• 제목/요약/키워드: casting defect

검색결과 102건 처리시간 0.021초

압전방식초음파치석제거기의작업조건에따른치과주조용합금의삭제결손부 양상에 관한 고찰 (A morphologic evaluation of defects created by a piezoelectric ultrasonic scaler on casting gold alloy)

  • 김영성;김수환;김원경;이영규
    • Journal of Periodontal and Implant Science
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    • 제39권4호
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    • pp.385-390
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    • 2009
  • Purpose: In this study we evaluated the morphologic aspects of defects created by a piezoelectric ultrasonic scaler with scaler tip on casting gold alloy using scanning electron microscope (SEM) images and defect surface profiles. Methods: 54 blocks of type III casting gold alloy (Firmilay, Jellenko Inc, CA, USA) were scaled by a piezoelectric ultrasonic scaler (P-MAX, Satelec, France) with scaler tip (No. 1 tip) on a sledge device. 2-dimensional profiles of defects on all samples were investigated by a surface profilometer (a-Step 500, KLA-Tencor, CA, USA). The selected working parameters were lateral force (0.5 N, 1.0 N, 2.0 N), mode (P mode, S mode), and power setting (2, 4, 8). SEM images were obtained. Defect surface profiles were made on Microsoft Excel program using data obtained by a surface profilometer. Results: Among P mode samples, there were similarities on defect surface profiles and SEM images regardless of lateral force. The defects created in P mode were narrow and shallow although the depth and the width increased as power setting changed low (2) to high (8). In P mode samples, the defect depth was the greatest when lateral force of 0.5 N was applied. However all the depths were smaller than 1 m. SEM images of Lateral force of 0.5 N, S mode, power setting 2 and 4 were similar to that of P mode, but the other SEM images of S mode showed discernible changes. Defect depth of S mode samples was the greatest when lateral force of 1.0 N was applied. Conclusions: Within the limitations of this study, it can be concoluded that removing capability of piezoelectric scaler with scaler tip becomes maximized as power level becomes higher but the capability is restricted when excessive lateral force is applied on scaler tip.

주조조건에 따른 순티타늄의 주조성 분석 (Analysis of castability in c.p.Ti according to casting conditions)

  • 황성식;권순석
    • 대한치과기공학회지
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    • 제29권1호
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    • pp.133-138
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    • 2007
  • In this study, the castability and of commercially pure titanium(c.p.Ti) grade according to the casting condition which are the vacuum condition in casting machine and mold temperature of investment, was investigated. Argon-arc melt/centrifugal casting machine was used for casting the specimens. The microstructure and mechanical properties were evaluated by using optical microscope. The results were as follows; 1. It could make a sure that there's relatively not much defect of casting body of c.p.Ti according to the deference of air pressure. 2. It could make sure that it formed porosity on the surface inside of the casting body of c.p.Ti according to deferent temperature. and on excellent castability was below $200^{\circ}C$ 3. As the mold temperature of investment was increased, the lamellar structure of phase and coarse grains were shown, especially under 42MPa.

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진공다이캐스팅 공법을 이용한 자동차용 조향장치 개발에 대한 사례연구 (Case Study for Developing Automobile Part (Steering Wheel) using Vacuum Die-Casting Mold)

  • 권홍규;장무경
    • 산업경영시스템학회지
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    • 제35권2호
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    • pp.196-203
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    • 2012
  • When manufacturing die casting mold, generally, the casting layout design should be considered based on the relation between injection system, casting condition, gate system, and cooling system. Also, the extent or the location of product defects were differentiated according to the various relations of the above conditions. High-qualified products can be manufactured as those defects are controled by the proper modifications or the changes of die casting mold with the conditions. In this research, the proper manufacturing method was derived intensively for reducing the defect of the internal porosity of steering wheel housing which is very complicated to achieve a good mold design. The method was also derived for minimizing and for guaranteeing the product quality through the analysis of the casting problem and the deduction of alternative plans.

컴퓨터를 이용한 회주철의 탕구방안 설계에 관한 연구 (A study on the computed aided gating design in gray cast iron)

  • 최정길;김동옥
    • 한국주조공학회지
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    • 제6권1호
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    • pp.27-35
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    • 1986
  • The gating design of gray cast iron was programmed in a Personal computer. By this program, casting test was done. The results obtained are as follows. 1. Gating design that can calculate the velocity of metal flow and size in each gate section by knowing the loss coefficient caused by friction loss and bend loss was programmed. 2. In the test casting, the gating ratio was changed into 1.1:1.3:1, 1:2:2, 1:4:4. And sound casting, free of sand washing defect, was obtained at the velocity of 35.5cm/sec in ingate.

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주조방안 자동설계 프레임워크 구축 (A Development of Casting Design Automation Framework)

  • 조원철;김성민;;손정우;이수홍
    • 한국CDE학회논문집
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    • 제17권2호
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    • pp.91-96
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    • 2012
  • Use of casting simulation software, analyzing the reason for defect became easy. However, to create a practical solution, experienced casting expert's knowledge is always indispensable. In this study, we develop casting design automation system and the algorithm based on casting expert's knowledge, so that faster and more accurate design is enabled. Especially, to generate runner which can be shaped in numerous ways, we suggest the 'nexus' method to shape runner system.

