• Title/Summary/Keyword: Runner shape

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Study of a Model Turbine Design Case Via Application of Spiral Case and Draft Tube Shape in Hydraulic Power Plant Modernization (수력 현대화 개·대체 시 스파이럴 케이스와 흡출관 형상에 따른 모델수차 설계 적용사례 연구)

  • Park, Nohyun;Kim, Jin-Hyuk;Kim, Seung-Jun;Hyun, Jungjae;Choi, Jongwoong;Cho, Yong
    • New & Renewable Energy
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    • v.16 no.2
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    • pp.35-46
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    • 2020
  • Recently, turbines operating in hydro power plants are required to undergo renovation and modernization due to their age exceeding 30 years. In the process of renovation or modernization, a performance test of the scaled-down model is necessary to verify the performance of the real-size model. This model test method, with criteria that is similar to that of a real turbine, is the most economical and important method. Furthermore, the shapes of the runner and guide vane can be modified or replaced easily. However, during the process of modernization, the components with the spiral casing and draft tube are impossible to repair or replace because of the buried ground. Thus, in this study, numerical analysis is conducted to investigate the hydraulic performance based on the difference between the two-dimensional computer-aided design (CAD) shape and the real three-dimensional scan shape of the spiral casing and draft tube.

Effect of different pattern size and pattern shape on castability of commercially pure titanium (납형의 크기와 형태가 티타늄의 주조성에 미치는 영향)

  • Seo, Yoon-Jeong;Oh, Gye-Jeong;Lee, Hyo-Il;Shin, Yoo-Jin;Kim, Hong-Joo;Park, Sang-Won
    • The Journal of Korean Academy of Prosthodontics
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    • v.51 no.4
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    • pp.261-268
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    • 2013
  • Purpose: The purpose of this study was to investigate the effect of geometrically different wax pattern shapes and sizes on the castability of Grade2 Cp-Ti (commercially pure titanium). Materials and methods: Total of 40 mesh wax pattern ($61mm{\times}24mm$, 207 grids), ($61mm{\times}17mm$, 138 grids) was cast in this experiment. Depending on the geometrical shape of the wax pattern, 8 groups was organized; Flat, Semicircular, Horse-shoe and V-shape, each consisting 5 samples. Runner-bar sprue was used in all patterns. The number of completely cast grid in wax pattern served as a measure for the castability of comercially pure titanium. Results: The mean value of square count in each group was as followed; 133.20 squares in group SS (96.52%), 132.40 squares in group SH (95.94%), 132.00 squares in group SF (95.65%), 127.60 squares in SV (91.43%), 198.60 squares in group LF (95.94%), 197.80 squares in group LV (95.56%), 196.40 squares in group LS (94.88%), and 188.00 squares in group LH (90.82%). Conclusion: Within the limitations of this study the results indicate that there were no sttistically significant difference in castability of titanium regarding wax pattern shape (P>.05). However, Small size wax patterns were showing the noticeable castability more than Large size pattern.

Development of 460[V]/225[A]/50[kA] Contact System in Current Limiting MCCB using an estimation and analysis method for the interrupting capability (차단성능 평가해석기법을 적용한 강자계 구동방식의 460[V]/225[A]/50[kA]급 한류형 MCCB 소호부 개발)

  • 최영길;박찬교
    • Journal of the Korean Institute of Illuminating and Electrical Installation Engineers
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    • v.18 no.1
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    • pp.78-84
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    • 2004
  • Low voltage circuit breakers which interrupt rapidly and raise the reliability of power supply are widely used in power distribution systems. In the paper, it has been investigated how much interrupting capability is improved by correcting the shape of the contact system in molded case circuit breaker(below MCCB), especially contacts and arc runner. Prior to the interrupting testing, it is necessary for the optimum design tc analyze electromagnetic forces on the contact system generated by current and flux density. This paper presents both our computational analysis and test results on contact system in MCCB

A Study on Die Casting Process of the Automobile Oil Pan Using the Heat Resistant Magnesium Alloy (내열마그네슘 합금을 이용한 자동차용 오일팬의 다이캐스팅 공정 연구)

