• Title/Summary/Keyword: Roll error

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Design of $H_{\infty}$ Controller for Underwater Vehicle and Nonlinear Simulation (수중운동체에 대한 $H_{\infty}$ 제어기 설계와 비선형 시뮬레이션)

  • 전찬식;김종해박홍배
    • Proceedings of the IEEK Conference
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    • 1998.06a
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    • pp.215-218
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    • 1998
  • In this paper, we design the $H_{\infty}$ controllers satisfying robust stability and performance for underwater vehicle. The underwater vehicle has computations delay time and input delay. In addition, there exist parameter uncertainties by the roll motion coefficient error, buoyance error, and gravity error. We design the $H_{\infty}$ controllers using model-matching method and check the performance of the proposed controller by nonlinear simulation which includes time delay model, sensor error model, and actuator model.

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Agricultural tractor roll over protective structure (ROPS) test using simplified ROPS model

  • Ryu-Gap Lim;Young-Sun Kang;Dae-Hyun Lee;Wan-Soo Kim;Jun-Ho Lee;Yong-Joo Kim
    • Korean Journal of Agricultural Science
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    • v.49 no.4
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    • pp.771-783
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    • 2022
  • In this study, the feasibility of alternative tractor Roll Over Protective Structure (ROPS) designed to evaluate conditions required for testing was confirmed. In accordance with Organization for Economic Cooperation and Development (OECD) code 4, the required load energy of the tractor ROPS was determined. First, the tractor ROPS test was performed and a repeated test was performed using a simplified ROPS as an alternative tractor ROPS. The test procedure is first rearward, second lateral, and last forward based on ROPS. The load test device consists of a load cell that measures force and a LVDT that measures deformation. Precision was confirmed by calculating the relative standard deviation of the simplified ROPS repeated test. Accuracy was analyzed by calculating the mean relative error between the mean measured values in the simplified ROPS test and the tractor ROPS test. As a result, the relative standard deviation was less than 2.5% for force and 3.3% for maximum deformation overall, showed the highest precision in lateral load. The mean relative error value for force measured at the lateral load of simplified ROPS was 0.5%, showing the highest accuracy. In the front load test, the mean relative error of maximum deformation was 20.5%, showing the lowest accuracy. The mean relative error (MRE) was high in the forward load test was because of structural factors of the ROPS. The simplified ROPS model is expected to save money and time spent preparing tractors.

A Study on Improvement of Roll Autopilot System (가로축 자동비행시스템 개선에 관한 연구)

  • Kim, Chong-Sup;Koh, Gi-Oak;Ji, Chang-Ho;Cho, In-Je;Lee, Dong-Kyu
    • Journal of the Korean Society for Aeronautical & Space Sciences
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    • v.43 no.8
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    • pp.706-711
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    • 2015
  • The fighter aircraft uses several different loading configurations for air-to-surface and air-to-air combat missions. To maintain wings-level flight with an asymmetric weapon configuration, a pilot controls a roll trim system. However, it is difficult to apply an accurate roll trim input for wings-level flight in the actual flight under disturbance. The inaccurate roll trim input degrades the performance of the roll autopilot system. In this paper, to solve this problem, an integrator was additionally designed in the command part of the roll autopilot system. The initial transient response was improved by scheduling the limiter to restrict the roll attitude error. As a result of the evaluation of the simulation for the designed flight control law, the roll attitude following performance was found to be improved in the autopilot system operation under the inaccurate roll trim condition.

Improvement of Recognition of Register Errors and Register Control in Roll-to-roll Printing Equipment by Data Compensation (데이터 보상을 통한 롤투롤 인쇄 장비의 레지스터 오차 인식 개선 및 제어)

  • Jeon, Sung Woong;Park, Jong-Chan;Nam, Ki-Sang;Kim, Cheol;Kim, Dong Soo;Kim, Chung Hwan
    • Journal of the Korean Society for Precision Engineering
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    • v.31 no.11
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    • pp.987-992
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    • 2014
  • Register control of roll-to-roll printing system for printed electronics requires accurate measurement of register errors. The register marks used for the recognition of patterns position between layers have inherently defects due to low printability of register marks themselves, which brings out inaccurate register accuracy and consequently low performance of printed electronics devices. In this study, the compensation methods for the unrecognized or missing register data are proposed to improve the recognition and consequently the control performance of register accuracy in roll-to-roll printing equipment. The compensation methods using the prior data and the linear interpolation are proposed and compared with the case without compensation for the simulation as well as experiment. Only the linear interpolation method could successfully compensate the missing data and consequently improve the register control performance. We should apply the compensation process of the register errors to improve the register control accuracy in the roll-to-roll printing equipment.

Development of Tilt angle measurement system of plastic thin-film using Position Sensitive Device (PSD를 이용한 플라스틱 박막 필름의 경사 각도 측정 시스템 개발)

  • Kim, Gi-Seung;Park, Yoon-Chang
    • Journal of the Korea Academia-Industrial cooperation Society
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    • v.22 no.2
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    • pp.134-138
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    • 2021
  • Various types of precision plastic thin films are used widely in high-performance displays, such as smartphones. For plastic thin-films manufactured by the Roll-to-Roll process, the film thickness must be measured and managed while moving. In the Roll-to-Roll process, wrinkles are generated when tension is applied to the film, which causes an inclination on the optical axis of the thickness gauge, resulting in a loss of accuracy. Therefore, this study attempted to develop an optical interference tomography measurement system. In this study, the tilt angle of the film was measured to correct the measurement value error in the thickness gauge caused by the tilt of the film. The system was constructed so that the laser was irradiated on the tilted film, and the laser reflected from the film was formed on the PSD. The relationship between the tilt angle of the film and the output value of the PSD was obtained experimentally. Using this, a device to measure the tilt angle of the film was constructed, and angle measurements were taken at a speed of 250,000Hz.

