• Title/Summary/Keyword: Speed-up test

Search Result 711, Processing Time 0.026 seconds

A Study on the Evaluation of Dynamic Characteristics of the Pantograph for the Korean High-Speed Train through 350km/h Trial Running Test (350km/h 본선 주행시험을 통한 한국형 고속열차 판토그라프의 접촉력 특성 평가 연구)

  • Lee Hi-Sung;Mok Jin-Yong
    • Journal of the Korean Society for Railway
    • /
    • v.8 no.4
    • /
    • pp.342-347
    • /
    • 2005
  • The Korean High-Speed Train(HSR 350x) had been developed by through 'G7-R&D project' in 1996-2002, and has been testing and evaluating it's reliability on the high-speed line until now. A number of core equipments designed and developed by using domestic technologies were boarded on the HSR 350x. In order to verify the performance of HSR 350x and core equipments such as traction system, brake system and pantograph, sophisticated testing and evaluating procedures should be considered and applied. In this paper, the tested and analysed results about the dynamic characteristics of HSR 350x pantograph are introduced in a view point of the mean contact force and it's variation trend, criterion of current collection, and up-lifting of contact wire when the MSR 350x running up to 350 km/h. Through the test and evaluation, we verified that HSR 350x pantograph had an excellent current collection performance and good dynamic characteristics as it had been designed.

Fabrication arid Performance Tests of Flywheel Energy Storage System using High Tc Superconducting Bearing (고온초전도체 베어링을 사용하는 에너지 저장용 플라이휠 장치의 제작 및 성능 평가)

  • Lee, Ho-Jin;Kim, Ki-Baik;Koh, Chang-Seop;Lee, Soo-Hoon;Hong, Gye-Won
    • 한국초전도학회:학술대회논문집
    • /
    • v.9
    • /
    • pp.310-314
    • /
    • 1999
  • A prototype of Flywheel Energy Storage System with high Tc superconducting bearings was fabricated and tested to verify its applicability for the energy industry. The moment of inertia of assembled wheel with rotor magnets is about 1.072${\times}$10$^{-1}$ Kg-m$^2$. The wheel was designed to withstand its integrity up to the rotation speed of 20,000 rpm. YBCO bulk superconductors prepared by seed growth method were used as bearing to levitate and stabilize the rotating wheel. High speed rotation of the flywheel without mechanical contact was achieved by using specially designed Halbach type motor. The flywheel system showed very high stability during test operation performed up to the speed of about 10,000rpm. The energy loss measured by free decay test performed between 9,300 rpm and 7,000 rpm was calculated as about 45 W.

  • PDF

The Study of Completion Vehicle Tilting System Test for Conventional Rail Speed-Up (기존선 고속화를 위한 틸팅시스템 완성차 시험연구)

  • Lee, Su-Gil;Han, Seong-Ho;Song, Yong-Soo
    • Proceedings of the KSR Conference
    • /
    • 2007.05a
    • /
    • pp.964-967
    • /
    • 2007
  • Tilting trains are now an established feature of railway operations throughout the world. For intercity traffic, tilt provides operators with increasing speeds, and therefore enhanced competitiveness, on existing routes where insufficient traffic or a lack of funds precludes the construction of a dedicated new high-speed railway. Appling the tilting train, we can expect 30% of speed up on existing lines, but the stability of the electric current would be low because of tilting the train. Also, the spark between the catenary and pantagraph cause environmental problems such as noise, radio wave malfunction. Therefore, the tilting on pantagraph for the power suppling device is very essential for stable electric power supply.

