• 제목/요약/키워드: Turbine casing

검색결과 85건 처리시간 0.023초

열전달계수에 대한 새로운 고찰 및 고-중압 터빈 케이싱 모형의 열응력 해석 (A new consideration for the heat transfer coefficient and an analysis of the thermal stress of the high-interim pressure turbine casing model)

  • 엄달선
    • 대한기계학회:학술대회논문집
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    • 대한기계학회 2004년도 추계학술대회
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    • pp.425-429
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    • 2004
  • In real design of the high & interim pressure turbine casing, it is one of the important things to figure out its thermal strain exactly. In this paper, with the establishment of the new concept for the heat transfer coefficient of steam that is one of the factors in analysis of the thermal stress for turbine casing, an analysis was done for one of the high & interim pressure turbine casings in operating domestically. The sensitivity analysis of the heat transfer coefficient of steam to the thermal strain of the turbine casing was done with a 2-D simple model. The analysis was also done with switching of the material properties of the turbine casing and resulted in that the thermal strain of the turbine casing was not so sensitive to the heat transfer coefficient of steam. On the basis of this, 3-D analysis of the thermal strain for the high and interim pressure turbine casing was done.

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주파수 응답해석을 통한 제작공차를 가지는 저압터빈 케이싱의 고진동 원인 규명 (Investigation of the Cause of High Vibration in a Low Pressure Turbine Casing with Manufacturing Defects by Frequency Response Analysis)

  • 윤희철;우창기;황재곤
    • 한국생산제조학회지
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    • 제24권4호
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    • pp.463-468
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    • 2015
  • High vibration of a low pressure (LP) turbine casing caused safety problems and life at the facility it was housed in. The main focus of this study was the cause of the high vibration in a low pressure turbine casing with manufacturing defects by frequency response analysis, compared with the results of experiments. Therefore, excited accelerations were obtained from the LP casing fundamental, and frequency responses were analyzed. The measurement and the modal analysis showed that the natural frequency of the LP turbine casing was 61.26 Hz and the excited frequency of the turbine rotor was 60.25 Hz. The manufacturing defect caused a decrease in the casing natural frequency and resulted in the high vibration of the casing because it moved close to the resonant frequency.

Performance and Flow Condition of Cross-Flow Wind Turbine with a Symmetrical Casing Having Side Boards

  • Shigemitsu, Toru;Fukutomi, Junichiro;Toyohara, Masaaki
    • International Journal of Fluid Machinery and Systems
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    • 제9권2호
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    • pp.169-174
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    • 2016
  • A cross-flow wind turbine has a high torque coefficient at a low tip speed ratio. Therefore, it is a good candidate for use as a self-starting turbine. Furthermore, it has low noise and excellent stability; therefore, it has attracted attention from the viewpoint of applications as a small wind turbine for an urban district. However, its maximum power coefficient is extremely low (10 %) as compared to that of other small wind turbines. In order to improve the performance and flow condition of the cross-flow rotor, the symmetrical casing with a nozzle and a diffuser are proposed and the experimental research with the symmetrical casing is conducted. The maximum power coefficient is obtained as $C_{pmax}=0.17$ in the case with the casing and $C_{pmax}=0.098$ in the case without the casing. In the present study, the power characteristics of the cross-flow rotor and those of the symmetrical casing with the nozzle and diffuser are investigated. Then, the performance and internal flow patterns of the cross-flow wind turbine with the symmetrical casings are clarified. After that, the effect of the side boards set on the symmetrical casing is discussed on the basis of the analysis results.

A study on the performance and internal flow of inline Francis turbine

  • Chen, Chengcheng;Inagaki, Morihito;Choi, Young-Do
    • Journal of Advanced Marine Engineering and Technology
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    • 제38권10호
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    • pp.1225-1231
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    • 2014
  • This paper presents the performance characteristic of a Francis hydro turbine with an inline casing. This turbine is designed for city water supply system. Due to large changes in ground elevation with high points and low points, some systems may experience larger-than-normal required pressures in areas with low ground elevations. One way to dissipate these excess pressures is by the use of an inline-turbine instead of an inline-pressure reducing valve. For best applicability and minimal space consumption, the turbine is designed with an inline casing instead of the common spiral casing. As a characteristic of inline casing, the flow accesses to the runner in the radial direction, showing a low efficiency. The installation of vanes improves the internal flow and gives the positive encouragement to the output power. For the power transmission to the outside of the turbine casing from the runner axis, a belt passage is designed in the inline casing, as its influence, the region after the belt passage shows a relatively low output power. The clearance gap in the runner side space is considered, in which a small volume of flow is contracted into the clearance gap, forming the leakage flow. The leakage flow leads to a decrease in the efficiency.

A Feasibility Study on the Flow Passage Shape for an Inline Francis Hydro Turbine

  • Chen, Chengcheng;Singh, Patrick Mark;Inagaki, Morihito;Choi, Young-Do
    • 한국유체기계학회 논문집
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    • 제18권2호
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    • pp.5-13
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    • 2015
  • The aim of this study is to investigate the feasibility of a new type of casing for the inline Francis hydro turbine. Comparing with the traditional turbine with spiral casing, this turbine is unique for its flow passage shape at the first stage of flow to the turbine, very similar to a pipe, called inline casing. Before the commercialization of this new type of casing, a global investigation of the inline casing must be conducted. Preserving the structural characteristics of simple, compact-size and convenient for manufacture, different shapes of the belt passage, vertical corner and stay vanes are applied to investigate the influence of flow passage shape on the turbine performance. Stable and relatively high efficiency is achieved regardless of flow passage shape difference proving the feasibility of the inline casing used in a hydro turbine.

