• Title/Summary/Keyword: 시험연소로

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비연소 혼합시험을 통한 이중스월 분사기의 연소성능 예측

  • Ryu, Eung-Hyun;Han, Jae-Seob;Kim, Yoo;Kim, Sun-Jin
    • Proceedings of the Korean Society of Propulsion Engineers Conference
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    • 2000.04a
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    • pp.7-7
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    • 2000
  • 액체추진 로켓 분야에서 비연소 혼합시험(cold flow mixing test)은 로켓엔진의 성능을 예측하고 인젝터와 관련된 문제의 진단에 도움을 줄 수 있는 자료를 확보할 수 있는 수단이 된다. 비연소 혼합시험이 실제 연소시험을 대신할 수 있는 신뢰성 있는 자료를 제공할 수는 없지만, 인젝터의 최적형상을 설계하기 위해서 실시해야할 고 비용의 연소시험에 대한 횟수를 줄일 수 있는 보조시험으로서의 역할을 할 수 있다. 혼합시험 성능이 우수한 인젝터가 수력학적인 혼합성능을 능가하는 연소반응에 의해서 실제 연소시험에서는 성능이 저하되는 경우도 있을 수 있으나 대부분의 경우에는 비연소 혼합시험에서 좋은 성능을 나타내는 인젝터는 실제 연소시험에서도 좋은 성능을 나타낸다. 일반적으로 비연소시험과 연소시험 사이의 상관 관계를 정확히 정립하기 위해서는 많은 상관 관계 변수의 적용 및 충분한 혼합시험 자료가 요구된다.

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Methane Engine Combustion Test Facility Construction and Preliminary Tests (메탄엔진 연소시험설비 구축 및 예비 시험들)

  • Kang, Cheolwoong;Hwang, Donghyun;Ahn, Jonghyeon;Lee, Junseo;Lee, Dain;Ahn, Kyubok
    • Journal of the Korean Society of Propulsion Engineers
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    • v.25 no.3
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    • pp.89-100
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    • 2021
  • This paper deals with the construction of a combustion test facility and preliminary tests for hot-firing tests of a methane engine. First, the combustion test facility for a 1 kN-class thrust chamber using liquid oxygen/gas methane as propellants was designed and built. Before hot-firing tests, the cold-flow tests of each propellant line and the ignition tests of torch igniter/afterburner were performed to verify propellant supply stability of the combustion test facility, operation of the control and measurement system, and successful ignition. Finally, a preliminary hot-firing test was conducted to measure the combustion efficiency, heat flux, and combustion stability of a thrust chamber prototype. The constructed combustion test facility will be helpfully used for basic research and development of methane engine thrust chambers.

Low Pressure Combustion Tests for Technology Demonstration Model of 75 tonf Thrust Chamber (75톤급 액체로켓엔진 연소기 저압연소시험)

  • Kim, Jong-Gyu;Ahn, Kyu-Bok;Lim, Byoung-Jik;Kim, Mun-Ki;Han, Yeoung-Min;Choi, Hwan-Seok
    • Proceedings of the Korean Society of Propulsion Engineers Conference
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    • 2010.05a
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    • pp.10-13
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    • 2010
  • Low pressure combustion tests for TDM(Technology Demonstration Model) of 75 tonf thrust chamber were performed. It has design chamber pressure of 60 bar, propellant mass flow rate of 243.6 kg/s. Due to the limitation of the current firing test facility in Korea, the combustion tests were conducted to verify the operation and the combustion performance at low pressure condition (30 bar, 121.8 kg/s). All the tests had been successfully executed without the damage of the hardware. These test results can be used as fundamental data to predict the combustion performance at design point condition for 75 tonf thrust chamber.

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Combustion Stability Rating Test of Liquid Rocket Engine Thrust Chamber (액체로켓엔진 연소기 연소안정성 평가시험)

  • Ahn, Kyubok;Kim, Jong-Gyu;Choi, Hwan-Seok
    • Journal of the Korean Society of Propulsion Engineers
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    • v.18 no.2
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    • pp.60-66
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    • 2014
  • As a evaluation method of combustion stability in a liquid rocket engine thrust chamber, external disturbance devices are used. In the paper, the study on pulse-gun ignition tests for a combustion stability rating test of a thrust chamber was performed. Charging volume of pulse-guns was determined by confirming the intensities of the pressure waves from the ignition tests in the cold-flow conditions. While using same injector head, combustion instabilities were not encountered during 14 hot-firing tests without pulse-guns but combustion instabilities were triggered by pulse-gun ignition during 2 hot-firing tests. The results showed that the pulse-gun ignition test could be the evaluation method and could reduce the hot-firing test number for the stability rating of a thrust chamber.

Design and Verification of a Injector-Head with Multiple Injectors Arranged in a Row (일렬형 다중 인젝터를 가진 분리형 헤드 제작 및 검증시험)

  • Yu, Isang;Choi, Jiseon;Shin, Donghae;Park, Jinsoo;Ko, Youngsung;Kim, Seonjin
    • Proceedings of the Korean Society of Propulsion Engineers Conference
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    • 2017.05a
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    • pp.1016-1020
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    • 2017
  • This study was conducted to develop a test facility that simulates the combustion instability that occurs in a real-scale liquid rocket combustor. A separate engine head with 3 injectors arranged in a row was designed/manufactured and verified through preliminary tests. The flow rate and spray pattern of the head were confirmed by the cold flow test. Next, propellant spray test and combustion test were carried out. A preliminary combustion test was carried out at 10 bar and the combustion chamber pressure was measured to be significantly lower than the target pressure. This is because it was a low pressure test, and it is expected to be resolved in the high pressure test in the future.

