• Title/Summary/Keyword: volute

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Production of Fluorosilicic Acid from Phosphoric Acid Slurry of a Fertilizer Manufacturing Plant (비료공장의 인산 슬러리로부터 규불산 제조)

  • Kim, Se-Won;Moon, Woo-Kyun;Park, Hung-Suck
    • Journal of the Korea Academia-Industrial cooperation Society
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    • v.13 no.2
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    • pp.926-933
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    • 2012
  • Phosphoric acid used for the production of phosphate fertilizers is synthesized by the reaction of phosphate rock and sulfuric acid. As the reaction is exothermic, yield of phosphoric acid is poor at elevated temperature. Therefore, enhancement in its yield requires the process temperature be maintained by releasing the vapor ($80^{\circ}C$) containing HF and SiF4 through a vacuum cooler. However, these valuable resources; Fand Si, which can be utilized for the manufacture of refrigerant and polysilicon, respectively, are being wasted in the treatment process. We performed lab-scale experiments to estimate the amount of recoverable H2SiF6, a by-product of phosphoric acid manufacturing process. The experimental results showed a decrease of fluorine concentration by 0.12wt% in the liquid phase. Preliminary estimation showed a possible recovery of 5,509 ton/yr of fluorine considering the scale of the fertilizer manufacturing plant. Furthermore, field-scale experiment showed that H2SiF6 could be enriched in liquid phase from 0.35wt% to 7.33wt% and the vapor flow-rate from vacuum cooler was estimated at $51,000m^3/hr$. Anew, the efficiency of fluorine recovery in the pilot-scale experiment was found to be 76.74% and the production of H2SiF6 was estimated at 5,340 ton/yr.

Mass Flow Rate Measurement of Pulsating Flow in a Twin-Scroll Turbocharger (트윈스크롤 터보과급기에서 맥동유동의 질량유량 측정)

  • Chung, Jin-Eun;Jeon, Se-Hun
    • Journal of the Korea Academia-Industrial cooperation Society
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    • v.20 no.12
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    • pp.723-729
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    • 2019
  • Turbochargers are an effective device to reduce the fuel consumption. In this study, the mass flow rate of pulsating flow in the twin-scroll turbocharger for the gasoline engine of passenger vehicles was measured. Pulsating flow was achieved using a pulse generator and the mass flow rate of the unsteady pulsating flow was analyzed by comparing it with those of the steady flow. The pulse generator consisted of a rotating upper plate and a fixed lower plate. To measure the mass flow rate of unsteady flow, the orifice flow meter equipped with the difference pressure transducer was used. To analyze the low speed performance of the turbocharger, the measurement was carried out in the speed of turbocharger from 60,000rpm to 100,000rpm. The mass flow parameters of the unsteady pulsating flow showed a large difference compared to those of the steady flow. Those of the unsteady flow showed the hysteresis loop surrounding the mass flow parameters of the steady flow and the maximum variation of the mass flow parameters were 5.0 times those of the steady flow. This phenomenon is the result of the filling and emptying the turbine volute space due to pulsating flow.

A Study on Hot Extrusion Characteristics of Particulate Reinforced Aluminium Matrix Composite. (입자분산강화 알루미늄 복합재의 압출가공특성에 관한 연구)

  • Gwon, Hyeok-Cheon;Yun, Ui-Park
    • Korean Journal of Materials Research
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    • v.5 no.8
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    • pp.953-959
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    • 1995
  • It was investigated that reinforced species, billet condition and extrusion variation in Al 6061 composite material effected on extrusion process of particulate reinforced composite material. The strength of composite material with reinforcement species revealed SiC$\sub$w/> A1$_2$O$\sub$3f/ > A1$_2$O$\sub$3f/ > A1$_2$O$\sub$3f/ orderly. K$\sub$w/ increased as volute fraction increased in all composite material. The composite materials reinforced by A1$_2$ $O_3$required the larger pressure in hot extrusion process than those by SiC$\sub$p/ at all condition. Extrusion process tended to decrease as the semi-angle of extrusion dies increased because larger contact area caused larger shear friction. Extrusion temperature went up about 50$^{\circ}C$ in low elevated deformation temperature. In extrusion temperature above 500$^{\circ}C$, severe tearing occurred on extrusion surface. More reinforcement in volume fraction, more hot tearing.