유한요소해석을 이용한 가스터빈 케이싱 열피로 균열발생 해석 (Investigation of the Thermo-mechanical Crack Initiation of the Gas Turbine Casing Using Finite Element Analysis)

  • 강명수;윤완노;김준성
    • 동력기계공학회지
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    • 제13권5호
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    • pp.52-58
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    • 2009
  • A gas turbine consists of an upstream compressor and a downstream turbine with a combustion chamber, and also the compressor and the turbine are generally coupled using a single shaft. Many casing bolts are used to assemble two horizontally separated casings, the gas turbine casing and the compressor casing, in both of axial and vertical directions. Because drilled holes for casing bolts in vertical direction are often too close to drilled holes for casing bolts in axial direction, one can observe cracks in the area frequently during operations of a gas turbine. In this study of the root cause analysis for the cracking initiating from the drilled holes of the casings of a gas turbine, the finite element analysis(FEA) was applied to evaluate the thermal and mechanical characteristics of the casings. By applying the field operation data recorded from combined cycle power plants for FEA, thermal and thermo-mechanical characteristics of a gas turbine are analyzed. The crack is initiated at the geometrical weak point, but it is found that the maximum stress is relieved when the same type of cracks is introduced on purpose during FEA. So, it is verified that the local fracture could be delayed by machining the same type of defects near the hole for casing flange bolts of the gas turbine, where the crack is initiated.

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지반침하 기인 저압 증기터빈 케이스 진동 저감 (Vibration Reduction of a LP Turbine Casing due to Subsidence)

  • 신범식;최연선
    • 한국소음진동공학회:학술대회논문집
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    • 한국소음진동공학회 2011년도 추계학술대회 논문집
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    • pp.384-389
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    • 2011
  • The vibration of a LP turbine casing may cause the problems of power generation and the life of its facility. In this study, we carried out on-site measurements of a LP Turbine in order to find the cause of the vibration and conducted experimental and numerical modal analysis of the turbine with its support frame. The measurement and the modal analysis show that the natural frequency of the turbine becomes close to 60 Hz due to the subsidence of the support. The elimination of the subsidence by shimming between the turbine and the support frame gave rise to the reduction of the vibration of the LP turbine case.

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증기터빈의 기동조건과 성능개선이 터빈의 진동에 미치는 영향 (Effect on Vibration of Start-up Condition and Retrofit of Steam Turbines)

  • 이혁순;정혁진;송우석
    • 한국압력기기공학회 논문집
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    • 제7권3호
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    • pp.1-7
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    • 2011
  • The analysis shows that the vibration is one of the main reasons of turbine failure. Especially, the problems caused by vibration occur right after retrofit of the turbine-generator and restarting the turbine. Through the case study of high vibration caused by after the turbine trip and restart, turbine vibration was identified to be influenced by startup condition. Turbine startup at high casing temperature right after unscheduled turbine trip cause radial expansion in rotor by contraction in axial direction, while casing continues to contract by steam flowing into casing. Consequently, gap between rotor and casing decrease until to metal contact to cause high vibration. Through the case study of high vibration of turbine-generator system after generator retrofit, it was identified that generator replacement could cause high vibration in turbine-generator system if the influence of generator replacement on entire system was not considered properly. To prevent startup delay caused by high vibration, it is important to keep the gaps at the design standard and start the turbine after thermal equilibrium.

가스터빈 케이싱의 구조안전성 및 누설 평가 (Evaluation of Structural Integrity and Leakage for a Gas Turbine Casing)

  • 서희원;함동우;김경국;한정삼
    • 한국전산구조공학회논문집
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    • 제29권4호
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    • pp.347-354
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    • 2016
  • 가스 터빈은 기동 및 정지 횟수가 많기 때문에 열피로나 취화 현상으로 인한 가스터빈 케이싱의 균열 또는 케이싱의 플랜지면에서 고온고압 가스의 누설이 발생할 가능성이 높다. 따라서 가스터빈 케이싱의 구조안전성 및 플랜지면에서의 누설평가는 반드시 수행되어야 하는 부분이다. 본 논문에서는 유한요소해석을 바탕으로 터빈 케이싱의 ASME B&PVC VIII-2 구조안전성 평가 및 접촉압력을 통한 누설 평가 그리고 볼트의 구조안전성 평가를 진행하였다. 또한 가스터빈 케이싱의 유한요소모델링 및 해석/평가 방법을 제안하여 가스터빈 개발에 활용할 수 있게 하였다.

Investigation of the Contributions of Creep and Thermal Fatigue to Failure of a High-Intermediate Pressure Steam Turbine Casing

  • Lee, Jaehong;Jung, Nam-gun
    • KEPCO Journal on Electric Power and Energy
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    • 제6권1호
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    • pp.41-47
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    • 2020
  • The contribution of damage mechanisms to failure of steam turbine casing made of Cr-Mo-V steel was investigated. Creep-fatigue interaction on the HP side corner of turbine casing was revealed as the root cause of the catastrophic failure performed by metallurgical analysis. The steady-state pressure and transient thermal stress were analyzed based on the actual operating condition of the thermal plant. Damage of creep-fatigue interaction to crack initiation was evaluated with multiaxial effects. The contribution ratio of creep and fatigue to the crack initiation was estimated to 3:1. Temporary geometrical correct action with repair weld was executed. For long-term operation, design improvement of casing equipment for creep resistance should be needed.