  • PDF

Scale-up of Melting Chamber for a Pyrolysis Melting Incinemtion System (폐기물 열분해/용융 소각 시스템의 용융로 Scale-up 연구)

  • Yang, Won;Kim, Bong-Keun;Yu, Tae-U;Jeun, Keum-Ha
    • 한국연소학회:학술대회논문집
    • /
    • 2007.05a
    • /
    • pp.168-175
    • /
    • 2007
  • Ash melting chamber is one of the key facility of the pyrolysis-melting incineration system, and it should be designed and operated very carefully for avoiding solidification of slag. In this study, an example of numerical and experimental scale-up process of the melting chamber, in which high speed air is injected to the molten slag and generates bubbles, which enhances agitation of the slag and char combustion, is presented. Cold flow test, combustion and melting test in a lab-scale (30 kg/hr) chamber and a pilot scale (200 kg/hr) chamber. Minimum energy for maintaining molten slag is derived, and it was found that the molten slag can be maintained efficiently by concentrating heat into the bubbling slag.

  • PDF

Variation Trends of the Contact Force between Pantograph-Catenary and Acceleration Behavior According to the Train Running Speed and Driving Pattern in Korean High Speed Train (열차의 운행패턴과 속도에 따른 한국형 고속전철용 판토그라프의 접촉력과 가속도 거동의 변화 경향)

  • 목진용;김영국;박춘수;김기환
    • Proceedings of the Korean Society for Noise and Vibration Engineering Conference
    • /
    • 2004.05a
    • /
    • pp.200-205
    • /
    • 2004
  • The pantograph for Korean High Speed Train was developed and had been evaluating by through 'G7-R&D project for home grown high speed train technology' In this study, in mechanical aspect, the variation trend of contact force between pantograph and catenary according to the train running speed and driving pattern is conducted. A measuring system for current collecting performance and mechanical characteristics is used for this study, developed and installed on the prototype Korean High Speed Train, and physical characteristics were measured while the KHST runs on the test track. Through this study, remarkable trends of variation are found and analyzed from measured acceleration and vertical contact force between the pan head in pantograph and contact wire in catenary system according to the driving pattern and the train raised a running speed up to 300km/h.

  • PDF

Relation and Variation Trend between the Behavior of the Pantograph vs. the Vehicle Running Speed in Korean High Speed Train (한국형 고속전철용 판토그라프의 거동 특성과 열차속도와의 상관관계와 경향)

  • 목진용;박춘수;조용현;최강윤;김기환
    • Proceedings of the Korean Society for Noise and Vibration Engineering Conference
    • /
    • 2003.11a
    • /
    • pp.170-176
    • /
    • 2003
  • The pantograph for Korean High Speed Train was developed and had been evaluating by through "G7- R&D for home grown high speed train technology". In this study, a relation in mechanical aspect between the train running speed and the current collecting performance of the pantograph is conducted.'for this study, a measuring system for current collecting performance and mechanical characteristics is developed and installed on the prototype Korean High Speed Train, and measurement is conducted while the train runs on the test track. The measuring system is composed of video monitoring system and telemetry & data processing unit. It monitors whether the hazard behavior in the pantograph is occurs or not, and measures acceleration and vertical contact force between the pan head and catenary. Through this study, evaluation of a mechanical vibration characteristics and trend of the pantograph and a interface performance of pantograph - catenary up to 200㎞/h train speed are facilitated.

  • PDF

The structural analysis of bogie for high speed freight car (고속화차용 용접대차의 구조강도해석)

  • 황원주;함영삼;권성태;허현무;전응식
    • Proceedings of the KSR Conference
    • /
    • 2001.05a
    • /
    • pp.217-221
    • /
    • 2001
  • Barber bogie and Y25 bogie is the main bogie of freight car which is used in the Korean railway. In case of Barber bogie and a mixed formation tile maximum speed limit of empty car is 70 km/h and that of loaded car is 90 km/t and also it runs a speed of 110 km/h in time of an exclusive formation of Y25 bogie. The car named as high speed freight car at present is Y25 bogie which modeled on the Y25 bogie or Europe developed in 1993, Y25 bogie has no problem about the running capacity up to the speed of 110 km/h, but it works as limiting factors to tile increasing cost of maintenance and repair expenses which caused by repair of bogie and the cost of materials. This study is going to describe the contents examined by analysis and tests, aimed at being used as an index of plan in the future through the strength test of high speed freight car which is used now.

