• 제목/요약/키워드: Standard Reactor

검색결과 362건 처리시간 0.03초

Optimization of membrane fouling process for mustard tuber wastewater treatment in an anoxic-oxic biofilm-membrane bioreactor

  • Chai, Hongxiang;Li, Liang;Wei, Yinghua;Zhou, Jian;Kang, Wei;Shao, Zhiyu;He, Qiang
    • Environmental Engineering Research
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    • 제21권2호
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    • pp.196-202
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    • 2016
  • Membrane bioreactor (MBR) technology has previously been used by water industry to treat high salinity wastewater. In this study, an anoxic-oxic biofilm-membrane bioreactor (AOB-MBR) system has been developed to treat mustard tuber wastewater of 10% salinity (calculated as NaCl). To figure out the effects of operating conditions of the AOB-MBR on membrane fouling rate ($K_V$), response surface methodology was used to evaluate the interaction effect of the three key operational parameters, namely time interval for pump (t), aeration intensity ($U_{Gr}$) and transmembrane pressure (TMP). The optimal condition for lowest membrane fouling rate ($K_V$) was obtained: time interval was 4.0 min, aeration intensity was $14.6 m^3/(m^2{\cdot}h)$ and transmembrane pressure was 19.0 kPa. And under this condition, the treatment efficiency with different influent loads, i.e. 1.0, 1.9 and $3.3kgCODm^{-3}d^{-1}$ was researched. When the reactor influent load was less than $1.9kgCODm^{-3}d^{-1}$, the effluent could meet the third discharge standard of "Integrated Wastewater Discharge Standard". This study suggests that the model fitted by response surface methodology can predict accurately membrane fouling rate within the specified design space. And it is feasible to apply the AOB-MBR in the pickled mustard tuber factory, achieving satisfying effluent quality.

방사화 분석에 의한 고순도 팔라듐 금속중의 미량 루테늄에 관한 새로운 정량법 (A New Method of Determination for the Trace Ruthenium in High Purity Palladium by Neutron Activation Analysis)

  • 이철;임영창;엄경자;정구순
    • 대한화학회지
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    • 제15권4호
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    • pp.191-197
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    • 1971
  • 고 순도 팔라듐 금속(99.9%)에 함유된 루테늄 함량을 $^{104}Ru(n,{\gamma};{\beta}^-)^{105}Rh$의 핵반응에 의하여 생성된 $^{105}Rh$의 방사능을 계축하므로써 결정하였다. 원자로에서 조사된 팔라듐 시료와 루테늄 표준시료를 왕수 처리 및 과산화나트륨으로 용융시킨다음 $^{105}Rh$을 음이온 및 양이온 교환수지로 분리하였다. 팔라듐 시료로 부터 얻은 $^{105}Rh$의 방사능을 루테늄 표준시료로 부터 얻은 $^{105}Rh$의 방사능과 비교하므로서 루테늄의 함량을 결정하였다. 본 방법으로 구한 루테늄의 검출한계는 팔라듐 10mg을 시료로 하였을 때 약 1ppm이었으며 이 검출 감도는 $^{102}Ru(n,{\gamma})^{103}Ru$의 핵반응을 사용한 종래의 방사화 분석에 비해 약 40배 더 예민하였다.

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Accuracy Improvement of Boron Meter Adopting New Fitting Function and Multi-detector

  • Kong, Chidong;Lee, Hyunsuk;Tak, Taewoo;Lee, Deokjung;Kim, Si Hwan;Lyou, Seokjean
    • Nuclear Engineering and Technology
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    • 제48권6호
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    • pp.1360-1367
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    • 2016
  • This paper introduces a boron meter with improved accuracy compared with other commercially available boron meters. Its design includes a new fitting function and a multi-detector. In pressurized water reactors (PWRs) in Korea, many boron meters have been used to continuously monitor boron concentration in reactor coolant. However, it is difficult to use the boron meters in practice because the measurement uncertainty is high. For this reason, there has been a strong demand for improvement in their accuracy. In this work, a boron meter evaluation model was developed, and two approaches were considered to improve the boron meter accuracy: the first approach uses a new fitting function and the second approach uses a multi-detector. With the new fitting function, the boron concentration error was decreased from 3.30 ppm to 0.73 ppm. With the multi-detector, the count signals were contaminated with noise such as field measurement data, and analyses were repeated 1,000 times to obtain average and standard deviations of the boron concentration errors. Finally, using the new fitting formulation and multi-detector together, the average error was decreased from 5.95 ppm to 1.83 ppm and its standard deviation was decreased from 0.64 ppm to 0.26 ppm. This result represents a great improvement of the boron meter accuracy.

