• 제목/요약/키워드: conditions of secondary air injection

검색결과 18건 처리시간 0.022초

가스터빈 연소기내 2차연료분사에 의한 연소 불안정성의 제어 (Control of Combustion Instabilities in a Gas Turbine Combustors Through Secondary Fuel Injection)

  • 전충환
    • 한국연소학회지
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    • 제3권1호
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    • pp.59-69
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    • 1998
  • The results of study on the active control of naturally occurring combustion oscillations with a single dominant frequency in an atmospheric dump combustor are presented. Control was achieved by an oscillatory infection of secondary fuel at the dump plane. A high speed solenoid valve with a maximum frequency of 250Hz was used as the actuator and a sound level meter, located at the combustor exit, measured the pressure fluctuations which served as the feedback signal for the control loop. Instability characteristics were mapped over a range of mean mixing section velocities from 6.7 m/s-9.3 m/s and with three mixing conditions. Different fuel/air mixing conditions were investigated by introducing varying percentages of primary fuel at two locations, one at the entrance to the mixing section and one 6 mixing tube diameters upstream of the dump plane. Control studies were conducted at a mean velocity of 9.3 m/s, with an air temperature of $415^{\circ}C$, and from flame blowout to the stoichiometric condition.

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Emissions in lean-lean two-stage combustion using premixed tubular flames

  • Takagi, Hideyuki;Hayashi, Shigeru;Yamada, Hideshi;Kawakami, Tadashige
    • 한국추진공학회:학술대회논문집
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    • 한국추진공학회 2004년도 제22회 춘계학술대회논문집
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    • pp.466-471
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    • 2004
  • In gas turbines, excess air for combustion is available and therefore lean premixed combustion is the most promising approach to the significant reduction of thermal NOx emissions. At lean conditions, however, flame stability is inherently worse and hence combustion tends to be incomplete. Efforts have been devoted toward extending the operating range of complete combustion at leaner conditions. One of them is the lean-lean two-stage combustion where lean to ultra-lean secondary mixtures are mixed with the hot burned gas from the primary stage. Conventional flame combustion or flameless reaction are initiated depending on the conditions of the secondary zone. In the first part of the present study, the effects of fuel injection on the emissions and flame stability were investigated for a single tubular flame, In the second part, the emissions and flame stability were studied for a two-stage combustor with secondary mixture injected through the tangential slots on a cylindrical combustor wall. The effects of the ratio of air flow rates to the primary and secondary zones on the emissions and combustion characteristics were investigate.

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연소실 압력변동이 스월 화염에서 화염 안정화와 NOx 배출에 미치는 영향 (Influence of changing combustor pressure on flame stabilization and NOx emission in swirl flame)

  • 김종률;최경민;김덕줄
    • 유체기계공업학회:학술대회논문집
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    • 유체기계공업학회 2006년 제4회 한국유체공학학술대회 논문집
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    • pp.569-572
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    • 2006
  • In present study, the influence of changing combustor pressure on flame stabilization and nitrogen oxide (NOX) emission in the swirl flame with secondary fuel injection was investigated. The combustor pressure was controlled by suction at combustor exit. Pressure index ($P^*=Pabs/Patm$), where Pabs and Patm indicated the absolute pressure and atmosphere pressure, was controlled in the range of 0.7~1.15 for each equivalence ratio conditions. It could be observed that flame stable region became narrower with decreasing equivalence ratio and pressure index. In this combustion system, stable flames were formed until $P^*=\;0.7$. Emission index decreased with decreasing pressure index for overall equivalence ratio conditions and NOx reduction rates were almost identical for $P^*<1$ regardless of equivalence ratio though EINOx values showed different level with change of equivalence ratio for $P^*{\geq}1$. It is also observed that EINOx decreased with increasing secondary fuel injection ratio. Emission index of nitric oxide was controllable by adjusting the changing combustor pressure and injecting secondary fuel and this NOx reduction technology is applicable to industrial furnaces and air conditioning system.

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이코노마이저를 채용한 스크류 냉동기에서 R22와 R407C의 부분부하 성능실험 (Part-Load Performance Test of a Screw Chiller with Economizer using R22 and R407C)

  • 장영수;이용철;김영일
    • 설비공학논문집
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    • 제15권11호
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    • pp.902-909
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    • 2003
  • Screw compressor type chillers are widely used in refrigeration for capacity over 30 RT. In general, chillers operate under part-load conditions. Therefore, information on characteristics at part-load is very important in view of chiller performance and energy economy. In this study, performance tests of part-load and economizer system using R22 and R407C have been performed for various secondary fluid temperatures. Adoption of an economizer system increased the cooling capacity and improved COP except for lower part-load condition when injection volume ratio is 1.01. For the same cooling capacity condition at part-load, COP of both non-economizer and economizer system showed similar values.

