The purpose of this paper is to analyze the behavior and to study the safety evaluation of the Unmun Dam located in Cheongdo-Gun of GyeongBuk Province, Korea. For this purpose, soil analyses including boring data, geophysical surveys and monitoring the buried geotechnical gauges, such as pore-pressure gauge, earth-pressure gauge, displacement gauge, multi-layer settlement gauge, leakage flow-meter, were conducted.
In addition to these data, numerical analyses of behavior of dam were performed to predict and to compare the data which were obtained from the above methods. Since many defects, such as gravel and weathered rock blocks in the dam core, and lots of amounts of leakage, by boring analyses were found, reinforcement by compaction grouting system (CGS) has been conducted in some range of dam. Some geotechnical gauge data were also used to confirm the effects of reinforcement. Analyses of monitoring the data of geotechnical gauges buried in the dam, such as pore-pressure gauge, earth-pressure gauge, displacement gauge, multi-layer settlement gauge, and leakage flow-meter shows the load transfer of dam and the possibility of hydraulic
fracturing. As a conclusion, some problems in the dam found. Especially, the dam near spillway shows the high possibility of leakage. It should be pointed out that only the left side of he dam has not a leakage problem. As a whole, the dam has problems of weakness, because of unsatisfactory construction. It is strongly recommended that highly intensive monitoring is required.
Journal of Korean Tunnelling and Underground Space Association
/
v.8
no.1
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pp.3-12
/
2006
The purpose of this study is to describe the Non-Destructive Testing(NDT) of the rockbolt and investigate the applicability of the NDT methods to estimate the integrity of the rockbolt. To examine the rockbolt integrity including rockbolt itself and grouting material, two methods are adopted: numerical and experimental methods. In the numerical method, the numerical code DISPERSE is used to analyze the dispersion of the rockbolt. The dispersion curve shows the effects of the thickness and stiffness of grouted materials on the embedded rockbolt. Therefore, the optimal frequency for the integrity test of the rockbolt is obtained: 20~120kHz in L(1,0) mode. In the experimental methods, destructive and non-destructive tests are carried out in a laboratory. In the non-destructive test, the low frequency mode generated by an impact and t he high frequency mode generated by an ultrasonic transducer seem to characterize the rockbolt condition readily. The experimental results show that the guided waves attenuate more significantly when the stiffness of the grouted material increases and/or the zone of the defect increases. Meanwhile, the ultimate capacity of rockbolt was evaluated through the pull-out tests and is compared to the NDT results. This study demonstrates that the NDT is a valuable tool for the rockbolt integrity evaluation.
A calcareous rock slope failed during excavation of the slope for construction of a tunnel entrance. The slope is located at the construction site for widening highway in Yeongwol, Korea. Field surveys, laboratory tests, and numerical analyses were performed to determine the reason for the slope failure. The numerical analysis revealed that the safety factor of the slope before construction of the entrance was less than 1, and that this decreased after construction. After construction of the entrance, the sliding zone of the slope increased and slope stability decreased because the shear strain and plastic zone in the slope over the tunnel entrance showed an increase relative to the lower part of the slope. To enhance the stability of the slope for construction of the tunnel entrance, countermeasures such as rock bolts, rock anchors, and FRP (Fiber glass Reinforced Plastic) grouting were adopted in light of the field conditions. Serial field monitoring performed to confirm the reinforcing effects of the adopted countermeasures revealed a small amount of horizontal deformation of the slope soils, most of the elastic deformation that can regain its former value. In addition, the axial forces of the rock bolt and anchor were more strongly affected by slope excavation during construction of the tunnel entrance than by tunnel excavation or the rainy season, and the axial forces tended to converge after excavation of the tunnel. Therefore, we can confirm that the slope is currently safe.
The corrosion rate measurement procedure for the permanent ground anchors using polarization resistance measurements and electrochemical impedance spectroscopy is presented in this paper. The polarization resistance measurements were used to determine the correlation between corrosion rate in the steel and soil characteristics. The electrochemical impedance spectroscopy was used to predict the time dependent corrosion reaction and evaluate the different type of coating systems and the effect of cement grouting on the corrosion attack under various conditions. The results indicate that a low pH soil is a good indicator of a corrosive soil. The low pH soil condition (<5) in both clay and sand has a significant effect on the corrosion reaction of steel members in permanent found anchors. In the case of neutral and alkaline conditions beyond pH 6 in clay and sand, no consistent acceleration of corrosion was measured and the corrosion rate was constant regardless of variations of soil pH levels. Laboratory test data for porcelain clay indicate that the change of soil pH level has a small influence on the corrosion reaction in the steel member. The use of cement footing in the bonded length is sufficient to decrease the corrosion rate to a level close to 0.003∼0.01mm/y at the end of the given period. With epoxy and fusion bonded epoxy coating, the steel specimens remained unaffected and retained the original condition. It is suggested that epoxy and fusion bonded epoxy coating can provide effective protection against corrosion for a long time even in aggressive environment.
