• Title/Summary/Keyword: reduced-scale laboratory test

Search Result 52, Processing Time 0.019 seconds

Nutrient Recovery from Sludge Fermentation Effluent in Upflow Phosphate Crystallization Process (상향류 인 결정화공정을 이용한 슬러지 발효 유출수로 부터의 영양소 회수)

  • Ahn, Young-Ho
    • Journal of Korean Society of Environmental Engineers
    • /
    • v.28 no.8
    • /
    • pp.866-871
    • /
    • 2006
  • The nutrient recovery in phosphate crystallization process was investigated by using laboratory scale uptlow reactors, adopting sequencing batch type configuration. The industrial waste lime was used as potential cation source with magnesium salt($MgCl_2$) as control. The research was focused on its successful application in a novel integrated sludge treatment process, which is comprised of a high performance fermenter followed by a crystallization reactor. In the struvite precipitation test using synthetic wastewater first, which has the similar characteristics with the real fermentation effluent, the considerable nutrient removal(about 60%) in both ammonia and phosphate was observed within $0.5{\sim}1$ hr of retention time. The results also revealed that a minor amount(<5%) of ammonia stripping naturally occurred due to the alkaline(pH 9) characteristic in feed substrate. Stripping of $CO_2$ by air did not increase the struvite precipitation rate but it led to increased ammonia removal. In the second experiment using the fermentation effluent, the optimal dosage of magnesium salt for struvite precipitation was 0.86 g Mg $g^{-1}$ P, similar to the mass ratio of the struvite. The optimal dosage of waste lime was 0.3 g $L^{-1}$, resulting in 80% of $NH_4-N$ and 41% of $PO_4-P$ removal, at about 3 hrs of retention time. In the microscopic analysis, amorphous crystals were mainly observed in the settled solids with waste lime but prism-like crystals were observed with magnesium salt. Based on mass balance analysis for an integrated sludge treatment process(fermenter followed by crystallization reactor) for full-scale application(treatment capacity Q=158,880 $m^3\;d^{-1}$), nutrient recycle loading from the crystallization reactor effluent to the main liquid stream would be significantly reduced(0.13 g N and 0.19 g P per $m^3$ of wastewater, respectively). The results of the experiment reveal therefore that the reuse of waste lime, already an industrial waste, in a nutrient recovery system has various advantages such as higher economical benefits and sustainable treatment of the industrial waste.

Material and Behavior Characteristics of Lightweight Embankment for Road Constructed on Soft Ground (연약지반에 시공된 도로용 경량성토체의 재료 및 거동특성)

  • Yea, Geu-Guwen;Lee, Yong-Jae;Kim, Hong-Yeon;Yoon, Gil-Lim;Han, Sang-Hyun
    • Journal of the Korean Geosynthetics Society
    • /
    • v.17 no.2
    • /
    • pp.41-49
    • /
    • 2018
  • The purpose of this study is to fabricate a full scale road embankment using lightweight air foamed soil as a soil material on soft ground and to investigate its material characteristics and behavior in order to promote dredged soil utilization and minimize ground improvement. As a result of the laboratory test of the onsite mixed samples, the total unit weight of the specimens decreased almost linearly until curing 28 days. In particular, the total unit weight after 28 days of curing was reduced to about 81% of the slurry state before curing, which will be useful in the formulation of similar native soil materials in the future. The unconfined compressive strength began to decrease with the 14th day of curing as shown in the previous study. When the cement content is increased, the strength decreases sharply at a small strain change after the occurrence of the maximum compressive strength, and the maximum strength is exhibited in a range of a smaller axial strain than normal range. The settlement at the surface layer of the ground due to the lightweight embankment was about 1 / 2.75 of the soil embankment and was in agreement with the unit weight ratio (1 / 2.7) of the embankment materials. This indicates the cause and effect of the settlement due to the difference in self weight of the embankments. Also, the difference in settlement between soil and lightweight embankment increased with increasing depth. This shows that the difference in the point at which the settlement is terminated is clear. The ground horizontal displacement under the lightweight embankment was about 15~20% smaller than that of the soil embankment and the depth of occurrence was also 4.5~5.0m shallower in the lightweight embankment.