  • PDF

Effects of Surface Roughness on the Performance of a Gas Foil Thrust Bearing (표면 거칠기가 가스 포일 스러스트 베어링의 성능에 미치는 영향)

  • Sung Ho Hwnag;Dae Yeon Kim;Tae Ho Kim
    • Tribology and Lubricants
    • /
    • v.39 no.2
    • /
    • pp.81-85
    • /
    • 2023
  • This study presents an experimental investigation of the effects of surface roughness on gas foil thrust bearing (GFTB) performance. A high-speed motor with the maximum speed of 80 krpm rotates a thrust runner and a pneumatic cylinder applies static loads to the test GFTB. When the motor speed increases and reaches a specific speed at which a hydrodynamic film pressure generated within the gap between the thrust runner and test GFTB is enough to support the applied static load, the thrust runner lifts off from the test GFTB and the friction mechanism changes from the boundary lubrication to the hydrodynamic lubrication. The experiment shows a series of lift-off test and load-carrying capacity test for two thrust runners with different surface roughnesses. For a constant static load of 15 N, thrust runner A with its lower surface roughness exhibits a higher start-up torque but lower lift-off torque than thrust runner B with a higher surface roughness. The load capacity test at a rotor speed of 60 krpm reveals that runner A results in a higher maximum load capacity than runner B. Runner A also shows a lower drag torque, friction coefficient, and bearing temperature than runner B at constant static loads. The results imply that maintaining a consistent surface roughness for a thrust runner may improve its static GFTB performance.

Motion Analysis of Head and Neck of Human Volunteers in Low-Speed Rear Impact (저속 후방 추돌 자원자 실험을 통한 두부와 경부의 동작분석)

  • Hong, Seong Woo;Park, Won-Pil;Park, Sung-Ji;You, Jae-Ho;Kong, Sejin;Kim, Hansung
    • Journal of Auto-vehicle Safety Association
    • /
    • v.4 no.2
    • /
    • pp.37-43
    • /
    • 2012
  • The purpose of this research is to obtain and analyze dynamic responses from human volunteers for the development of the human-like mechanical or mathematical model for Korean males in automotive rear collisions. This paper focused on the introduction to a low-speed rear impact sled test involving Korean male subjects, and the accumulation of the motion of head and neck. A total of 50 dynamic rear impact sled tests were performed with 50 human volunteers, who are 30-50 year-old males. Each subject can be involved in only one case to prevent any injury in which he was exposed to the impulse that was equivalent to a low-speed rear-end collision of cars at 5-8 km/h for change of velocity, so called, ${\Delta}V$. All subjects were examined by an orthopedist to qualify for the test through the medical check-up of their necks and low backs prior to the test. The impact device is the pendulum type, tuned to simulate the crash pulse of a real vehicle. All motions and impulses were captured and measured by motion capture systems and pressure sensors on the seat. Dynamic responses of head and T1 were analyzed in two cases(5 km/h, 8 km/h) to compare with the results in the previous studies. After the experiments, human subjects were examined to check up any change in the post medical analysis. As a result, there was no change in MRI and no injury reported. Six subjects experienced a minor stiffness on their back for no more than 2 days and got back to normal without any medical treatment.

Performance Test for a Centrifugal Air Compressor (원심형 공기압축기 성능시험)

  • 신유환;안이기;김광호;손병진
    • Transactions of the Korean Society of Mechanical Engineers
    • /
    • v.19 no.8
    • /
    • pp.1964-1971
    • /
    • 1995
  • In the present study, the performance characteristics of a centrifugal air compressor were investigated experimentally. The PC controlled performance test facility for a centrifugal air compressor driven by an electric motor with a gear box to achieve higher compressor rotating speed was set up in the present study. The performance test for a turbocharger compressor of a diesel engine was conducted, and in a case of 34,800 rpm, pressure ratio 1.18, flow rate 0.09kg/s, compressor efficiency 61% were investigated. Adiabatic power for a tested compressor showed maximum value at mass flow ratio 0.8. The value of mass flow ratio of maximum efficiency was about 0.37, it was independent of compressor rotating speed.