/Keyword: 터보펌프 (turbopump)

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Numerical Investigation of Geometrical Design Variables for Improvement of Aerodynamic Performance of Supersonic Impulse Turbine (초음속 충동형 터빈익형의 공력성능 향상을 위한 기하학적 설계변수 수치연구)

  • Lee,Eun-Seok;Kim,Jin-Han;Jo,Gwang-Rae
    • Journal of the Korean Society for Aeronautical & Space Sciences
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    • v.31 no.8
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    • pp.99-106
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    • 2003
  • Geometrical design variables are numerically investigated to improve aerodynamic performance of the supersonic impulse turbine of a turbopump in a liquid rocket engine. Aerodynamic redesign was performed for maximization of the blade power. Four design variables considered are blade angle, blade thickness and radii of upper and lower arc blade with appropriate constraints. A fast Navier-Stokes solver was developed and Chien's k-$\varepsilon$ turbulence modelling was used for turbulence closure. In initial shape, a flow separation was found in the middle of blade chord. However, it disappeared in final shape via its geometrical design variable change. About 3.2 percent of blade power was increased from this research.

Study on the performance improvement of turbopump inducer by numerical flow analysis (수치 유동 해석을 이용한 터보펌프용 인듀서의 성능 향상에 대한 연구)

  • Lee, Kyoung-Hoon;Kim, Kyung-Ho;Kim, Young-Soo;Woo, Yoo-Cheol
    • 유체기계공업학회:학술대회논문집
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    • 2001.11a
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    • pp.235-242
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    • 2001
  • Hydraulic performance of LCH4 fuel inducer in turbopump system was predicted by 3-D Wavier-stokes calculation. The inducer was designed initially using 1-D method. Different parameters with blade angle and flow coefficient were set from the initial design one, md computation was fulfilled to assess the redesigned models. Especially, influence of inlet back flow on inducer performance and its effective control were explored. The numerical results showed that through reducing inlet back flow strength., the hydraulic efficiency of inducer could be improved up to about $20\%$ compared to that of the initial design one.

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터보펌프 인듀서의 유동해석

  • Choi, Chang-Ho;Hong, Soon-Sam;Kim, Jin-Han
    • Aerospace Engineering and Technology
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    • v.2 no.2
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    • pp.25-32
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    • 2003
  • In the present paper, a computational study on the hydrodynamic behavior of the inducer are presented including the effect of the mass flow rate. The adopted inducer showed very low head rise with high volume flow rates, which may be caused by the small passage area near the trailing edge. The static pressure distributions at the shroud surface are compared with experimental results showing very good agreements. The overall performance of the inducer such as, efficiency, head rise is also compared with experiments. The computational results are generally in good agreements with experimental ones near the design point, but at the high flow rate, the two results shows discrepancy.

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Improvement of the Startup Transient Analysis on the Liquid Rocket Engine Using the TP+GG Coupled Test Result (터보펌프+가스발생기 연계시험 결과를 이용한 액체로켓엔진 시동 과정에 대한 해석 방법의 개선)

  • Park, Soon-Young;Cho, Won-Kook;Moon, Yoon-Wan
    • Proceedings of the Korean Society of Propulsion Engineers Conference
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    • 2011.11a
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    • pp.821-826
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    • 2011
  • The turbopump+gas generator (TP+GG) coupled test for the liquid rocket engine development was performed. By comparing the results of a engine startup transient analysis with this test results, the verification of the analysis model was performed. From this, as to the analysis of the engine startup, the method calculating the pressure ratio of the turbine during the initial stage of startup was improved. And a fact that the transient heat transfer phenomenon between the working fluid and the solid parts of turbine effects to the calculation of turbine pressure ratio and consequentially to the startup analysis was revealed.

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Current Development Status of Inter-Propellant Seal for a Turbopump (터보펌프용 Inter-Propellant Seal의 개발 현황)

  • Kwak Hyun D.;Jeon Seong-Min;Kim Jinhan
    • Proceedings of the Korean Society of Tribologists and Lubrication Engineers Conference
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    • 2004.11a
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    • pp.195-200
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    • 2004
  • To avoid an unexpected explosion occurring from a mixture of LOx and fuel, Inter-Propellant Seal (IPS) is used in a Turbopump. This paper presents a brief theoretical backgrounds of IPS and also reports preliminary test results. Tests were performed up to 1.5 MPa and 20,000 rpm and leakage performance of IPS was evaluated. As a result it was verified that leakage flow rate of IPS satisfied its design requirement.