DIESEL ENGINE NOx REDUCTION BY SNCR UNDER SIMULATED FLOW REACTOR CONDITIONS

  • Nam, Chang-Mo;Kwon, Gi-Hong;Mok, Young-Sun
    • Environmental Engineering Research
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    • 제11권3호
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    • pp.149-155
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    • 2006
  • NOx reduction experiments were conducted by direct injection of urea into a diesel fueled, combustion-driven flow reactor which simulated a single engine cylinder ($966cm^3$). NOx reduction tests were carried out over a wide range of air/fuel ratios (A/F=20-40) using an initial NOx level of 530ppm, and for normalized stoichiometric ratios of reductant to NOx (NSR) of 1.5 to 4.0. The results show that effective NOx reduction with urea occurred over an injection temperature range of 1100 to 1350K. NOx reduction increased with increasing NSR values, and about a 40%-60% reduction of NOx was achieved with NSR=1.5-4.0. Most of the NOx reduction occurred within the cylinder and head section (residence time <40msec), since temperatures in the exhaust pipe were too low for additional NOx reduction. Relatively low NOx reduction is believed to be due to the existence of higher levels of CO and unburned hydrocarbons (UHC)inside the cylinder, and large temperature drops along the reactor. Injection of secondary combustible additives (diesel fuel/$C_2H_6$) into the exhaust pipe promoted further substantial NOx reduction (5%-30%) without shifting the temperature windows. Diesel fuel was found to enhance NOx reduction more than $C_2H_6$, and finally practical implications are further discussed.

공동이 있는 수직 분사 초음속 연소기 내의 불안정 연소유동 해석 (Numerical Analysis of Unstable Combustion Flows in Normal Injection Supersonic Combustor with a Cavity)

  • Jeong-Yeol Choi;Vigor Yang
    • 한국추진공학회:학술대회논문집
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    • 한국추진공학회 2003년도 제20회 춘계학술대회 논문집
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    • pp.91-93
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    • 2003
  • A comprehensive numerical study is carried out to investigate for the understanding of the flow evolution and flame development in a supersonic combustor with normal injection of ncumally injecting hydrogen in airsupersonic flows. The formulation treats the complete conservation equations of mass, momentum, energy, and species concentration for a multi-component chemically reacting system. For the numerical simulation of supersonic combustion, multi-species Navier-Stokes equations and detailed chemistry of H2-Air is considered. It also accommodates a finite-rate chemical kinetics mechanism of hydrogen-air combustion GRI-Mech. 2.11[1], which consists of nine species and twenty-five reaction steps. Turbulence closure is achieved by means of a k-two-equation model (2). The governing equations are spatially discretized using a finite-volume approach, and temporally integrated by means of a second-order accurate implicit scheme (3-5).The supersonic combustor consists of a flat channel of 10 cm height and a fuel-injection slit of 0.1 cm width located at 10 cm downstream of the inlet. A cavity of 5 cm height and 20 cm width is installed at 15 cm downstream of the injection slit. A total of 936160 grids are used for the main-combustor flow passage, and 159161 grids for the cavity. The grids are clustered in the flow direction near the fuel injector and cavity, as well as in the vertical direction near the bottom wall. The no-slip and adiabatic conditions are assumed throughout the entire wall boundary. As a specific example, the inflow Mach number is assumed to be 3, and the temperature and pressure are 600 K and 0.1 MPa, respectively. Gaseous hydrogen at a temperature of 151.5 K is injected normal to the wall from a choked injector.A series of calculations were carried out by varying the fuel injection pressure from 0.5 to 1.5MPa. This amounts to changing the fuel mass flow rate or the overall equivalence ratio for different operating regimes. Figure 1 shows the instantaneous temperature fields in the supersonic combustor at four different conditions. The dark blue region represents the hot burned gases. At the fuel injection pressure of 0.5 MPa, the flame is stably anchored, but the flow field exhibits a high-amplitude oscillation. At the fuel injection pressure of 1.0 MPa, the Mach reflection occurs ahead of the injector. The interaction between the incoming air and the injection flow becomes much more complex, and the fuel/air mixing is strongly enhanced. The Mach reflection oscillates and results in a strong fluctuation in the combustor wall pressure. At the fuel injection pressure of 1.5MPa, the flow inside the combustor becomes nearly choked and the Mach reflection is displaced forward. The leading shock wave moves slowly toward the inlet, and eventually causes the combustor-upstart due to the thermal choking. The cavity appears to play a secondary role in driving the flow unsteadiness, in spite of its influence on the fuel/air mixing and flame evolution. Further investigation is necessary on this issue. The present study features detailed resolution of the flow and flame dynamics in the combustor, which was not typically available in most of the previous works. In particular, the oscillatory flow characteristics are captured at a scale sufficient to identify the underlying physical mechanisms. Much of the flow unsteadiness is not related to the cavity, but rather to the intrinsic unsteadiness in the flowfield, as also shown experimentally by Ben-Yakar et al. [6], The interactions between the unsteady flow and flame evolution may cause a large excursion of flow oscillation. The work appears to be the first of its kind in the numerical study of combustion oscillations in a supersonic combustor, although a similar phenomenon was previously reported experimentally. A more comprehensive discussion will be given in the final paper presented at the colloquium.

