• Title/Summary/Keyword: 배기가스 유입

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The Risk Assessment of Carbon Monoxide Poisoning by Gas Boiler Exhaust System and Development of Fundamental Preventive Technology (가스보일러 CO중독 위험성 예측 및 근원적 예방기술 개발)

  • Park, Chan Il;Yoo, Kee-Youn
    • Journal of the Korean Institute of Gas
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    • v.25 no.3
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    • pp.27-38
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    • 2021
  • We devised the system to automatically shutdown the boiler and to fundamentally block the harmful gases, including carbon monoxide, into the indoor when the exhaust system swerves: (1) The discharge pressure of the exhaust gas decreases when the exhaust pipe is disconnected. The monitoring system of the exhaust pipe is implemented by measuring the output voltage of APS(Air Pressure Sensor) installed to control the amount of combustion air. (2) The operating software was modified so that when the system recognizes the fault condition of a flue pipe, the boiler control unit displays the fault status on the indoor regulator while shutting down the boiler. In accordance with the ventilation facility standards in the "Rules for Building Equipment Standards" by the Ministry of Land, Infrastructure and Transport, experiments were conducted to ventilate indoor air. When carbon monoxide leaked in worst-case scenario, it was possible to prevent poisoning accidents. However, since 2013, the number of indoor air exchange times has been mitigated from 0.7 to 0.5 times per hour. We observed the concentration exceeding TWA 30 ppm occasionally and thus recommend to reinforce this criterion. In conclusion, if the flue pipe fault detection and the indoor air ventilation system are introduced, carbon monoxide poisoning accidents are expected to decrease significantly. Also when the manufacturing and inspection steps, the correct installation and repair are supplemented with the user's attention in missing flue, it will be served to prevent human casualties from carbon monoxide poisoning.

Analysis of Corona Discharge Characteristics according to Flue Gas Composition (배기가스 조성에 따른 코로나 방전특성의 해석)

  • 정재우;조무현;남궁원
    • Proceedings of the Korea Air Pollution Research Association Conference
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    • 2000.11a
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    • pp.249-250
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    • 2000
  • 최근에 환경 오염물질의 제거를 위한 코로나 방전기술이 큰 관심을 끌고 있으며 재래적인 기술들을 능가하는 여러 가지 장점으로 인해 강도 높은 연구들이 이루어지고 있다. 전기방전을 이용하는 공정에서 방전특성은 공정의 효율과 에너지 소모량에 중요한 영향을 미친다. 공정에 따라서 요구되는 방전특성이 다르며, 효율적인 공정이 되기 위해서는 최적의 방전특성에 대한 규명이 이루어져야 한다. 방전에 의해 생성되는 플라즈마 상태는 공정의 전기적 변수들, 반응기의 기하학적 형태, 유입기체의 조성 등 다양한 요소들에 의해 영향을 받으므로 특성에 대한 규명이 매우 어렵다. (중략)

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Design of SCR Reactor for NOx Reduction (질소산화물 제거를 위한 SCR 반응기 설계)

  • 이인영;김동화;이정빈;김우영
    • Proceedings of the Korea Air Pollution Research Association Conference
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    • 2001.11a
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    • pp.425-426
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    • 2001
  • 선택적촉매환원(Selective Catalytic Reduciton: SCR)공정은 배기가스 중 질소산화물을 암모니아와 촉매상에서 반응시켜 무해한 질소와 물로 전환하는 기술이다(Bosch, 1988). SCR 공정에서 우수한 촉매가 확보되었을 경우, 설비의 성능은 촉매층로 유입되는 유동의 조건에 따라 좌우되므로 최적의 유동조건을 갖도록 반응기의 구조와 가이드 베인등 유로변경장치를 설계하는 것은 매우 중요하다(Cho, 1994). (중략)