Evaluation of Setup Errors for Tomotherapy Using Differently Applied Vacuum Compression with the Bodyfix Immobilization System (토모테라피 치료 시 Bodyfix System에서 진공압박에 따른 환자 위치잡이오차(Setup errors)의 평가)

  • Jung, Jae-Hong;Cho, Kwang-Hwan;Lee, Jeong-Woo;Kim, Min-Joo;Lim, Kwang-Chae;Moon, Seong-Kwon;Kim, Yong-Ho;Suh, Tae-Suk
    • Progress in Medical Physics
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    • v.22 no.2
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    • pp.72-78
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    • 2011
  • The aim of this study is to evaluate the patient's setup errors in TomoTherapy (Hi-Art II, TomoTherapy, USA) Bodyfix system (Medical Intelligence, Ele-kta, Schwabmuchen, Germany) pressure in the vacuum compression, depending on and were evaluated. Bodyfix immobilization system and vacuum pressure was compression applied to the patients who received Tomotherapy thoracic and abdominal area, 21 patients were selected and TomoTehpay treatment total 477 of MVCT images were obtained. The translational (medial-lateral: ML, anterior-posterior: AP, superior-inferior: SI directions) and rolling were recorded and analyzed statistically. Using Pearson's product-moment coefficient and One-way ANOVA, the degree of correlation depending on the different vacuum pressure levels were statistically analyzed for setup errors from five groups (p<0.05). The largest average and standard deviation of systematic errors were 6.00, 5.95 mm in the AP and SI directions, respectively. The largest average of random errors were 4.72 mm in the SI directions. The correlation coefficients were 0.485, 0.244, and 0.637 for the ML-Roll, AP-Vector, and SI-Vector, respectively. SI-Vector direction showed the best relationship. In the results of the different degree of vacuum pressure in five groups (Pressure range: 30~70 mbar), the setup errors between the ML, SI in both directions and Roll p=0.00 (p<0.05) were shown significant differences. The average errors of SI direction in the vacuum pressure of 40 mbar and 70 mbar group were 4.78 mm and -0.74 mm, respectively. In this study, the correlation between the vacuum pressure and the setup-errors were statistically analyzed. The fact that setup-errors in SI direction is dependent in vacuum pressure considerly setup-errors and movement of interal organs was identified. Finally, setup-errors, and it, based on the movement of internal organs in Bodyfix system we should apply more than 50 mbar vacuum pressure. Based on the results of this study, it is suggested that accuracy of the vacuum pressure and the quantitative analysis of movement of internal organs and the tumor should be studied.

Design and Development of Gravure Offset Printing System (그라비아 옵셋 인쇄 장비 설계 및 제작)

  • Noh, Jae-Ho;Lee, Taik-Min;Park, Sang-Ho;Jo, Jeong-Dai;Kim, Dong-Soo
    • Journal of the Korean Society for Precision Engineering
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    • v.27 no.9
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    • pp.16-19
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    • 2010
  • This paper presents how to design and fabricate the gravure offset printing system for enhancement of register precision. Factors of precision error are caused by imprecision of gravure plate, deformation of substrate, printing quality change due to the change of ink viscosity, Imprecision of printing machine, and so on. This study suggests concept design of gravure offset printing system which is able to minimize or remove these error factors.

Development of roll bending process technology applied precision orthogonal feeding robot system (정밀 직교 피딩 로봇시스템 적용 롤 밴딩 공정 기술 개발)

  • Lim, Sang-Ho;Ahn, Sang-Jun;Yun, Gyeong-Yeol
    • Industry Promotion Research
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    • v.7 no.4
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    • pp.9-15
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    • 2022
  • This study evaluated the automated system of the roll bending process, which is one of the difficult processes. In the past, 20 cartridges were produced per hour. but Automation changed it to a process that produces 50 pieces per hour. The average value of production was 57.6 pieces per hour, error of repeatability was 0.03 mm, average roll diameter error value was 0.49 mm, average alignment error value was 0.09 mm and average process lead time was 43.21 seconds. This paper presented specific evaluation methods such as productivity, repeatability, defect rate, alignment defect rate, and process lead time. It is thought that the contents performed in this study will be helpful in the verification of other automation systems in the future.

Development of Technology for Setting Rolling Speed of Finishing Rolling Process in Hot Strip Mill (열연 마무리 압연공정 압연롤 회전속도 설정 기술 개발)

  • Hong, Seong-Cheol;Lee, Haiyoung
    • Journal of the Korean Institute of Illuminating and Electrical Installation Engineers
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    • v.27 no.11
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    • pp.47-56
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    • 2013
  • Rolling speed, roll gap, and cooling pattern in hot strip finishing mill process should be determined before inserting strip into roll. Such parameters are initially calculated by a mathematical set-up model. The technique to find adequate roll speed via a mathematical model has inherently limit because required working conditions are various and rolling process is nonlinear. To improve the accuracy of initial rolling speed for a finishing mill, this paper suggests a correction technology for initial rolling speed. The proposed method was implemented in hot strip mill process. As the results, the magnitude of width error in strip head-end part caused by excessive strip tension was decreased remarkably.