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연소로 열유동 해석 방식과 결과 분석에 대한 고찰;화격자식 소각로의 사례 (Discussion on the Practical Use of CFD for Furnaces;A Case of Grate Type Waste Incinerators)

  • 류창국;최상민
    • 한국연소학회:학술대회논문집
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    • 한국연소학회 2002년도 제24회 KOSCO SYMPOSIUM 논문집
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    • pp.85-94
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    • 2002
  • Computational flow dynamics(CFD) has been frequently applied to the waste incinerators to understand the flow performance for various design and operating parameters. Though it needs many simplifications and complicated flow models, the reasonability of its results is not fully evaluated. For example, the inlet condition is calculated from an arbitrarily assumed properties of combustion gas release from the waste bed, since the combustion in the bed is difficult to be predicted. In this study, the computational modeling and calculation procedures of CFD for the grate type waste incinerator were evaluated using comparative simulations. Though the assumption method on the generation of the combustion gas directly affected the temperature and gas species concentrations, the overall flow pattern was dominated by the secondary air jets. The gaseous reaction could be included by assuming the release of the products of incomplete combusion from the bed. However, the reaction effficiency cannot not be directly evaluated from the species concentration, since it is not possible to simulate the actual co-existence of fuel rich or oxygen rich puffs over the bed. In predicting the turbulence, the higher order model, such as Reynolds stress model, gave difference shape of local recirculation zones, but similar results was acquired from the standard $k-{\varepsilon}$ model. Introducing radiation model was required for accurate temperature prediction, but it also caused heat imbalance due to the fixed temperature of the inlet, i.e. the waste bed. Thus, the computational modeling procedures on incinerators and the analysis of the predicted results should be progressed carefully. Though not validated experimentally, current simulation method is capable of comparative evaluation on the flow-related parameters such as the furnace shape and secondary air injection using identical inlet conditions. Quantitative analysis using measures of the residence time and mixing is essential to compare the flow performance efficiently.

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경유 화염에서 왕겨를 이용한 바이오매스 재연소의 NOx 저감 효과 (The Effect of Biomass Reburning with Rice Husk on NOx Reduction in Light Oil Flame)

  • 김세원;신명철;이창엽
    • 한국연소학회지
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    • 제14권4호
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    • pp.17-24
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    • 2009
  • Reburning is one of the most useful technologies for reducing nitric oxide in economically and technically. The reburning process was demonstrated as an effective NOx reduction method through injection of a secondary hydrocarbon fuel. An experimental study has been conducted to evaluate the effect of biomass reburning on NOx and CO formation in a light oil flamed combustion furnace. Reburning tests on NOx reduction of air-carried rice husk powder as the reburn fuel and light oil as the main fuel were performed in flames stabilized by a co-flow swirl and fuel staged burner, which was mounted at the front of the furnace. The results included flue gas emissions and temperature distribution in the furnace for several kinds of experimental conditions. It was observed clearly that NOx concentrations in the exhaust have considerably decreased due to effect of biomass reburning. The maximum NOx reduction rate was 42% when the reburn fuel fraction was 0.18. The CO emissions were kept under 42 ppmv in all experimental tests. And this paper makes clear that in order to decrease NOx concentration in the exhaust when the biomass reburning system is adapted, the control of some factors such as reburn fuel fraction and reburn zone fraction is very important.

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