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헬륨냉동계통의 헬륨가스 순도 제어 운전

  • Choe, Ho-Yeong;Son, U-Jeong;Lee, Mun;An, Guk-Hun
    • Proceedings of the Korean Vacuum Society Conference
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    • 2011.08a
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    • pp.171-171
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    • 2011
  • 헬륨냉동계통은 연구용 원자로인 하나로에서 냉중성자를 생산할 수 있도록 설치된 수조내기기 내의 감속재인 수소가 정상적으로 열 사이펀을 유지하기 위한 주요 계통이다. 헬륨냉동계통은 헬륨가스를 압축하는 헬륨 압축부분과 헬륨가스를 팽창시켜 저온을 생성시키는 헬륨 팽창부분으로 나누어진다. 헬륨 압축부분은 두 개의 스크류가 맞물려 회전하면서 약 1.05 bar(a)의 헬륨가스를 최대 13 bar(a)까지 압축시키는 압축기가 있으며, 헬륨 팽창부분인 냉동박스의 팽창 터빈은 self-acting gas bearing에 의해 구동되며, 저온모드 운전 시작시 헬륨 압축부분에서 일부의 가스는 팽창 터빈 축(shaft)으로 유입되어 회전속도가 서서히 증가하면서 고속으로 회전하여 극저온의 헬륨가스(14~18 K)를 생성하는 주요 기기이다. 헬륨을 팽창하는 부분인 냉동박스 내로 헬륨 압축가스를 유입하기 전에 압축된 헬륨가스 내 불순물의 순도를 분석하여 냉동박스의 주요 부품인 팽창터빈의 운전에 영향을 미치지 않는 것이 가장 중요하다. 따라서 헬륨 저압측에 헬륨가스 내 불순물 즉, 수소($H_2$), 수분($H_2O$), 질소($N_2$), 탄화수소류(CxHy) 및 오일(Oilaerosol) 등의 함량을 분석하기위해 가스 분석기가 설치되어 있으며, 냉동박스 내로 유입되기 전에 헬륨압축에서 순환되는 가스 내 불순물인 수분, 질소, 탄화수소류 및 오일은 10 vpm 이하이어야 하며, 수소 함량은 0.1 % 이내이어야 한다. 헬륨 압축부분에서 순환되는 가스의 불순물이 요구 조건에 만족하도록 헬륨 고압측과 헬륨 저압측에 cryogenic adsorber를 설치하여 가스 내 불순물을 제거하는 가스순도제어 작업을 수행해야 한다. cryogenic adsorber를 사용하기 위해서는 장치 내의 불순 가스를 공정진공도(1.33 X $10^{-3}$ mbar) 이하로 진공배기하는 작업이 매우 중요하다. 이는 계통의 헬륨가스가 오염되지 않도록 하는 것으로 cryogenic adsorber 내에는 액체질소를 충전하여 액체질소 온도에 노출된 활성탄층을 헬륨가스가 흐르면서 수분, 질소, 탄화수소류 및 오일 등이 제거된다. 이 논문에서는 헬륨냉동계통의 가스 순도 제어 작업을 통해 헬륨가스의 순도가 요구조건 이하로 만족하며, 팽창 터빈의 운전에 영향을 미치지 않음을 기술하고자 한다.

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Analysis of cause of engine failure during power generation using biogas in sewage treatment plant (하수처리장 바이오가스를 이용한 발전시 가스엔진의 고장원인 분석)

  • Kim, Gill Jung;Kim, Lae Hyun
    • Journal of Energy Engineering
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    • v.25 no.4
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    • pp.13-29
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    • 2016
  • In this study, we analyzed the causes of major faults in the biogas plant through the case of gas engine failure when cogenerating electricity and heat using biogas as a fuel in the actual sewage treatment plant and suggested countermeasures. Hydrogen sulfide in the biogas entering the biogas engine and water caused by intermittent malfunction of the water removal system caused intercooler corrosion in the biogas engine. In addition, the siloxane in the biogas forms a silicate compound with silicon dioxide, which causes scratches and wear of the piston surface and the inner wall of the cylinder liner. The substances attached to the combustion chamber and the exhaust system were analyzed to be combined with hydrogen sulfide and other impurities. It is believed that hydrogen sulfide was supplied to the desulfurization plant for a long period of time because of the high content of hydrogen sulfide (more than 50ppm) in the biogas and the hydrogen sulfide was introduced into the engine due to the decrease of the removal efficiency due to the breakthrough point of the activated carbon in the desulfurization plant. In addition, the hydrogen sulfide degrades the function of the activated carbon for siloxane removal of the adsorption column, which is considered to be caused by the introduction of unremoved siloxane waste into the engine, resulting in various types of engine failure. Therefore, hydrogen sulfide, siloxane, and water can be regarded as the main causes of the failure of the biogas engine. Among them, hydrogen sulfide reacts with other materials causing failure and can be regarded as a substance having a great influence on the pretreatment process. As a result, optimization of $H_2S$ removal method seems to be an essential measure for stable operation of the biogas engine.

Pressure Recovery in a Supersonic Ejector of a High Altitude Turbofan Engine Testing Chamber (터보팬 엔진의 고고도 성능의 초음속 이젝터의 압력회복에 관한 연구)

  • Omollo, Owino George;Kong, Chang-Duk
    • Journal of the Korean Society of Propulsion Engineers
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    • v.14 no.6
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    • pp.53-59
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    • 2010
  • This research aims in finding a more optimal ejector size for evacuating engine exhaust gasses and 20% of the cell cooling air. The remaining 80% of cell cooling air pumped into the test chamber is separately exhausted from the test chamber via a discharge port fitted with flow control valves and vacuum pump. Unlike its predecessor this configuration utilizes a smaller capture area to improve pressure recovery. The modified ejector size has a diameter of 1100mm enough to evacuate 66kg/s jet engine exhaust in addition to about 20%, 24kg/s of the cell cooling air tapped from the sterling chamber. This configurations has an area ratio of the engine exit and ejector inlet of about 1.2. Simulation results of the proposed ejector configuration, indicates improved pressure recovery.