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Study on the Decontamination of Primary Cooling Pump in HANARO (하나로 1차 냉각펌프 제염에 대한 고찰)

  • An Jung-Sug;Lee Kyung-Ho;Kim Kwang-Dug;Park Young-Chul
    • Proceedings of the Korean Radioactive Waste Society Conference
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    • 2005.06a
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    • pp.21-29
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    • 2005
  • The HANARO, a multi-purpose research reactor of 30 MWth open-tank-in-pool type, has been under normal operation since its initial criticality in February, 1995. Recently, ten years after the initial operation of the HANARO, one of the two primary cooling pumps was decontaminated for overhaul maintenance in 2004. Before decontamination exposure doserate and surface contamination level of primary cooling pump measured at 4 points. After final decontamination exposure doserate and surface contamination level of primary cooling pump remeasured by same method done before. It is easy to decontaminate the out side exposed surfaces of the pump, but it is difficult to approach the inside surface due to double volute installed in the casing. Therefore, a new decontamination facility has been developed to solve this problem. A concentrated de-contaminant (DX-300) is rotated in the closed pump casing by the impeller actuated by a temporary motor. Nuclide particles are removed by the emulsification effect of the de-contaminant and the surface contaminants are chemically removed from the pump by the corrosion and dissolution effect. The inside surfaces of the primary cooling pump have been decontaminated by using the facility. As results, the contamination level of the inside surfaces was maintained below the surface contamination limit.

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Analysis of Abnormal Signals for Induction Motor according to Operating Status of Fire Pumps (소방펌프의 운전상태에 따른 유도전동기의 이상 신호 분석)

  • Ku, Bonhyu;Kim, Doo-Hyun;Kim, Sung-Chul
    • Journal of the Korean Society of Safety
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    • v.37 no.4
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    • pp.20-27
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    • 2022
  • This article aims to develop an algorithm that detects fire pump defects by analyzing the current signals of an induction motor, which are triggered by changes in the flow rate and pressure of multistage volute pumps that are used for fire services. The operational status of the pumps was categorized into three: first, normal operation; second, a defect that is caused by a change in the current value; and third, a defect occasioned by a change in current, pressure, and flow rate. When a fire pump was in normal operation, the motor's operating current was measured between 5.06 A and 6.9 A, the flow rate was estimated at 0-0.27 m3/min, and the pressure ranged from 0 to 0.47 MPa. In the event that a defect was caused by an abnormal current value in the motor, it was attributed to the pump's adherence. Furthermore, if there was no source of water, the defect was considered to have been induced by phase-loss operation, no-load operation, or run-stop operation, with the current value of each scenario being measured at > 52.8 A, < 4.13 A, > 45.15 A, and < 3.8 A, respectively, placing its overall range between 0 and 50 A. The sources of defects were detected based on an analysis of the flow rate, pressure, and current, which represent the following causes: air inflow into the casing, inadequate suction of water, and reverse-phase operation, respectively. Each cause entailed the following values: when air seeped into the casing, the pressure was measured at 0.24 MPa irrespective of changes in the flow rate; when there was inadequate suction of water, the pressure was recorded between 0 and 0.05 MPa despite changes in the flow rate; and when the power line's reverse-phase loss was the cause of the defect, the pressure was measured at 0.33 MPa for a flow rate of 0 L/min, and a higher flow rate decreased the pressure to nearly 0 MPa. The results of this study will enable engineers to develop a pump defect detection algorithm that is based on an analysis of current, and this algorithm will facilitate the execution of a program that will control a fire pump defect detection system.