Journal of Korean Tunnelling and Underground Space Association
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v.11
no.2
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pp.131-140
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2009
It has been repeatedly reported that a drainage system of a drained tunnel is deteriorated. And consequently the water pressure on the lining increases with time. However, little research on the watertight tunnel was found in the literatures. According to field measurements, leakage of the undrained tunnel has increased with time, which is completely opposite to the behavior of the drained tunnel. It is evident that the hydraulic deterioration of the tunnel lining changes the water pressure on the lining and the amount of leakage, thus the design coneept in terms of groundwater is not maintained tightly throughout the life time of the tunnel. The Segment lining is generally constructed as watertight. However, it is frequently reported that the leakage in the segment tunnel increases with time. It is also reported that the leakage is generally concentrated at the joints of the segments. In this study structural and hydraulic interaetion of the segment lining due to the hydraulic deterioration of the segments and the joints is investigated using the numerical modeling method. An electric utility tunnel below groundwater table is considered for the analyses. The effects of hydraulic deterioration of the segment lining are identified in terms of ground loading, water pressure and lining behavior. A remedial grouting measure for leakage is also numerically simulated, and its appropriateness is evaluated.
Currently, a grouting method that minimizes damage to the reservoir embankment by injecting solidification agent at low pressure is commonly used to ensure waterproofing and safety of the embankment, but the use of solidification agents can cause issues, such as a decrease in durability and a lack of clear method for determining the mixing ratio. In this study, when the base ground and solidification agent were stirred and mixed at various weight mixing ratios, the permeability coefficient and strength of the mixture were confirmed through laboratory tests, and the optimal mixing ratio was suggested through analysis of the test results. The specimen for the laboratory test was produced considering the mixing ratio of the solidification agent. The specimen for the permeability coefficient test was tested by producing one each of cohesionless and cohesive soil for a mixing amount of 1.5 kN/m3 of solidification agent, and the permeability test results confirmed that the water barrier performance was secured below the permeability coefficient value required by various design criteria. A total of 24 specimens for the strength test were produced, 3 for each of 5 mixing amounts for cohesive soil and 3 mixing amounts for cohesionless soil. The strength test results showed that the uniaxial compressive strength tends to increase linearly with increasing curing time for both cohesionless soil and cohesive soil when the mixing amount is less than 2.0 kN/m3. Therefore, the optimal mixing ratio applied to the site is determined to be mixing amount of 1.5 kN/m3 and 2.0 kN/m3. Finally, numerical analysis reflecting test results was conducted on design case for improvement projects for aging reservoirs embankment to verify the water barrier performance and safety improvement effects.
A spiting reinforcement system is composed of a series of radially installed reinforcing spites along the perimeter of the tunnel opening ahead of excavation. The reinforcing spill network is extended into the in-situ soil mass both radially and longitudinally The sailing reinforcement system has been successfully used for the construction of underground openings to reinforce weak rock formations on several occasions. The application of this spiting reinforcement system is currently extended to soft ground tunneling in limited occasions because of lack of reliable analysis and design methods. A method of threetimensional limit equilibrium stability analysis of the smile-reinforced shallow tunnel in soft ground is presented. The shape of the potential failure wedge for the case of smile-reinforced shallow tunnel is assumed on the basis of the results of three dimensional finite element analyses. A criterion to differentiate the spill-reinforced shallow tunnel from the smile-reinforced deep tunnel is also formulated, where the tunnel depth, soil type, geometry of the tunnel and reinforcing spites, together with soil arching effects, are considered. To examine the suitability of the proposed method of threedimensional stability analysis in practice, overall stability of the spill-reinforced shallow tunnel at facing is evaluated, and the predicted safety factors are compared with results from twotimensional analyses. Using the proposed method of threetimensional limit equilibrium stability analysis of the smile-reinforced shallow tunnel in soft ground, a parametric study is also made to investigate the effects of various design parameters such as tunnel depth, smile length and wadial spill spacing. With slight modifications the analytical method of threeiimensional stability analysis proposed may also be extended for the analysis and design of steel pipe reinforced multi -step grouting technique frequently used as a supplementary reinforcing method in soft ground tunnel construction.
