• Title/Summary/Keyword: runout control

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Analysis and Design of Diaphragm-type Air Braking System for Train (철도차량의 막판식 공기제동시스템의 해석 및 설계)

  • 노진환;김재도
    • Proceedings of the Korean Society of Precision Engineering Conference
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    • 1997.10a
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    • pp.605-608
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    • 1997
  • In this paper, the case study of reducing rotational errors is done for a grinding spindle with an active magnetic bearing system. The rotational errors acting on the magnetic bearing spindle are due to mass unbalance of rotor, runout, grinding excitation and ed nonlinear dynamics of electromagnets. For the most case, the electrical runout of sensor target is big even in well-finished surface; this runout can cause a rotation error amplified by feedback control system. The adaptive feedforward method based on LMS algorithm is discussed to compensate this kind of runout effects, and investigated its effectiveness by numerical simulation and experimental analysis. The rotor orbit size in both bearings is reduced about to 5 pin due to lX rejection by feedforward control up to 50,000 rpm.

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AN ADVANCED DISTURBANCE REJECTION CONTROL FOR REPEATABLE RUNOUT IN DISK DRIVE SYSTEMS (컴퓨터 하드디스크의 반복 런아웃에서 비롯된 외란의 효율적 제어)

  • 용부중
    • Journal of the Korean Society of Manufacturing Technology Engineers
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    • v.9 no.1
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    • pp.60-67
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    • 2000
  • An improved disturbance rejection control scheme is presented for minimizing the position error due to the repeatable runout disturbances in high density disk drive systems The proposed control algorithm is capable of attenuating repeatable disturbances which is one of the major detractors to hard disk drive quality and performance. This is achieved by a sys-tematic combination of an optimal feedback component and a feedforward preview component. The feedback component is designed where the emphasis is placed on robustness. The feedforward component is on the basis of a preview control comprised of a measured disturbance signals which leads to better disturbance rejection capabilites. The designed con-troller is applied as a plug-in module to a high density hard disk drive with a pre-existing conventional servo controller. Simulations have been carried out to demonstrate the effectiveness of this control scheme in the reduction of the periodic disturbances.

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Investigation of Surface Roughness Characteristics according to Tool Runout Variations in Side Milling Cutter for Worm Screw (사이드 밀링 커터를 이용한 워엄 스크루 가공에서 공구 런아웃이 표면조도에 미치는 영향분석)

  • Kim, Sun Ho
    • Journal of the Korean Society of Manufacturing Process Engineers
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    • v.8 no.4
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    • pp.76-82
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    • 2009
  • A worm screw is widely used in a geared motor unit for motion conversion from rotation to linear motion. For mass production of a high quality worm, the current roll forming process is substituted with the milling cutter process. Since the milling cutter process enables the integration of all machining operations of worm manufacturing on a CNC(Computer Numerical Control) lathe, productivity can be remarkably improved. The tooling system for side milling cutter on the CNC lathe to improve machinability is developed. However, the runout of spindle and cutting tips are important factors to be considered for producing high quality worms because the tooling system has multiple tips. In this study, surface roughness variations accuracy according to runout was investigated in side milling cutter for worm screw. The result shows by simulation and experiment.

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In-Process Cutter Runout Compensation Using Repetitive Learning Control

  • Joon Hwang;Chung, Eui-Sik
    • International Journal of Precision Engineering and Manufacturing
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    • v.4 no.4
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    • pp.13-18
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    • 2003
  • This paper presents the in-process compensation to control cutter ronout and to improve the machined surface quality. Cutter ronout compensation system consists of the micro-positioning servo system with piezoelectric actuator which is embeded in the sliding table to manipulate radial depth of cut in real-time. Cutting force feedback control was proposed in the angle domain based upon repetitive learning control strategy to eliminate chip load variation in end milling process. Micro-positioning control due to adaptive actuation force response improves the machined surface quality by cutter ronout compensation.

The Experimental Study for Variance of Sediment Volume Concentration of Debris Flow due to Damped Structures (감쇠 구조물에 의한 토석류 토사체적 농도 변화에 관한 실험적 연구)

  • Youngdo Choi;Sungduk Kim;Hojin Lee
    • Journal of Korean Society of Disaster and Security
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    • v.16 no.4
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    • pp.1-7
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    • 2023
  • The purpose of this study is an experimental research to investigate the effectiveness of debris flow reduction structures when a debris flow disaster occurs on a steep slope. The control structure for debris flow took the form of baffle, and the soil deposition area and soil runout distance due to debris flow from the downstream were investigated according to the installation number of baffle and each specification. As the slope of the channel became steeper, the sediment deposition area and runout distance increased, and as the sediment volume concentration decreased, the sediment deposition area and runout distance increased. When the sediment concentration was low, differences appeared depending on the slope of the channel because the debris flow had a high liquid content. Overall, the larger the sediment volume concentration, the greater the decrease in sediment deposition area and soil runout distance. As the number of baffles increases, the soil deposition area and runout decrease, showing that the baffles have the ability to control debris flows. The results of this research will provide good information when installing attenuation or control structures when sediment disasters occur in steep slopes.