Design of Shock Absorber Housing Using Aluminum Vacuum Die Casting Technology

  • Jin, Chul-Kyu;Kang, Chung-Gil
    • 한국산업융합학회 논문집
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    • 제21권1호
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    • pp.1-8
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    • 2018
  • The purpose of this study is to develop a high-strength, high-toughness, thin-walled aluminum shock absorber housing product by applying a high vacuum die casting method to improve internal gas defect and formability. The analysis program dedicated for the casting was used because it was too costly and time-consuming to adopt the gating system design. The final casting plan was designed based on the flow pattern of the material filled into the mold and the result of air pressure and air pocket after the material was completely filled in the mold. Gaty shape was designed as a split type. The runner was designed to have the same shape as the initial inlet curve of the cavity, and the flow of the molten metal was prevented from turbulent flow. The most favorable results were obtained when the injection speed was $V_2=4.0m/s$. Defects on pores were reduced by applying high vacuum level inside the mold.

신속한 주물 시제품 개발을 위한 전산모사 기술과 산업용 단층촬영기 및 쾌속표형기의 적용 (The Application of Computer Simulation, Industrial CT and DLS RP for the rapid development of casting pilot models)

  • 유승목;임채호;조인성;최정길
    • 한국정밀공학회:학술대회논문집
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    • 한국정밀공학회 2006년도 춘계학술대회 논문집
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    • pp.195-196
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    • 2006
  • Direct laser sintering (DLS) technology for the resign coated sand is one of attractive technologies to produce molds and cores for the foundry industry rapidly and cost effectively. The objective of this case study is to develop casting pilot models using computer simulation technology, DLS RP machine and industrial computed tomography. The proposed casting design was verified by the Z-Cast software in the fields of fluid flow and solidification during the casting process. Casting parts with aluminum alloy using the post-curing treated sand moulds and cores are accurate to dimension and defect free.

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고압 다이캐스팅 공정에서 제품 결함을 사전 예측하기 위한 기계 학습 기반의 공정관리 방안 연구 (Study on the Process Management for Casting Defects Detection in High Pressure Die Casting based on Machine Learning Algorithm)

  • 이승로;이승철;한도석;김낙수
    • 한국주조공학회지
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    • 제41권6호
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    • pp.521-527
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    • 2021
  • 본 연구는 고압 다이캐스팅 공정에서 제품 결함을 사전에 예측하기 위한 기계 학습 기반의 공정 관리 모델 개발에 관한 연구이다. 모델은 이전 사이클에서의 온도를 입력받고, 사이클에 걸쳐서 나타나는 특징을 인식하여 다음 사이클의 결함 발생 여부를 예측한다. 기어 박스 형상에 대하여 제안된 알고리즘을 적용하여, 3 사이클의 정보를 통해서 98 .9%의 정확도와 96.8 %의 재현율로 제품 수축 결함을 사전에 예측하였다.

큐렛팁을 장착한 압전방식 초음파치석제거기의 작업조건에 따른 치과주조용 합금의 삭제에 관한 연구 (The Effect of a Piezoelectric Ultrasonic Scaler with Curette Tip on Casting Gold Removal in Vitro)

  • 이영규
    • Journal of Periodontal and Implant Science
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    • 제31권3호
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    • pp.531-542
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    • 2001
  • Periodontal debridement is most important procedure in periodontal treatment, because periodontal disease is the biofilm infection. The use of ultrasonic instrument has many clinical advantages compared to classical hand instrument. The introduction of newly developed ultrasonic scaler tips made the use of ultrasonic scaler popular. However the study of tooth substance removal according to the working parameters of ultrasonic scaler with newly developed tips is not sufficient. The purpose of this study is to evaluate the effects of working parameters of piezoelectric ultrasonic scaler with curette tip on casting gold removal. The working parameters was standardized by the sledge device which controls lateral force(0.5 N, 1.0 N, 2.0 N) and power setting was adjusted 2, 4, 8 in P mode and S mode and instrumentation time was 5 seconds. The defect depth and width were measured with profile meter and defect surface was examined by SME. The depth of defect was significantly large in S mode( $39.58{\pm}19.35{\mu}m$) compared to P mode( $8.37{\pm}6.98{\mu}m$). There was significant decrease of depth of defect between 1.0N($32.87{\pm}27.18{\mu}m$) and 2.0N( $14.86{\pm}15.04{\mu}m$). The area of defect was also significantly large in S mode($4482.42{\pm}3551.71{\mu}m^2$) compared to P mode( $922.06{\pm}960.32{\mu}m^2$). There was significant decrease of area of defect between 1.0N($3889.12{\pm}3936.00{\mu}m$) and 2.0N( $974.66{\pm}986.01{\mu}m$). The change of mode did not effect on the width of the defect. The change of power setting did not effect on the depth, width, and area of defect. In spite of limitation of this study it could be concluded that the use of piezoelectric ultrasonic scaler with curette tip on S mode could make significant tooth substance loss.

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대형잉곳 전산모사 결함 정량화 및 활용연구 (Cast Defect Quantify on the Simulation for Large Steel Ingots and Its Application)

  • 남궁정;김용찬;김문철;윤중묵;채영욱;이동희;오상훈;김남수
    • 한국소성가공학회:학술대회논문집
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    • 한국소성가공학회 2009년도 춘계학술대회 논문집
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    • pp.94-97
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    • 2009
  • Cast defect in large steel ingots are estimated in quality and compared each other cast conditions on simulation results by now. The cast defects, micro-crack, shrinkage, pin hole which are predictable in simulation with a reasonable accuracy. In this study, 15 ton steel ingot casting was simulated for solidification model and cast defect prediction. And the real cast was carried out in a foundry for the compeer to the simulation results, the cast defect prediction. Also, the quantity of predicted defect was tried to measuring with the defect mach counting for the various simulated cast conditions. The defect quantity work was used to find the optimized cast condition in DOE(design of experiment) procedure.

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