고도(高度) 하수처리(下水處理) 시스템의 처리성능 및 경제성 평가에 관한 연구 (Evaluation of Performance and Economical Efficiency of the Advanced Wastewater Treatment System)

  • 김동하
    • 상하수도학회지
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    • 제13권1호
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    • pp.61-71
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    • 1999
  • For a high-rate fermentation and recovery of organic acid, we have developed a new organic acid fermentation reactor with membrane filter, which is the most important part in the new advanced wastewater treatment system. The recovered organic acid is to be reused as an organic carbon source at denitrification process. Some experiments were conducted to compare the performance of acid fermentation at different SRTs, such as 5, 10, and 20 days. The total organic acid concentration produced during the runs was in the range of 2,100-2,900 (mgC/L). The conversion efficiency from substrate to organic acid reached to from 43% to 59%. The recovery rate of organic acid from substrate based on TOC was from 26% to 53%. Regardless of operational conditions, it has been able to maintain the membrane flux constantly, in the range of 0.4-0.46 ($m^3/m^2/day$). The transmembrane pressure drop was 0.2-0.3 (kg/cm) for 100 day's operation. The result of simulation is as follows. Organic removal efficiency of the new advanced treatment system is 95%. 73% of Nitrogen is removed. The removal efficiency of Phosphorus is 93%. By coqulation, soluble phosphorus is able to remove from the water treatment lines, which is impossible at conventional activated sludge system. The unit construction cost is 65000 (yen/m3) and it was 1.4 times than that of the standard activated sludge system. The unit operation cast is 7.7 ($yen/m^3/day$) and it was 1.3 times than that of the standard activated sludge system.

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최적 핵연료집합체와 표준 핵연료집합체의 열수력학적 특성비교 (Comparison of the Thermal-Hydraulic Characteristics of Optimised Fuel Assembly with That of Standard Fuel Assembly)

  • Paik, Hyun-Jong;Rim, Chang-Saeng;Park, Goon-Cherl
    • Nuclear Engineering and Technology
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    • 제22권1호
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    • pp.66-74
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    • 1990
  • 원자력 7, 8호기에 장전된 17$\times$17 최적 핵연료집합체의 열수력학적 특성을 원자력 5, 6호기에 장전된 17$\times$17표준 핵연료집합체와 비교하여 분석하였다. 분석된 열수력학적 특성은 정상상태와 과도출력상태에서의 최소 DNBR, 연료봉 중심온도, 출구 기포율등이며, 아울러 연료봉의 중심이 용융되는 국부선출력과 원자로 운전변수들에 대한 DNBR 민감도 계수도 계산하였다. 사용된 코드는 COBRA-IV-I이며, 임계열속 계산에는 R형 그리드에 대해 수정된 W-3 상관식을, 기포율계산에는 drift-flux model을 이용하였다. 계산결과, DNB가 발생할 확률은 최적 핵연료집합체가 더 높았으나, 연료봉의 중심이 용융되는 국부선출력은 표준 핵연료집합체와 거의 동일한 것으로 나타났다.

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단축질소제거 공정을 이용한 가축분뇨의 적정 처리조건 연구 (Optimal Operation Condition of Livestock Wastewater Treatment Using Shortcut Biological Nitrogen Removal Process)

  • 강진영;장영호;정병환;김연진;김용호
    • 한국물환경학회지
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    • 제39권5호
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    • pp.390-395
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    • 2023
  • The feasibility of applying the shortcut nitrogen removal process to treat livestock wastewater on individual farms was examined, and appropriate operating parameters were established. As a result,, it was determined that the nitrification reaction was carried out under 550 mg/L of ammonium nitrogen concentration, but it was less effective under conditions of high ammonia concentration. Consequently, it was confirmed that a partial injection of inflow water was necessary to minimize the effects of ammonia toxicity. Following the sequential batch reactor (SBR) operation results, it was difficult to achieve the effluent quality standard without an external carbon source. Also, selection of the appropriate hydraulic retention time was critical for the optimal SBR operation. Following the livestock farm application, with external carbon source injecting, the total nitrogen concentration in the effluent was 85.1 mg/L. This result revealed that the standard could be accomplished through a single treatment on individual livestock farms. The ratio of nitrite nitrogen to ammonia nitrogen in the effluent was verified to be suitable for implementing the anammox process with a 10 days of hydraulic retention time. This study demonstrated the potential applicability of process in the future. However, in order to apply to livestock farms, managing variations in wastewater load across individual farms and addressing reduced nitrogen oxidation efficiency during the winter season are crucial.