In this study to improve stability, workability and economics of the H-Pile+Earth plate or H-Pile+Earth plate+Cutoff grouting currently in use, we had developed HCS method belonging to the retaining wall which is consisting of a combination H-Pile, Plastic Sheet Pile and Steel Square Pipe for gap maintenance and reinforcement of flexible plastic Sheet Pile, and the behavior of each member composing HCS method is investigated by three-dimensional finite element analysis. To numerically analyze the behavior of the HCS method, we have performed extensive three-dimentional finite element analysis for three kinds of plastic Sheet Pile size, two kinds of H-Pile size and three kinds of H-Pile installation interval, one kinds of Steel Square Pipe and three kinds of Steel Square Pipe installation interval. After analyzing the numerical results, we found that the combinations of $P.S.P-460{\times}131.5{\times}7t$ (PS7) and H-Pile $250{\times}250{\times}9{\times}14$ (H250), $P.S.P473{\times}133.5{\times}9t$ (PS9) and H-Pile $300{\times}200{\times}9{\times}14$ (H300) is the most economical because these combinations are considered to have a stress ratio (=applied stress/allowable stress) close to that as the stiffness of H-Pile, plastic Sheet Pile and Steel Square Pipe composite increased, the horizontal displacement of the retaining wall and the vertical displacement of the upper ground decreased. Especially, due to the arching effects caused by the difference in stiffness between H-Pile and plastic Sheet Pile, a large part of the earth pressure acting on plastic Sheet Pile caused a stress transfer to H-Pile, and the stress and displacement of plastic Sheet Pile were small. Through this study, we can confirm the behavior of each member constituting the HCS method, and based on the confirmed results of this study, it can be used to apply HCS method in reasonable, stable and economical way in the future.
Journal of Korean Tunnelling and Underground Space Association
/
v.15
no.3
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pp.187-199
/
2013
Umbrella arch method (UAM) used for improving the stability of the tunnel ground condition has been widely applied in the tunnel construction projects due to the advantage of obtaining both reinforcement and waterproof. The purpose of this study is to develop the evaluation technique of the integrity of bore-hole in UAM by using a non-destructive test and to evaluate the possibility of being applied to the field. In order to investigate the variations of frequency depending on grouted length, the specimens with different grouted ratios are made in the two constraint conditions (free boundary condition and embedded condition). The hammer impact reflection method in which excitation and reception occur simultaneously at the head of pipe was used. The guided waves generated by hitting a pipe with a hammer were reflected at the tip and returned to the head, and the signals were received by an acoustic emission (AE) sensor installed at the head. For the laboratory experiments, the specimens were prepared with different grouted ratios (25 %, 50 %, 75 %, 100 %). In addition, field tests were performed for the application of the evaluation technique. Fast Fourier transform and wavelet transform were applied to analyze the measured waves. The experimental studies show that grouted ratio has little effects on the velocities of guided waves. Main frequencies of reflected waves tend to decrease with an increase in the grouted length in the time-frequency domain. This study suggests that the non-destructive tests using guided ultrasonic waves be effective to evaluate the bore-hole integrity of the UAM in the field.
Journal of Korean Tunnelling and Underground Space Association
/
v.13
no.4
/
pp.347-370
/
2011
Slurry type shield would be very effective for the tunnelling in a sandy ground, when the slurry pressure would be properly adjusted. Low slurry pressure could cause a tunnel face failure or a ground settlement in front of the tunnel face. Thus, the stability of tunnel face could be maintained by applying an excess slurry pressure that is larger than the active earth pressure. However, the slurry pressure should increase properly because an excessively high slurry pressure could cause the slurry flow out or the passive failure of the frontal ground. It is possible to apply the high slurry pressure without passive failure if a horizontal impermeable layer is located in the ground in front of the tunnel face, but its location, size, and effects are not clearly known yet. In this research, two-dimensional model tests were carried out in order to find out the effect of a horizontal impermeable layer for the slurry shield tunnelling in a saturated sandy ground. In tests slurry pressure was increased until the slurry flowed out of the ground surface or the ground fails. Location and dimension of the impermeable layer were varied. As results, the maximum and the excess slurry pressure in sandy ground were linearly proportional to the cover depth. Larger slurry pressure could be applied to increase the stability of the tunnel face when the impermeable layer was located in the ground above the crown in front of the tunnel face. The most effective length of the impermeable grouting layer was 1.0 ~ 1.5D, and the location was 1.0D above the crown level. The safety factor could be suggested as the ratio of the maximum slurry pressure to the active earth pressure at the tunnel face. It could also be suggested that the slurry pressure in the magnitude of 3.5 ~4.0 times larger than the active earth pressure at the initial tunnel face could be applied if the impermeable layer was constructed at the optimal location.
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