• Title/Summary/Keyword: increments

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Pilot-scale Applications of a Well-type Reactive Barrier using Autotrophic Sulfur-oxidizers for Nitrate Removal (독립영양 황탈질 미생물을 이용한 관정형 반응벽체의 현장적용성 연구)

  • Lee, Byung-Sun;Um, Jae-Yeon;Lee, Kyu-Yeon;Moon, Hee-Sun;Kim, Yang-Bin;Woo, Nam-C.;Lee, Jong-Min;Nam, Kyoung-Phile
    • Journal of Soil and Groundwater Environment
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    • v.14 no.3
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    • pp.40-46
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    • 2009
  • The applicability of a well-type autotrophic sulfur-oxidizing reactive barrier (L $\times$ W $\times$ D = $3m\;{\times}\;4\;m\;{\times}\;2\;m$) as a long-term treatment option for nitrate removal in groundwater was evaluated. Pilot-scale (L $\times$ W $\times$ D = $8m\;{\times}\;4\;m\;{\times}\;2\;m$) flow-tank experiments were conducted to examine remedial efficacy of the well-type reactive barrier. A total of 80 kg sulfur granules as an electron donor and Thiobacillus denitrificans as an active bacterial species were prepared. Thiobacillus denitrificans was successfully colonized on the surface of the sulfur granules and the microflora transformed nitrate with removal efficiency of ~12% (0.07 mM) for 11 days, ~24% (1.3 mM) for 18 days, ~45% (2.4 mM) for 32 days, and ~52% (2.8 mM) for 60 days. Sulfur granules attached to Thiobacillus denitrificans were used to construct the well-type reactive barrier comprising three discrete barriers installed at 1-m interval downstream. Average initial nitrate concentrations were 181 mg/L for the first 28 days and 281 mg/L for the next 14 days. For the 181 mg/L (2.9 mM) plume, nitrate concentrations decreased by ~2% (0.06 mM), ~9% (0.27 mM), and ~15% (0.44 mM) after $1^{st}$, $2^{nd}$, and $3^{rd}$ barriers, respectively. For the 281 mg/L (4.5 mM) plume, nitrate concentrations decreased by ~1% (0.02 mM), ~6% (0.27 mM), and ~8% (0.37 mM) after $1^{st}$, $2^{nd}$, and $3^{rd}$ barriers, respectively. Nitrate plume was flowed through the flow-tank for 49 days by supplying $1.24\;m^3/d$ of nitrate solution. During nitrate treatment, flow velocity (0.44 m/d), pH (6.7 to 8.3), and DO (0.9~2.8 mg/L) showed little variations. Incomplete destruction of nitrate plume was attributed to the lack of retention time, rarely transverse dispersion, and inhibiting the activity of denitrification enzymes caused by relatively high DO concentrations. For field applications, it should be considered increments of retention time, modification of well placements, and intrinsic DO concentration.

Clinical Impact of Bronchial Reactivity and Its Relationship with Changes of Pulmonary Function After Asthmatic Attack Induced by Methacholine (기관지 반응성의 임상적 의의 및 메타콜린으로 유도된 천식 발작시 폐기능 변화와의 관계)

  • Ryu, Yon-Ju;Choi, Young-Ju;Kwak, Jae-Jin;Lee, Ji-A;Nam, Seung-Hyun;Park, Chang-Han;Chaon, Saon-Hee
    • Tuberculosis and Respiratory Diseases
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    • v.52 no.1
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    • pp.24-36
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    • 2002
  • Background: Bronchial reactivity is known to be a component of airway hyperresponsiveness, a cardinal feature of asthma, with bronchial sensitivity, and is increments in response to induced doses of bronchoconstrictors as manifested by the steepest slope of the dose-response curve. However, there is some controversy regarding methods of measuring bronchial reactivity and clinical impact of such measurements. The purpose of this study was to evaluate the clinical significance and assess the clinical use by analyzing the relationship of the bronchial sensitivity, the clinical severity and the changes in pulmonary function with bronchial reactivity. Method: A total of 116 subjects underwent a methacholine bronchial provocation test. They were divided into 3 groups : mild intermittent, mild persistent, moderate and cough asthma. Severe patients were excluded. Methacholine PC20 was determined from the log dose-response curve and PC40 was determined by one more dose inhalation after PC20. The steepest slope of log dose-response curve, connecting PC20 with PC40, was used to calculate the bronchial reactivity. Body plethysmography and a single breath for the DLCO were done in 43 subjects before and after methacholine test. Results: The average bronchial reactivity was 38.0 in the mild intermittent group, 49.8 in the mild persistent group, 61.0 in the moderate group, and 41.1 in the cough asthma group. There was a weak negative correlation between PC20 and bronchial reactivity. A heightened bronchial reactivity tends to produce an increased clinical severity in patients with a similar bronchial sensitivity and basal spirometric pulmonary function. There were significant correlations between the bronchial reactivity and the initial pulmonary function before the methacholine test in the order of sGaw, Raw, $FEV_1$/FVC, MMFR. There were no correlations between the bronchial sensitivity and the % change in the pulmonary function parameters after the methacholine test. However, there were significant correlations between the bronchial reactivity and the PEF, $FEV_1$, DLCO. Conclusion: There was weak significant negative correlation between the bronchial reactivity and the bronchial sensitivity, and the bronchial reactivity closely reflected the severity of the asthma. Accordingly, measuring both the bronchial sensitivity and the bronchial reactivity can be of assistance in assessing of the ongoing disease severity and in monitoring the effect of therapy.