• Title/Summary/Keyword: Process of spray development

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A study on the Dioxin behavior in the process of representative pyrolysis/gasfication/melting plant (대표적인 열분해가스화 용융시설의 공정별 다이옥신 배출거동에 관한 연구)

  • Shin, Chan-Ki;Shin, Dae-Yun
    • Journal of environmental and Sanitary engineering
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    • v.22 no.1 s.63
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    • pp.1-16
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    • 2007
  • The incineration process has commonly used for wastes amount reduction and thermal treatments of pollutants as the technologies accumulated. However, the process is getting negative public images owing to matter of hazardous pollutants emission. Specially dioxins became a main issue and is mostly emitted from municipal solid wastes incineration. In this reason, pyrolysis/gasfication/melting process is presented as a alternative of incineration process. The pyrolysis/gasfication/melting process, a novel technology, is middle of verification of commercial plant and development of technologies in Korea. But the survey about the pollutant emission from the process, and background data in these facilities is necessary. So in this survey, it Is investigated that the behavior of dioxins in three pyrolysis/gasfication/melting plant (S, T, P) of pilot scale. In case of S plant, concentration of dioxins shows high at latter part of cogenerated boiler and stack which are operate on low temperature conditions than a latter parts of pyrolysis and melting furnace which are operate on high temperature condition. Concentration of gas phage dioxins had increased after combusted gas passed cogenerated boiler and this is attributed to react of precursor materials such as chlorobenzene and chlorophenol. Concentration of dioxins in T plant showed lower levels at latter part of cooling equipment which are operate with water spray type on low temperature conditions than a latter parts of gasfied melting furnace which are operate on high temperature condition. Removal efficiency of dioxins at gas treatment equipment was 78.8 %. Concentration of dioxins in P plant was low at latter part of SDA/BF which is operate at low temperature conditions than a latter parts of pyrolysis gasfied chamber which are operate at high temperature condition. Removal efficiency of dioxins of SDA/BF was 85.9 % and therefore, it showed high efficiency at those of stoker type incineration facility. However, concentration of dioxins which emitted at high temperature condition were low in three facilities and satisfied present standard emission level of dioxins. To consider the distribution ratio of dioxins, Particulate phase dioxins at S and P plants showed similar ratio with which shows in current stoker type for middle scale domestic waste incineration facility. It is necessary to continuos monitoring the ratio of distribution of dioxins in T plant in because ratio of gas phage dioxins showed high.

A Study on the Development of Contemporary Jewelry through Resin Infusion Method -Focusing on Basalt fiber- (레진 인퓨전 성형을 통한 현대장신구 개발에 관한 연구 -바살트 섬유를 중심으로-)

  • Kwon, In-Hye;Hwang, Sun-Wook
    • Journal of Digital Convergence
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    • v.20 no.4
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    • pp.597-606
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    • 2022
  • This study attempted to find a new manufacturing method through Basalt fiber and resin infusion method to expand the range of expressions of Contemporary jewelry produced in studios. To this end, the concept of fiber introduction and infusion method was examined through analysis of used cases, and based on this, flat plates and color samples were produced, and then the samples were made to estimate the possibility of direct use in jewelry. As a result, the infusion method process presented certain results that could be used as a production process in the studio, and Basalt fibers were able to express various colors of spray and porselin, especially fiber its painted with porselin, which have high strength and they can be expressed intentionally, it are very valuable as jewelry's material, it is expected to be an opportunity to expand the practical production methods and expressions of Contemporary jewelry.

Control of Algal Blooms in Eutrophic Water Using Porous Dolomite Granules

  • Huh, Jae-Hoon;Choi, Young-Hoon;Lee, Shin Haeng;Cheong, Sun Hee;Ahn, Ji Whan
    • Journal of the Korean Ceramic Society
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    • v.54 no.2
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    • pp.108-113
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    • 2017
  • The use of aluminum-based coagulants in water pretreatment is being carefully considered because aluminum exposure is a risk factor for the onset of Alzheimer's disease. Lightly burned-dolomite kiln dust (LB-DKD) was evaluated as an alternative coagulant because it contains high levels of the healthful minerals calcium and magnesium. An organic pore forming agent (OPFA) was incorporated to prepare porous granules after OPFA removal through a thermal decomposition process. A spray drying method was used to produce uniform and reproducible spherical granules with low density, since fine dolomite particles have irregular agglomeration behavior in the hydration reaction. The use of fine dolomite powder and different porosity granules led to a visible color change in raw algae (RA) containing water, from dark green to transparent colorlessness. Also, dolomite powders and granules exhibited a mean removal efficiency of 48.3% in total nitrogen (T-N), a gradual increase in the removal efficiency of total phosphorus (T-P) as granule porosity increased. We demonstrate that porous dolomite granules can improve the settling time and water quality in summer seasons for the emergent treatment of excessive algal blooms in eutrophic water.

