• Title/Summary/Keyword: 기어식

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Development of the Steering Gear Box for Electric Vehicles based on the Reverse Engineering (역설계 기반의 전기자동차 스티어링 기어박스 개발)

  • Moon, Sung-Sik;Yoo, Young-Min;Yoo, Woo-Sik
    • IE interfaces
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    • v.25 no.1
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    • pp.134-141
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    • 2012
  • The steering gear box for mid-heavy duty electric vehicles are usually produced by only a few specialized companies. The special techniques, such as designing, producing and testing technology have been veiled. For this reason, steering gear boxes are imported from other country. The durability test with the electric vehicle which is satisfies the design parameters takes several years, and a prototype is installed in the real vehicle for the test. In this research, the steering gear box of the steering system was developed based on the reverse engineering and the testing methods and the steering gear box development process have been suggested. The prototype is also developed with the CAD and CAE tools. Developed steering gear box have been tested in torque tester and have satisfied requied torque. As a result, the process and testing methods studied in this research are useful in the development processes of electric vehicles steering system.

An Experimental Study on the Rotational Performances of NC Lathe Spindle System (NC 선반주축 의 회전성능 향상 을 위한 실험적 연구)

  • 이형식;이봉진;송기무
    • Transactions of the Korean Society of Mechanical Engineers
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    • v.8 no.1
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    • pp.86-94
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    • 1984
  • In order to improve the rotational performances of NC lathe spindle system in high speed range, a new type(Floating-type driven by V-belt)spindle system was optimally designed and experimented. Through the results of the experiments, the rotational performances of the new type spindle system was discussed and compared with the three equivalent conventional lathe spindle systems. The spindle rotational accuracy( radial error motion of spindle axis), the accelation and the temperature rise of the front spindle bearings for the non-cutting operation were considered as the spindle rotational performances. The radial error motion of the spindle axis was measured by applying the modified L.R.L. method. Compared with the equivalent conventional spindle systems, the following results were obtained. (1) The new type spindle system reduces the radial error motion of the spindle axis in high speed range(1800rpm-2000rpm). (2) The new type spindle system reduces the acceleration and the temperature rise of the spindle bearings considerably with increasing the spindle speed. It is also confirmed that, by this new type spindle system, the max. allowable speed can be increased with satisfying the spindle rotational performances.

Reduction of Rattle Noise in a Direct-Engine PTO Driveline Using an Anti-backlash Gear (안티-백래시 기어를 이용한 엔진 직결식 PTO 전동 라인의 치타음 감소)

  • Shim, Sung-Bo;Park, Young-Jun;Kim, Kyeong-Uk
    • Journal of Biosystems Engineering
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    • v.32 no.3
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    • pp.137-144
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    • 2007
  • An anti-backlash gear was developed to reduce the rattle noise generated from the gearbox of a direct-engine PTO driveline of agricultural tractors under idling. A pair of gears using the anti-backlash gear as driven part was modeled and verified. Using the verified model, a computer simulation was conducted to investigate the effects of design parameters of the anti-backlash gear on the reduction of rattle noise. The optimum values of the design parameters were also determined by the computer simulation. The optimized anti-backlash gear was then manufactured and installed on the experimental PTO driveline for the performance test. Measurement of rattle noise was made to evaluate its performance before and after the driven gear of the PTO gearbox was replaced by the optimized anti-backlash gear. Results of the study were as follows: The optimum values of the design parameters, spring constant and deformation, may be determined by a relationship: $$k{\ge}\frac{4364.7}{150{\delta}-23.564}$$ The optimized anti-backlash gear reduced the rattle noise maximally by 16.9 dBA. This concluded that it would be most effective to use the optimized anti-backlash gear to eliminate the rattle noise in the PTO driveline.

Development of a new hybrid power system (신개념 하이브리드 동력장치 개발)

  • Kim, Nam-Wook;Yoon, Young-Min;Ha, Seung-Bum;Lim, Won-Sik;Park, Young-Il;Lee, Jang-Moo
    • 한국신재생에너지학회:학술대회논문집
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    • 2005.11a
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    • pp.533-536
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    • 2005
  • In this paper, a new drive system(SHS) for hybrid electric vehicle is proposed. As dual rotor hybrid electric vehicle using planetary gearsets, the SHS has the advantages of both series and parallel systems. The output speed and torque of SHS can be determined at specific point regardless of the engine's operating point. When the size of generator which is used in SHS is same as in THS, the SHS has more activities of engine control due to the ability that is operated in lower speed range. To maximize the performance of system, we carried out optimization for the three parameters that are engine, motorl and motor2. As the result of the optimization, we confirmed the SHS is more preferable to THS in fuel consumption and acceleration area.

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A Study on the Modeling and Simulation of an Electro-Hydraulic Power Steering system (전기 유압식 동력 조향시스템의 모델링 및 시뮬레이션에 관한 연구)

  • Kim, Ji-Hye;Kim, Sung-Gaun
    • Journal of the Korea Academia-Industrial cooperation Society
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    • v.13 no.3
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    • pp.1008-1013
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    • 2012
  • Electro-hydraulic power steering (EHPS) system is the power-assisted steering which operates the hydraulic pump by BLDC motors for assisting the steering force. EHPS consists of BLDC motor, gear pump, oil-hydraulic circuit and steering system. Since EHPS is a convergence system consisting of electricity and electronic, hydraulic and mechanical system, it is difficult to establish the simulation model. In this paper, the mathematical model of EHPS system components were presented, and the simulations of the multi-domain system were performed by using AMESim. The trial and error of development would be reduced by using this simulation results, and it would be helpful for developing high-quality EHPS.