A Study on the Treatment Performance of Coalescer to Treat Exhaust Gas Cleaning Water (콜레이서를 이용한 배기가스 세정수 처리 성능에 관한 연구)

  • Ha, Shin-Young;Kim, In-Soo
    • Journal of Navigation and Port Research
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    • v.40 no.1
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    • pp.1-6
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    • 2016
  • This study was conducted on a circulation system which can recycle waste water from EGCS(Exhaust Gas Cleaning System) using a wet scrubber that is used to treat air pollutants from ships. Though we developed a water treatment system that could remove effectively particulate matters and dispersed oil included in cleaning water for Ship Exhaust Gas Recycle System(DePM & DeSOx), we found that it is difficult to treat minutely dispersed oil only by means of centrifugal-typed purifier. Therefore, to this system, we applied a coalescer that coalesces emulsified minute oil particles in the 2nd phase of dispersion state after being filtered through the centrifugal-typed purifier. After we treated cleaning water drained out of Ship Exhaust Gas Recycle System(DePM & DeSOx) by using both purifier and coalescer, we found that particulate matters and dispersed oil were removed more than 55% and 99%, respectively, in comparison with those contained in cleaning water influent. Putting the results together, we conclude that the treated cleaning water can be recycled as normal cleaning water if this cleaning water treatment system is employed by the wet cleaning tower system for the reduction of air pollutants from ships.

특집:녹색선박 SCR시스템 기술개발 현황 - 촉매반응기 내부 유동특성에 관한 수치해석

  • Jeong, Gyeong-Yeol;Park, Chang-Dae;Im, Byeong-Ju;Lee, Jung-Seop;Seo, Jeong-Se;Yun, Ji-Hun
    • 기계와재료
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    • v.24 no.2
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    • pp.80-93
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    • 2012
  • 본 연구는 5,000PS급 선박용 SCR 촉매시스템에 관한 내부 유동특성을 전산유체역학(CFD)을 통해 예측하고 설계에 반영하기 위한 기초를 확보하기 위함이다. 따라서 SCR 촉매반응기 내부 유동특성을 수치해석하기 위한 기법을 소개하였고, 촉매 Cell에 대한 수학적 모델링을 제시한 후 SCR 촉매시스템에서 NOx를 환원시켜 주는 촉매담체에 대한 압력강하를 실험과 수치해석을 통해 비교하였다. 그 결과 수치해석 결과가 실험에 매우 근접함을 확인할 수 있었다. SCR 촉매반응기에 대한 유동특성을 수치해석을 수행하여 각 지점에 대한 압력과 속도분포를 확인하였다. 또한 촉매 담체로 배기가스가 유입되는 입구부의 유동균일도를 예측하기 위해 Inlet pipe의 $90^{\circ}$ 각도에서 유입길이를 변화시켜 수치해석을 수행하였다. 그 결과 각도와 길이에 영향을 받는 것으로 나타났다.

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Pressure Recovery in a supersonic ejector of a high altitude testing chamber (초음속 이젝터의 압력회복에 관한 연구)

  • Omollo, Owino George;Kong, Chang-Duk
    • Proceedings of the Korean Society of Propulsion Engineers Conference
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    • 2010.11a
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    • pp.833-837
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    • 2010
  • This study aims at finding an optimal exhaust diffuser design of a high altitude testing chamber for a low bypass turbofan engine (F404-402) with thrust pound force of 17,700 and air mass flow rate of 66kg/s ejecting at a speed of Mach 1.66. The final proposed ejector size has better pressure recovery characteristics and targets to reduce operational cost at engine performance testing. Conventional high altitude test chamber layout was adopted and first drawn in two dimensions using Autocad software so as to determine the gas path, the ejector frontal size was then determined from gas dynamics equations considering traditional gas ejection method where both the engine exhaust and cell cooling air are exhausted via the ejector. Modification to a smaller ejector with an alternative secondary cell cooling exhaust port was then performed and modelled in 3D using Solid Works software.

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Study on Heat Exchanging Characteristics of Automobile Exhaust Heat Recirculation Device (자동차 배기열 재순환장치의 열교환 특성에 관한 연구)

  • Hong, Young-Jun;Choi, Doo-Seuk;Jung, Young-Chul;Kim, Jong-Il
    • Journal of the Korea Academia-Industrial cooperation Society
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    • v.12 no.10
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    • pp.4302-4307
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    • 2011
  • Recently, various technologies for the fuel efficiency improvement are being developed. The purpose of this study is to evaluate the heat exchanging performance of a exhaust heat recirculation device and to propose a model with optimized performance. The device has been designed to warm up engine coolant as quickly as possible using wasted exhaust heat. To achieve these goals, heat transfer characteristics has been analyzed using CFD for the flow direction effect and in/out location effect of coolant. A method improving the effectiveness of heat exchange has been proposed. As a result, the highest efficiency in heat exchange was observed on condition that exhaust heat affects the coolant directly with a separate flow path between exhaust gas and coolant and that coolant flow rate is relatively low.