  • Shin, Hyun-Woo;Chung, Yeon-Jun;Kang, Seung-Goo
    • Transactions of the Korean Society of Automotive Engineers
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    • v.17 no.3
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    • pp.45-53
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    • 2009
  • Die casting process of Mg alloys for high temperature applications was studied to produce an engine oil pan. The aim of this paper is to evaluate die casting processes of the Aluminium oil pan and in parallel to apply new Mg alloy for die casting the oil pan. Temperature distributions of the die and flow pattern of the alloys in cavity were simulated to diecast a new Mg alloy by the flow simulation software. Dies have to be modified according to material characteristics because melting temperature and heat capacity are different. We changed the shape and position of runner, gate, vent hole and overflow by the simulation results. After several trial and error, oil pans of AE44 and MRI153M Mg alloys are produced successfully without defect. Sleeve filling ratio, cavity filling time and shot speed of die casting machine are important parameter to minimize the defect for die casting Magnesium alloy.

An Experimental Study on the Effects of Intake Manifold Shapes on the Torque Characteristics in a 3-Cylinder LPG Engine (흡기다기관 형상변화가 3기통 LPG엔진의 토크 특성에 끼치는 영향에 관한 실험적 연구)

  • 이지근;이한풍;강신재;노병준
    • Transactions of the Korean Society of Automotive Engineers
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    • v.5 no.6
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    • pp.175-182
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    • 1997
  • The purpose of this study is to investigate the effects of intake manifold shapes to improve the engine performance in a 3-cylinder LPG engine with a closed loop fuel supply system. To know the flow resistance of intake manifolds with shape, the intake negative pressure of each runner in intake manifolds were measured by using the digital pressure meter at each driving condition. And, the engine torque and power have been measured with an engine dynamometer while adjusting the optimal fuel consumption ratio with a solenoid driver. As 속 results form this experiment, the torque characteris- tics were more improved with the plenum chamber(B type intake manifold) than with the banana type(A type intake manifold). The torque characteristics were improved at mid-engine speed(rpm) range as the inner diameter of the intake manifold became smaller. And also the optimum volume among the examined plenum chamber volume was 0.74 times(590cc) the displacement of the test engine.

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A Study on the Moulding Analysis of Automobile Valve Body Mid-plate (자동차 밸브바디 중간플레이트 성형해석에 관한 연구)

  • Jang Hun;Sung Back-Sub;Cha Yong-Hoon;Kim Duck-joong;Lee Youn-sin
    • Proceedings of the Korean Society of Machine Tool Engineers Conference
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    • 2005.05a
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    • pp.174-179
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    • 2005
  • In the super slow speed die casting process, the casting defects due to melt flow should be controlled in order to obtain sound casting products. The casting defects that are caused by molten metal were cold shut formation, entrapment of air, gas, and inclusion. But the control of casting defects has been based on the experience of the foundry engineers. The calculation of simulation can produce very useful and important results. The calculation data of die casting process condition from the computer simulation by the Z-CAST is made to insure that the liquid metal is injected at the right velocity range and that the filling time is small enough to prevent premature solidification. The parameters of runner shape that affected on the optimized conditions that was calculated with simple equation were investigated. These die casting process control techniques of automobile valve body mid-plate have achieved good agreement with the experimental data of tensile strength, hardness test, and material structure photographies satisfactory results.

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Development of Contact System in 460[V]/225[A]/50[kA] Molded Case Circuit Breaker (460[V]/225[A]/50[kA] 한류형 배선용 차단기 소호부 개발)

  • 최영길;구태근;이광식
    • Journal of the Korean Institute of Illuminating and Electrical Installation Engineers
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    • v.16 no.6
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    • pp.137-144
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    • 2002
  • Low voltage circuit breakers which interrupt rapidly and raise the reliability of power supply are widely used in power distribution systems. In the paper, it has been investigated how much interrupting capability is improved by correcting the shape of the contact system in molded case circuit breaker(below MCCB), especially arc runner. Prior to the interrupting testing, it is necessary for the optimum design to analyze electromagnetic forces on the contact system generated by current and flux density. This paper presents both our computational analysis and test results on contact system in MCCB.