Design of Electric Automatic Manual Wheelchair Driving System (수·전동 휠체어 구동부 시스템 설계)

  • Kim, Jin-Nam
    • Journal of the Korea Academia-Industrial cooperation Society
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    • v.14 no.11
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    • pp.5392-5395
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    • 2013
  • Application of electric wheelchair, sort of wheelchair which is playing important role in transporting patients and old people, has been increasing. In this study, we designed the electric wheelchairs' driving system. Using the multi-step gear, the driving system can get great power, even though the small capacity of motors. First, we designed the multi-step gear, test its bending strength and contact strength, as well as verified its performance. We installed 'B-type electric brake(Multiple plate clutch, Anti-magnetization) in same axle of the driving system, so it is possible to stop under huge torque and small size. Using this driving system of the multi-step gear which we designed, it's possible to improve driving gear efficiency 30% up and create the high-competitive electric wheelchair. And, it is easy to repair and control.

Development and Application of an Open Water Test System for Azimuth Thrusters (아지무스 추진기 단독시험 시스템 개발 및 적용)

  • Lee, Young-Jin;Rhyu, Seong-Sun;Seo, Jong-Soo;Lew, Jae-Moon
    • Journal of the Society of Naval Architects of Korea
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    • v.50 no.4
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    • pp.199-205
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    • 2013
  • To research and develop an azimuth thruster, the new type of open water test dynamometers to measure thrust, torque, total thrust and duct force are designed and manufactured by Samsung Ship Model Basin(SSMB). A compact servomotor to be accurately controlled is connected to precise spiral bevel gear through shafting system combined by couplings and main shafts. The dynamometers have shown excellent linearity and repeatability for all components of forces and a torque. Also, the open water tests have been successfully performed to show the performance of the system. In near future, it is expected that the device can be used for the study of scale effects and development of azimuth thrusters.

Multi-stage Cold Forging Process Design and Backward Extrusion Characteristics Evaluation of Serration Gear for Electronic Parking Brake (전자식 파킹 브레이크용 세레이션 기어의 냉간다단단조 공정 설계 및 후방 압출특성에 관한 평가)

  • Seo, Ju-Han;Choi, Jong-Won;Jung, Eu-Enn;Kang, Myungchang
    • Journal of the Korean Society of Manufacturing Process Engineers
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    • v.21 no.2
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    • pp.130-136
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    • 2022
  • Reducing production costs through net-shaped cold forging is an important aspect in the automobile industry. In this study, we intend to produce a net-shaped electronic parking brake (EPB) serration gear for automobiles, using multi-stage cold forging. These serrations are then assembled to the reduction gear of an EPB actuator. The forging process of the serrations and the cold forging design were verified through finite element analysis (FEA) in order to evaluate metal flow. The forging machine was selected by checking the load using FEA. Based on the FEA results, molds were designed, and parts were made using multi-stage cold forging to produce a net-shaped serration gear.

Design of the Hydro-Mechanical Transmission for a 55kW-Class Agricultural Tractor (55kW급 농업용 트랙터 정유압 기계식 변속기 설계)

  • Baek, Seung Min;Kim, Wan Soo;Kim, Yeon Soo;Baek, Seung Yun;Kim, Yong Joo
    • Journal of Drive and Control
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    • v.17 no.2
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    • pp.19-27
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    • 2020
  • The purpose of this study was to suggest design criteria for the HMT (hydro-mechanical transmission) of a 55 kW-class agricultural tractor, develop a simulation model, and evaluate its performance such as axle rotational speed, tractor speed, and power transmission efficiency. In this study, the HMT comprised a compound planetary gear and a HSU (hydro-static unit), and the compound planetary gear comprised two planetary gear sets. The HMT has three gear stages, and the maximum tractor speed was selected as 40 km/h. The simulation time was set at 2736 hours considering the lifetime of the tractor, and the simulation was performed for each gear stage at the engine-rated power conditions. As a result of the simulation, the axle rotational speeds for each gear stage were 39, 77, and 158 rpm, respectively. The range of tractor speed for each gear stage were 1.05-10.22 km/h, 10.74-20.17 km/h, and 20.70-41.40 km/h, respectively. The APE (absolute percentage gear) for the tractor's maximum speed between target value and simulation results were 2.20%, 0.85%, and 3.50%, respectively. Also, the power transmission efficiency for each gear stage were 0-75%, 72-81%, and 69-81%, respectively. The simulation results for the power transmission efficiency of the HMT were similar with the results of the previous research. This was a basic study on the development of the HMT for an agricultural tractor. In future studies, it is necessary to develop a tractor platform and evaluate the performance. The comparison between the simulation model and the HMT tractor should be performed.

Design of a Torque Application Device in Test Rig for a Wind Turbine Gearbox (풍력발전기용 증속기 시험 장비의 토크 인가 장치 설계)

  • Kim, Jeong-Gil;Park, Young-Jun;Lee, Geun-Ho;Nam, Yong-Yun;Oh, Joo-Young
    • Transactions of the Korean Society of Mechanical Engineers A
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    • v.39 no.5
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    • pp.507-515
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    • 2015
  • This study was conducted to develop and verify a torque application device for use in a mechanical power-circulation test rig for 5.5 MW wind turbine gearboxes. The design and analysis of the torque application device was conducted. In addition, the torsional stiffness of the test rig was calculated using the rotational angle measurements for each of the components. The calculated stiffness of the test rig was $231.13kN{\cdot}m/rad$ for a clockwise torque application. The rated torque can be applied when the stiffness of the gearbox is greater than $1,064,400kN{\cdot}m/rad$ for a clockwise torque application. Because of the limited rotational angle of the test rig, the potential application of the rated torque is determined according to the torsional stiffness of the test gearbox.