• 제목/요약/키워드: Steel Mill

검색결과 282건 처리시간 0.023초

다중회귀모형을 이용한 벤츄리가 없는 충격기류식 여과집진장치 압력손실 예측 (Pressure Drop Predictions Using Multiple Regression Model in Pulse Jet Type Bag Filter Without Venturi)

  • 서정민;박정호;조재환;진경호;정문섭;이병인;홍성철;시바쿠마르;최금찬
    • 한국환경과학회지
    • /
    • 제23권12호
    • /
    • pp.2045-2056
    • /
    • 2014
  • In this study, pressure drop was measured in the pulse jet bag filter without venturi on which 16 numbers of filter bags (Ø$140{\times}850{\ell}$) are installed according to operation condition(filtration velocity, inlet dust concentration, pulse pressure, and pulse interval) using coke dust from steel mill. The obtained 180 pressure drop test data were used to predict pressure drop with multiple regression model so that pressure drop data can be used for effective operation condition and as basic data for economical design. The prediction results showed that when filtration velocity was increased by 1%, pressure drop was increased by 2.2% which indicated that filtration velocity among operation condition was attributed on the pressure drop the most. Pressure was dropped by 1.53% when pulse pressure was increased by 1% which also confirmed that pulse pressure was the major factor affecting on the pressure drop next to filtration velocity. Meanwhile, pressure drops were found increased by 0.3% and 0.37%, respectively when inlet dust concentration and pulse interval were increased by 1% implying that the effects of inlet dust concentration and pulse interval were less as compared with those changes of filtration velocity and pulse pressure. Therefore, the larger effect on the pressure drop the pulse jet bag filter was found in the order of filtration velocity($V_f$), pulse pressure($P_p$), inlet dust concentration($C_i$), pulse interval($P_i$). Also, the prediction result of filtration velocity, inlet dust concentration, pulse pressure, and pulse interval which showed the largest effect on the pressure drop indicated that stable operation can be executed with filtration velocity less than 1.5 m/min and inlet dust concentration less than $4g/m^3$. However, it was regarded that pulse pressure and pulse interval need to be adjusted when inlet dust concentration is higher than $4g/m^3$. When filtration velocity and pulse pressure were examined, operation was possible regardless of changes in pulse pressure if filtration velocity was at 1.5 m/min. If filtration velocity was increased to 2 m/min. operation would be possible only when pulse pressure was set at higher than $5.8kgf/cm^2$. Also, the prediction result of pressure drop with filtration velocity and pulse interval showed that operation with pulse interval less than 50 sec. should be carried out under filtration velocity at 1.5 m/min. While, pulse interval should be set at lower than 11 sec. if filtration velocity was set at 2 m/min. Under the conditions of filtration velocity lower than 1 m/min and high pulse pressure higher than $7kgf/cm^2$, though pressure drop would be less, in this case, economic feasibility would be low due to increased in installation and operation cost since scale of dust collection equipment becomes larger and life of filtration bag becomes shortened due to high pulse pressure.

인위적 지방자기 변동에 의한 가야호의 선체자기 분포특성에 관한 연구 (A Study on the Characteristic of Ship`s Magnetic Distribution of M. S. KAYA by the Varies of Artificial Local Disturbance)

  • 조현정
    • 수산해양기술연구
    • /
    • 제34권2호
    • /
    • pp.144-158
    • /
    • 1998
  • In order to study basic information on the developed electro-magnetic compass, experiments were carried out on board M. S. KAYA at the pier of Dong Kuk Steel Mill in Pusan and the Korean southern sea using a three-axis magnetic sensor from Jan. 21, 1995 to Feb. 14, 1996. The obtained results were as follows : 1. The amount of old metal on the pier was about 27,290tons~57,440tons with an average of 40,560tons, the artificial local disturbance at the pier was min. 27.1$\mu$T, max. 66.5$\mu$T, ave. 433$\mu$T for the horizontal component and min. -27.0$\mu$T, max. 45.1$\mu$T, ave. 3.7$\mu$T for the vertical component. Its direction of horizontal component was 305$^{\circ}$ with the ship's head up bearing at 225$^{\circ}$. 2. The ship's magnetic distribution on the starboard side on berthing at the pier was 17.4$\mu$T for the horizontal component and -6.2$\mu$T for the vertical component. On the ship's port side, it was 19.8$\mu$T for the horizontal component and 4.1$\mu$T for the vertical component. On the ship's starboard side at sea, the ship's magnetic distribution was 19.2$\mu$T for the horizontal component and 3.2$\mu$T for the vertical component. On the ship's port side, the readings were 22.0$\mu$T for the horizontal component and -1.8$\mu$T for the vertical component. The directions of these readings were nearly starboard side. 3. On the pier, the secular change of the artificial local disturbance decreased 8.3$\mu$T from 61.0$\mu$T to 52.7$\mu$T for the horizontal component and decreased 7.1$\mu$T from 8.9$\mu$T M 1.8$\mu$T for the vertical component. On the starboard side from its berth, the ship, s magnetic distribution increased 2.6$\mu$T from 14.8$\mu$T to 17.4$\mu$T for the horizontal component and increased -0.1$\mu$T from -6.1$\mu$T to -6.2$\mu$T for the vertical component. On the ship's port side from its berth, it increased 7.1$\mu$T from 12.7$\mu$T to 19.8$\mu$T for the horizontal component and increased 10.2$\mu$T from -6.1$\mu$T to 4.1$\mu$T for the vertical component. 4. While at sea, on the ship's starboard side, the Secular change of the ship's magnetic distribution increased 3.9$\mu$T from 15.3$\mu$T to 19.2$\mu$T for the horizontal component and increased 2.0$\mu$T from -5.2$\mu$T to -3.2$\mu$T for the vertical component. On the port side, the changes increased 11.4$\mu$T from 10.6$\mu$T to 22.0$\mu$T for the horizontal component and increased 4.9$\mu$T from -6.7$\mu$T to -1.8$\mu$T for the vertical component. Upon berthing at the pier, the deviation of the secular change increased westerly 1 degree W~ 2.5$^{\circ}$ W from 3.5$^{\circ}$ W~ 5$^{\circ}$ W M 6W with the ship's head up bearing at 225$^{\circ}$. While at sea, these increased westerly 2$^{\circ}$ ~ 3$^{\circ}$ from the Northeast to the South and increased easterly 1$^{\circ}$ ~ 8$^{\circ}$ from the Southwest to the North. 5. While at port, within 1 mile between the ship and berth of the pier, as we approached the pier, the westerly deviation increased and when we departed the pier easterly deviation increased. When approaching the pier, the deviation was smaller than the deviation when the ship was departing from the pier. When approaching the bearing at 225$^{\circ}$ with the ship's head up bearing, the varies of deviation was smaller than the varies when the ship's head up bearing was departing from it.

  • PDF