Track-following Control under Disk Surface Defect of Optical Disk Drive Systems (광디스크 드라이브의 디스크 표면 결함에 대한 트래킹 제어)

  • Jeong, Dong-Seul;Lee, Joon-Seong;Chung, Chung-Choo
    • Transactions of the Society of Information Storage Systems
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    • v.2 no.1
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    • pp.56-64
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    • 2006
  • This paper proposes a new and simple input prediction method for robust servo system. A robust tracking control system for optical disk drives to reject disk runout was recently proposed based on both Coprime Factorization(CF) and Zero Phase Error Tracking(ZPET) control. The CF control system can be designed simply and systematically. Moreover, this system has not only stability but also robustness to parameter uncertainties and disturbance rejection capability. Since optical disk tracking servo systems can detect only racking error, it was proposed that the reference input signal for ZPET could be estimated from tracking errors. In this paper, we propose a new control structure for the ZPET controller. It requires less memory than the previously proposed method for the reference signal generation. Therefore, it is very effective in runout control. Furthermore, this method can be applied to defective optical disk like surface defects on disk. Numerical simulation and experimental result show the proposed method effective.

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Adaptive control of Runout in Active magnetic bearing (능동 자기베어링 런아웃의 적응제어)

  • 김재실;배철용;이재환;안대균;최헌오
    • Proceedings of the Korean Society of Machine Tool Engineers Conference
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    • 2002.04a
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    • pp.333-338
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    • 2002
  • 자기베어링의 회전정밀도에 영향을 미치는 인자로 PWM 전력증폭기, 위치 센서 등과 같은 자기베어링 구성 장치의 동특성 및 정밀도, 시스템의 정확한 모델링, 제어기법, 런아웃 등이 있다. 본 연구에서는 능동 자기베어링을 제어하기 위해 자기베어링의 PWM 전력증폭기와 회전축을 모델링하고 이를 바탕으로 능동 자기베어링 제어를 위한 PID 제어기를 구성하였으며, 변위 센서의 부착위치 및 회전축의 진원도의 영향으로 발생하는 주기적인 런아웃 요소를 첨가하여 런아웃의 영향을 확인하였으며, 런아웃 (Runout)에 의해 발생하는 에러(Error)를 효과적으로 제어하여 자기베어링의 제어 정밀도를 향상시키기 위한 방법으로 기본적인 PID 제어기에 최소평균자승(Least Mean Square, LMS) 알고리즘을 적용한 적응 피드포워드 제어기를 구성하여 자기베어링의 능동 제어에서 발생하는 주기적인 런아웃을 효과적으로 제어할 수 있음을 MATLAB을 통한 시뮬레이션을 통해 확인하였다.

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Identification of Runout. Unbalance and Eddy Current Effect in Active Magnetic Bearing System Using LMS Algorithm (LMS 알고리즘을 이용한 전자기 베어링계에서의 런아웃, 불균형력 및 와전류 효과 규명)

  • 김하용;김승종;이종원
    • Proceedings of the Korean Society for Noise and Vibration Engineering Conference
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    • 2001.05a
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    • pp.172-177
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    • 2001
  • This paper proposes an adaptive feedforward controller (AFC) based on LMS for periodic disturbance rejection in active magnetic bearing system. The proposed controller does not alter the stability and robustness of the existing AMB system. It is shown that the control delay due to the eddy current as well as runout and unbalance can be identified and compensated using the estimated displacement from the measured magnetic flux. The simulation results confirm that the proposed scheme successfully identifies and compensates for the runout, unbalance and eddy current effect, leading to a high-precision magnetic bearing system.

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Influence of Manufacturing Errors on the Dynamic Characteristics of Planetary Gear Systems

  • Cheon, Gill-Jeong;Park, Robert G. er
    • Journal of Mechanical Science and Technology
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    • v.18 no.4
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    • pp.606-621
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    • 2004
  • A dynamic analysis using a hybrid finite element method was performed to characterize the effects of a number of manufacturing errors on bearing forces and critical tooth stress in the elements of a planetary gear system. Some tolerance control guidelines for managing bearing forces and critical stress are deduced from the results. The carrier indexing error for the planet assembly and planet runout error are the most critical factors in reducing the planet bearing force and maximizing load sharing, as well as in reducing the critical stress.

Runout Control of a Magnetically Suspended Grinding Spindle (자기베어링으로 지지된 연삭 스핀들의 런아웃 제어)

  • 노승국;경진호;박종권;최언돈
    • Proceedings of the Korean Society of Precision Engineering Conference
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    • 2000.05a
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    • pp.1011-1015
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    • 2000
  • In this paper, the case studies of reducing rotational errors is theoretically done for a grinding spindle with an active magnetic bearing system. The rotational errors acting on the magnetic bearing spindle are due to mass unbalance of rotor, runout, grinding excitation and unmodeled nonlinear dynamics of electromagnets. The adaptive feedforward method based on LMS algorithm is discussed to compensate output and input disturbances, and investigated its effectiveness by numerical simulation. The feedforward control reduced external excitation and rotational error for specified frequency. The interpolation method using impulse function for cancelling the electrical 'uncut is studied. These methods show their effectiveness for the rotational accuracy of the improving magnetic bearing spindle through some simulation results of the rotational error decreased by them.

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