The Effect of Turbulence Penetration on the Thermal Stratification Phenomenon Caused by Coolant Leaking in a T-Branch of Square Cross-Section

  • Choi, Young-Don;Hong, Seok-Woo;Park, Min-Soo
    • International Journal of Air-Conditioning and Refrigeration
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    • 제11권2호
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    • pp.51-60
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    • 2003
  • In the nuclear power plant, emergency core coolant system (ECCS) is furnished at reactor coolant system (RCS) in order to cool down high temperature water in case of emergency. However, in this coolant system, thermal stratification phenomenon can occur due to coolant leaking in the check valve. The thermal stratification produces excessive thermal stresses at the pipe wall so as to yield thermal fatigue crack (TFC) accident. In the present study, effects of turbulence penetration on the thermal stratification into T-branches with square cross-section in the modeled ECCS are analysed numerically. Standard k-$\varepsilon$ model is employed to calculate the Reynolds stresses in momentum equations. Results show that the length and strength of thermal stratification are primarily affected by the leak flow rate of coolant and the Reynolds number of duct. Turbulence penetration into the T-branch of ECCS shows two counteracting effects on the thermal stratification. Heat transport by turbulence penetration from main duct to leaking flow region may enhance thermal stratification while the turbulent diffusion may weaken it.

냉각탑수 수질이 Ru/Ti 전극을 이용한 Legionella pneumophila 소독에 미치는 영향 (Effect of Water Quality of Cooling Tower on Legionella pneumophila Disinfection Using Ru/Ti Electrode)

  • 김동석;박영식
    • 한국환경과학회지
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    • 제17권6호
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    • pp.581-589
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    • 2008
  • This study was carried out to evaluate the effect of water quality of cooling tower on Legionella pneumophila disinfection using Ru/Ti electrode. The influences of parameters such as pH, turbidity, $CaCO_3$ and TOC were investigated using laboratory scale batch reactor. Oxidants such as free Cl, $ClO_2,\;H_2O_2\;and\;O_3$ were measured. The results showed that all of the water quality parameters of cooling tower had deteriorated disinfection of Legionella pneumophila. When the turbidity, $CaCO_3$ and TOC was increased, oxidants which was generated during electrolysis was decreased. pH, free Cl, $ClO_2\;and\;H_2O_2$ concentration were decreased with the increase of pH, whereas $O_3$ concentration was increased with the increase of pH. The order of effect of water quality on the disinfection performance for Legionella pneumophila was turbidity > $CaCO_3$ > TOC > pH. To obtain the safety standard (1000 CFU/L), the simultaneous increase current and NaCl dosage was needed.

1D AND 3D ANALYSES OF THE ZY2 SCIP BWR RAMP TESTS WITH THE FUEL CODES METEOR AND ALCYONE

  • Sercombe, J.;Agard, M.;Struzik, C.;Michel, B.;Thouvenin, G.;Poussard, C.;Kallstrom, K.R.
    • Nuclear Engineering and Technology
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    • 제41권2호
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    • pp.187-198
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    • 2009
  • In this paper, three power ramp tests performed on high burn-up Re-crystallized Zircaloy2 - UO2 BWR fuel rods (56 to 63 MWd/kgU) within the SCIP project are simulated with METEOR and ALCYONE 3D. Two of the ramp tests are of staircase type up to Linear Heat Rates of 420 and 520 W/cm and with long holding periods. Failure of the 420 W/cm fuel rod was observed after 40 minutes. The third ramp test consisted of a more standard ramp test with a constant power rate of 80 W/cm/min up to 410 W/cm with a short holding time. The tests were first simulated with the METEOR 1D fuel rod code, which gave accurate results in terms of profilometry and fission gas releases. The behaviour of a fuel pellet fragment and of the cladding piece on top of it was then investigated with ALCYONE 3D. The size and the main characteristics of the ridges after base irradiation and power ramp testing were recovered. Finally, the failure criteria validated for PWR conditions and fuel rods with low-to-medium burn-ups were used to analyze the failure probability of the KKL rodlets during ramp testing.

Monte Carlo 모사기법을 이용한 해체 콘크리트의 방사능 분석법 연구 (A Study on the Radioactivity Analysis of Decommissioning Concrete Using Monte Carlo Simulation)

  • 서범경;김계홍;정운수;이근우;오원진;박진호
    • 한국방사성폐기물학회:학술대회논문집
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    • 한국방사성폐기물학회 2004년도 학술논문집
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    • pp.43-51
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    • 2004
  • 현재 해체가 진행 중인 연구로 1. 2호기의 원자로 차폐 콘크리트를 해체하기 위해서는 운전기간동안 중성자 조사에 의한 방사화 정도 및 범위를 정확하게 결정하여야 한다. 차폐 콘크리트의 방사화 정도 및 범위를 결정하기 위해서 코어 시료를 채취하여 분석하여야 하는데, 시료 전처리의 어려움과 표준선원의 준비 및 자체흡수효과에 의하여 정확한 측정효율을 결정하는데 어려움이 있다. 본 연구에서는 방사능 분석에 이용되는 HPGe 검출기의 전에너지 검출 효율을 표준선원을 이용한 측정값과 Monte Carlo 방법을 이용하여 계산 값을 비교하였다. 또한, Monte Carlo 모사 기법을 이용하여 콘크리트의 밀도 및 성훈 변화에 따른 자체흡수 효과를 계산하였으며, 향후 실제 콘크리트 코어 시료를 채취 시 방사능 분석에 이용할 계획이다.

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