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Effect of a Booster Inducer on the Suction Performance of Turbopumps (보조 인듀서가 터보펌프의 흡입성능에 미치는 영향)

  • Choi, Chang-Ho;Hong, Soon-Sam;Kim, Jin-Han
    • The KSFM Journal of Fluid Machinery
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    • v.8 no.3 s.30
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    • pp.42-47
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    • 2005
  • Effects of a booster inducer on the suction performance of turbopumps are investigated in this paper. To see the effect of the booster inducer, suction performance tests are conducted with and without the booster inducer for three turbopumps. It is shown that the booster inducer can enhance the suction performance of turbopumps when the tip clearance of the main inducers are relatively large. Numerical analysis are also carried out to see the effects of the booster inducer on the performance of the main inducer. The booster inducer is shown to increase the static pressure at the inlet of the main inducer and prevent growing of inlet back flows which are believed to have deleterious effects on the suction performance of the inducer.

Effect of a booster inducer on the suction performance of turbopumps (보조 인듀서가 터보펌프의 흡입성능에 미치는 영향)

  • Choi, Chang-Ho;Hong, Soon-Sam;Kim, Jinhan
    • 유체기계공업학회:학술대회논문집
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    • 2004.12a
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    • pp.552-557
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    • 2004
  • Effects of a booster inducer on the suction performance of turbopumps are investigated in this paper. To see the effect of the booster inducer, suction performance tests are conducted with and without the booster inducer for three turbopumps. It is shown that the booster inducer can enhance the suction performance of turbopumps when the tip clearance of the main inducers are relatively large. Numerical analysis are also carried out to see the effects of the booster inducer on the performance of the main inducer. The booster inducer is shown to increase the static pressure at the inlet of the main inducer and prevent growing of inlet back flows which are believed to have deleterious effects on the suction performance of the inducer.

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Numerical study on the reactive flow in Gas Generator (가스발생기 내부 유동 특성에 관한 수치 연구)

  • Yu Jungmin;Lee Changjin
    • Proceedings of the Korean Society of Propulsion Engineers Conference
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    • v.y2005m4
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    • pp.198-202
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    • 2005
  • Gas generator is the equipment to produce high enthalpy gas used to generate sufficient power to operate turbine and pump system for propellant feeding in liquid rocket engine. Since the limit in operating temperature is imposed due to turbine blade, the gas generator has to be operated at the temperature far below stoichiometric maintaining fuel rich combustion. In this research, fundamental study was performed to understand the non-equilibrium combustion process with in-house code and CFD-ACE as well.

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로켓엔진용 연료펌프의 성능 시험

  • Kim, Dae-Jin;Hong, Soon-Sam;Choi, Chang-Ho;Kim, Jin-Han
    • Aerospace Engineering and Technology
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    • v.4 no.1
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    • pp.143-149
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    • 2005
  • To evaluate the hydraulic and cavitation performance of a fuel pump for a liquid rocket engine, performance tests of the pump, which consist of hydraulic tests and cavitation tests, were conducted in water environment with various condition. In the hydraulic tests, the head, efficiency and volute pressure distribution of the pump are found to follow the conventional similarity rule, whereas the secondary flow pressure shows a small deviation from the similarity rule. As the floating gap is constricted, the efficiency of the pump improves and the secondary flow pressure decreases. However, the inner diameter of bypass line orifice does not show clear relationship with the pump efficiency. In the cavitation tests, measurements of the head and the NPSH indicate that the pump shows better cavitation performance as the rotational speed of the pump increases.

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Water Tests of Fuel Pump for 75-ton Class Liquid Rocket Engine (75톤급 액체로켓엔진용 연료펌프의 수류시험)

  • Kim, Dae-Jin;Choi, Chang-Ho;Hong, Soon-Sam;Kwak, Hyun-D.;Kim, Jin-Han
    • The KSFM Journal of Fluid Machinery
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    • v.14 no.1
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    • pp.61-65
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    • 2011
  • A series of water tests of a fuel pump for liquid rocket engines are performed at a room temperature. According to the test results, the head coefficient of the pump follows the conventional similarity rule - unlike this, the pump shows better efficiency with higher rotational speed. Also, it is found that the pressure at the rear bearing outlet is higher than expected because the inlet of bypass pipe line is narrow. Furthermore, the cavitation performance of the fuel pump is found to be sufficient for the engine operation and is better at the lower flow ratio and higher rotational speed.