• Title/Summary/Keyword: screw conveyer

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Study on Dechlorination of Iron Oxide (산화철중 염소성분 제거기술 연구)

  • Jin-Gun Sohn
    • Resources Recycling
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    • v.9 no.5
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    • pp.22-27
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    • 2000
  • Iron oxide produced form the pickling process at the cold rolling mill in iron & steelmaking industry, use for raw material of electronic an colorant product. Recently, decreasing of the chlorine content in iron oxide is demanded at the market. In this study, under the field test of the spray roaster and the screw conveyer for dechlorination, the experiments of the chlorine content in iron oxide were investigated. From the results of experiment, the chlorine content in iron oxide can be reduced to 1,100 ppm from the spray roaster and, 383 ppm from the screw conveyer.

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Development of Air-jet Washer for the Agaricus Bisporus (공기분사에 의한 양송이 버섯 세척기 개발)

  • Park, H.M.;Cho, K.H.;Hong, S.G.;Lee, S.H.
    • Journal of Biosystems Engineering
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    • v.34 no.3
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    • pp.167-174
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    • 2009
  • This study was conducted to develop an agaricus bisporus washing machine which uses compressed air to remove foreign materials attached on the surface of agaricus bisporus. A prototype of the washing machine was constructed, and performance of removing foreign materials was tested. Research results are as follows: 1. Several transferring methods including PE roller rotation, brush roller rotation, PE screw rotation, vibration plate, and belt conveyor were evaluated. Roller, screw, and vibration methods caused damages on the surface of the products, but belt conveyor method caused the least damages. 2. For air jet, a stationary nozzle type and a rotational type were evaluated. The best air jet nozzle was the jet-type nozzle, and the rotational type was more effective than stationary type nozzle. 3. With the conveyer belt, box type moving method and the rotational air jet nozzle, the washing machine showed the best performance when higher than 5.4${\times}$105 Pa of air jet pressure and lower than 0.047 m/s of moving speed was used. Working performance of the system was 650 kg/h, and the damaging rate was 1.2 %.

Automation of Tire Tread Extruder Line Using Cameras (카메라를 이용한 타이어 트레드 압출라인 자동화)

  • Pyo, Choon-Seon;Lyou, Joon
    • Journal of Institute of Control, Robotics and Systems
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    • v.19 no.3
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    • pp.262-267
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    • 2013
  • This paper describes a vision based automation case study for the tire tread extruder line. To accurately measure the thread widths, two cameras with laser line illumination have been installed near the takeaway conveyer. The overall tread extruder line is then automated by controlling the speeds of take away conveyor and screw motor such that a difference between measured widths and the targeted data is minimized. By doing this, the conventional tread extruder line has been replaced by the developed automated computer system and with only one operator, increasing the production efficiency and reducing safety accidents.

The Development of U-recovery by Continuous Electrorefining (연속식 전해정련에 의한 우라늄 회수기술 개발)

  • Kim, Jeong-Guk;Park, Sung-Bin;Hwang, Sung-Chan;Kang, Young-Ho;Lee, Sung-Jai;Lee, Han-Soo
    • Journal of Nuclear Fuel Cycle and Waste Technology(JNFCWT)
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    • v.8 no.1
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    • pp.71-76
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    • 2010
  • The electrorefining process, one of main processes which are composed of pyroprocess to recover the useful elements from spent fuel, and the domestic development of electrorefiner have been reviewed. The electrorefiner is composed of an anode basket containing reduced spent fuel such as uranium, transuranic and rare earth elements, and a solid cathode, which are in LiCl-KCl eutectic electrolyte. Oxidation (dissolution) reaction occurs on the anode and a pure uranium is electrochemically reduced (deposited) on the solid cathode. By application of graphite cathode, which has a self-scrapping characteristics for the uranium deposits, and a recovery of the fallen deposits by a screw conveyer, a high-throughput continuous electrorefiner with a capacity of 20 kgU/day has been developed.

Development of an Automated Measurement System for Dilution Process and Spraying Amount of Disinfectant

  • Kim, Jung-Chul;Chung, Sun-Ok;Cho, Byoung-Kwan;Chang, Hong-Hee;Kim, Suk;Chang, Dongil
    • Journal of Biosystems Engineering
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    • v.38 no.4
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    • pp.228-239
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    • 2013
  • Purpose: The objectives of this study were to develop an automated disinfectant dilution system, and an automated data management system for spraying amount for resolving uncertainty problem. Methods: Proper diluting rate was made by a controlled volume pump for liquid disinfectant and a screw conveyer pump for solid disinfectant. The water capacity of disinfecting system of 400 L was controlled by two water level sensors. The water quantity of water tank was controlled by the signals which were produced by the water level sensors. Signals were processed by Labview Programming, and ON/OFF of solenoid valve that was used for controlling water supplying to water tank, was controlled by SSR. The operating time of pumps for disinfectant was controlled quantitatively. A turbine flowmeter was used for development of automated measurement system for spraying amount of disinfectant. In order to save the flowmeter data and to control the spraying system, a multi-function data logger was used, and it was processed and saved in Excel file by a program developed in this study. Results: Labview 2010 was used for programming to control the automated measurement system for spraying amount of disinfectant. Results showed that the relationship between flowmeter value and time had a significant linear relationship such as 0.99 of $R^2$. Generally, 6.74 L/s of diluted disinfectant is sprayed for a vehicle passing through the disinfection system (about 15 seconds). Test results showed that average error between the measured spraying amount and the flowmeter data was 50 mL, and the range of error was 1.3%. Since the amount and time of spraying could be saved in real-time by using the spreadsheet files which could not be modified arbitrarily, it made possible to judge objectively whether the disinfection spraying was performed or not. Test results of spraying liquid and solid disinfectant showed that the errors between the measured discharge rate and the theoretical one were ranged within 3-4% for various dilution rates. Conclusions: The disinfection system developed would be working accurately. The automated spraying data base management system satisfied the purpose of this study. The automated dilution process system developed in this study could discharge liquid and solid disinfectant with accurate dilution rate, relatively.