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A Study of Combustion Test Facility for LRE Using Hydrogen peroxide and Kerosene as Propellant (과산화수소/케로신 액체로켓엔진의 연소시험 설비 개발에 관한 연구)

  • Choi, Yu-Ri;Jeon, Jun-Su;Kim, Young-Mun;Ko, Young-Sung;Kim, Yoo;Kim, Sun-Jin
    • Proceedings of the Korean Society of Propulsion Engineers Conference
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    • 2009.05a
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    • pp.29-32
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    • 2009
  • This study is for development combustion test facility of liquid rocket engine system using hydrogen peroxide/kerosene as propellent. For this new facility, we construct thrust measure system, propellent supply system, control and data acquisition system. To perform 200N liquid rocket engine combustion test, operation scenario and sequence were designed. Result of combustion test propellents were supplied to engine stably and confirm of development combustion test facility very well.

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Design of Compressed Gas Supply System for Combustion Chamber Test Facility (연소기 연소시험설비 고압가스 공급시스템 설계)

  • Chung, Yonggahp;Cho, Namkyung;Han, Yeoungmin
    • Journal of the Korean Society of Propulsion Engineers
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    • v.18 no.1
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    • pp.85-90
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    • 2014
  • To develop liquid propulsion engine, the development of combustion chamber must be preceded. For performance validation of the combustion chamber, the designed and manufactured combustion chamber should be tested in combustion chamber test facility (CCTF). The CCTF is the test facility to develop the combustor of rocket engine, which uses liquid oxygen as a oxidizer and kerosene as a fuel. Present paper introduces the detailed design results of compressed gas supply system of CCTF, which is planned to be installed at Naro Space Center.

Combustion Performance Tests of Fuel-Rich Gas Generator for Liquid Rocket Engine at Design Point (액체로켓엔진용 가스발생기의 연소성능시험)

  • Han, Yeoung-Min;Kim, Seung-Han;Moon, Il-Yoon;Kim, Hong-Jip;Kim, Jong-Gyu;Seol, Woo-Seok;Lee, Soo-Yong;Kwon, Sun-Tak;Lee, Chang-Jin
    • 한국연소학회:학술대회논문집
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    • 2003.12a
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    • pp.125-130
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    • 2003
  • 본 논문에서는 액체로켓엔진에서 터보펌프의 160kW급 터빈을 구동하고, 액체산소와 케로신을 추진제로 사용하는 가스발생기의 설계점 연소성능시험 결과에 대해 논의하였다. 충돌형 F-O-F 인젝터, 물냉각 채널을 가진 연소실, torch ignitor, turbulence ring 그리고 측정 링을 갖는 가스발생기에 대해 기술하였고, 점화, 연소, 종료 등의 시험 cyclogram에 대해 언급하였다. 설계점에서의 연소시험 및 turbulence ring 장착여부, 연소실 길이 변화에 따른 연소시험의 결과들에 대해 기술하였다. 연소시험 결과 가스발생기는 설계점에서 안정된 작동성을 보여주었고, 연소압력 및 온도 등의 성능이 예측치에 근접하는 결과를 보여 주었다. Turbulence ring은 출구에서의 가스온도를 균일하게 분포시켜 효과적인 혼합 장치임을 보여 주었고, 4-6msec 정도에서의 잔류시간에서는 연소효율의 차이가 크지 않음을 알 수 있었다. 가스발생기 출구에서의 온도는 공급되는 추진제의 O/F ratio에 따라 매우 민감하게 반응함을 알 수 있었다.

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Certification Test Result of After-burner Test Facility for Gas-generator of 75 tonf Class Liquid Rocket Engine (75톤급 액체로켓엔진용 가스발생기 후연소 시험설비 인증시험 결과)

  • Kim, Chae-Hyoung;Lee, Kwang-Jin;Han, Yeoungmin;Chung, Yonggahp
    • Journal of the Korean Society of Propulsion Engineers
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    • v.19 no.5
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    • pp.91-97
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    • 2015
  • After-burner test facility for gas generators of 75 tonf class liquid rocket engines was designed, which was verified by the facility certification test of the Combustion Chamber Test Facility(CCTF). The purpose of the certification test of the after-burner test facility is to verify the combustion stability of gas torches equipped in the gas generator and the after-burner test facility by using methane and oxygen gases. In the case of the autonomous test, the supply system provided steadily methane and oxygen gases to the after-burner system without pressure drop. The combustion pressure of the gas torch approached the design requirement. In the case of the coupled test, the gas generator ignition and the fuel-rich exhaust gas combustion were successfully carried out, leading to the verification of the test facility.

Experiments on Development A Pulse-Gun Pressure-Wave Inducing Device for Stability Rating Test Technique (연소안정성 평가시험 기법을 위한 펄스건 압력파 유도장치 개발 실험)

  • Lee, Kwang-Jin;Kim, Hong-Jip;Seo, Seong-Hyeon;Moon, Il-Yoon;Kim, Hyung-Mo;Lee, Soo-Yong;Ko, Young-Sung
    • Journal of the Korean Society for Aeronautical & Space Sciences
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    • v.33 no.3
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    • pp.99-106
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    • 2005
  • The SRT(stability rating test) technique, which is indispensable for the development of a LRE(liquid rocket engine), essentially requires a development of a combustion test sequence as well as artificial perturbation devices. For the development of an indigenous SRT technique, several combustion tests of sub-scale LRE were performed to search a proper combustion test sequence. At first, a pressure-wave inducing device which is used for adapting pulse gun was designed and a cooling gas supply system for the pressure-wave inducing device was set up to prevent a malfunction of pulse gun. Through the several combustion tests which included cooling procedure of a pressure-wave inducing device, a proper combustion test sequence was found out. It did not make any significant disturbance at normal combustion process. Finally, an indigenous SRT technique has been developed successfully.