A Study on the Inner Temperature Behaviors in the Casting Process for the Development of the Automatic Parts (자동차 부품 소재 개발에 따른 캐스팅 과정의 부품 내부온도 거동에 관한 연구)

  • Cha Young-Hoon;Sung Back-Sub;Jang Hoon;Kim Mi-Ai;Kim Jung-Dae;Kim Sun-Jun;Kim Duck-Joong;Lee Youn-Sin
    • Proceedings of the Korean Society of Precision Engineering Conference
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    • 2005.10a
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    • pp.279-284
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    • 2005
  • The casting defects that are caused by molten metal were cold shut formation, entrapment of air, gas, and inclusion. But the control of casting defects has been based on the experience of the foundry engineers. In this thesis, the computer simulation analyzed the flow of molten metal. The quantitative analyses which proposed the effective mold design was executed Flow patterns of 0.15-0.16m/s molten metal in 15 mm thin plate casting were investigated in order to optimize die-casting process. As increasing ingate velocity in thin plate casting, cold shot was decreased. The parameters of runner shape that affected on the optimized conditions that was calculated with simple equation were investigated. These die casting process control techniques of automobile valve body mid-plate have achieved good agreement with the experimental data of tensile strength, hardness test, and material structure photographies satisfactory results.

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A Study on Hopper Design for Minimizing the Wrapage Deformation at Injection Molding Processes (사출공정에서 휨 변형을 최소로 하는 호퍼 설계 연구)

  • Kim, Young-Suk;Lee, Eui-Joo;Son, Jae-Hwan
    • Journal of the Korea Academia-Industrial cooperation Society
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    • v.16 no.1
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    • pp.35-42
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    • 2015
  • Injection molding is a high efficient manufacturing technology for producing plastic parts. On the other hand, the warpage of molded plastic parts is an ubiquitous problem in the injection molding process. The main objective of this study was to minimize the amount of warpage occurring in the injection molding process of a hopper of ATDPS made of crystalline polymer (PP) instead of amorphous polymer (ABS). The moldflow CAE simulation was conducted for the molding process of the hopper to clarify the injection moldability, shear rate, shear stress, warpage by changing the gate shape and the number of ribs installed on the top of the hopper flange. The wide gate shape of runner system and multiple rib installation were found to be useful for minimizing the warpage of the hopper. The validity of the CAE simulations was supported by the injection molding experiment for the optimized design case.

Performance Improvement of Very Low Head Cross Flow Turbine with Inlet Open Duct (입구 개방형 덕트를 적용한 초저낙차 횡류수차의 성능향상)

  • Chen, Zhenmu;Singh, Patrick Mark;Choi, Young-Do
    • The KSFM Journal of Fluid Machinery
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    • v.17 no.4
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    • pp.30-39
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    • 2014
  • The cross flow turbine is economical because of its simple structure. For remote rural region, there are needs for a more simple structure and very low head cross flow turbines. However, in this kind of locations, the water from upstream always flows into the turbine with some other materials such as sand and pebble. These materials will be damage to the runner blade and shorten the turbine lifespan. Therefore, there is a need to develop a new type of cross flow turbine for the remote rural region where there is availability of abundant resources. The new design of the cross flow turbine has an inlet open duct, without guide vane and nozzle to simplify the structure. However, the turbine with inlet open duct and very low head shows relatively low efficiency. Therefore, the purpose of this study is to optimize the shape of the turbine inlet to improve the efficiency, and investigate the internal flow of a very low head cross flow turbine. There are two steps to optimize the turbine inlet shape. Firstly, by changing the turbine open angle along with changing the turbine inlet open duct bottom line (IODBL) location to investigate the internal flow. Secondly, keeping the turbine IODBL location at the maximum efficiency achieved at the first step, and changing the turbine IODBL angle to improve the performance. The result shows that there is a 7.4% of efficiency improvement by optimizing turbine IODBL location (open angle), and there is 0.3% of efficiency improvement by optimizing the turbine IODBL angle.