Development of online drone control management information platform (온라인 드론방제 관리 정보 플랫폼 개발)

  • Lim, Jin-Taek;Lee, Sang-Beom
    • Journal of the Institute of Convergence Signal Processing
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    • v.22 no.4
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    • pp.193-198
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    • 2021
  • Recently, interests in the 4th industry have increased the level of demand for pest control by farmers in the field of rice farming, and the interests and use of agricultural pest control drones. Therefore, the diversification of agricultural control drones that spray high-concentration pesticides and the increase of agricultural exterminators due to the acquisition of national drone certifications are rapidly developing the agricultural sector in the drone industry. In addition, as detailed projects, an effective platform is required to construct large-scale big data due to pesticide management, exterminator management, precise spraying, pest control work volume classification, settlement, soil management, prediction and monitoring of damages by pests, etc. and to process the data. However, studies in South Korea and other countries on development of models and programs to integrate and process the big data such as data analysis algorithms, image analysis algorithms, growth management algorithms, AI algorithms, etc. are insufficient. This paper proposed an online drone pest control management information platform to meet the needs of managers and farmers in the agricultural field and to realize precise AI pest control based on the agricultural drone pest control processor using drones and presented foundation for development of a comprehensive management system through empirical experiments.

Structural characterization of $Al_2O_3$ layer coated with plasma sprayed method (플라즈마 스프레이 방법으로 코팅 된 $Al_2O_3$막의 구조적 특성)

  • Kim, Jwa-Yeon;Yu, Jae-Keun;Sul, Yong-Tae
    • Journal of the Korean Crystal Growth and Crystal Technology
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    • v.16 no.3
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    • pp.116-120
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    • 2006
  • We have investigated plasma spray coated $Al_2O_3$ layers on Al-60 series substrates for development of wafer electrostatic chuck in semiconductor dry etching system. Samples were prepared without/with cooling bar on backside of samples, at various distances, and with different powder feed rates. There were many cracks and pores in the $Al_2O_3$ layers coated on Al-60 series substrates without cooling bar on the backside of samples. But the cracks and pores were almost disappeared in the $Al_2O_3$ layers on Al-60 series substrates coated with cooling bar on the back side of samples, 15 g/min. powder feed rate and various 60, 70, 80 mm working distances. Then the surface morphology was not changed with various working distances of 60, 70, 80 mm. When the powder feed rate was changed from 15 g/min to 20 g/min, the crack did not appear, but few pores appeared. Also the $Al_2O_3$ layer was coated with many small splats compared with $Al_2O_3$ layer coated with 15 g/min powder feed rate. The deposited rate of $Al_2O_3$ layer was higher when the process was done without cooling bar on the back side of sample than that with cooling bar on the back side of sample.

Development of Mobile Vortex Wet Scrubber and Evaluation of Gas Removal Efficiency (기체상 유해화학물질 제거를 위한 이동형 와류식 세정장치 개발 및 가스 제거효율 분석)

  • Kwak, Ji Hyun;Hwang, Seung-Ryul;Lee, Yeon-Hee;Kim, Jae-Young;Song, Ki Bong;Kim, Kyun;Kang, Jae Eun;Lee, Sang Jae;Jeon, Junho;Lee, Jin Hwan
    • Korean Journal of Environmental Agriculture
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    • v.34 no.2
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    • pp.134-138
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    • 2015
  • BACKGROUND: In recent years, several researchers have focused on odour control methods to remove the harmful chemicals from chemical accidents and incidents. The present work deals with the system development of the hazardous. METHODS AND RESULTS: For on-site removal of hazardous gaseous materials from chemical accidents, mobile vortex wet scrubber was designed with water vortex process to absorb the gas into the water. The efficiency of the mobile vortex wet scrubber was evaluated using water spray and 25% ammonia solution. The inlet air velocity (gas flow rate) was according to the damper angle installed within the hood and with increase of gas flow rate, consequently the absorption efficiency was markedly decreased. In particular, when 25% ammonia solution was exposed to the hood inlet for 30 min, the water pH within the scrubber was changed from 7 to 12. Interestingly, although the removal efficiency of ammonia gas exhibited approximately 80% for 5 min, its efficiency in 10 min showed the greatest decrease with 18%. Therefore, our results suggest that the ammonia gas may be absorbed with the driving force of scrubbing water in water vortex process of this scrubber. CONCLUSION: When chemical accidents are occurred, the designed compact scrubber may be utilized as effective tool regarding removal of ammonia gas and other volatile organic compounds in the scene of an accident.

Production of Carbonized Rice Husk by a Cyclone Combustor (III) (사이클론 연소기를 이용한 탄화왕겨의 제조 (III))

  • 김원태;노수영
    • Journal of Biosystems Engineering
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    • v.25 no.3
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    • pp.187-194
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    • 2000
  • One of effective utilization technique of rice husk is known to carbonize it for using as the culture materials. A series of study on the production of carbonized rice husk by a cyclone combustor shows that the carbonized rice husk produced have a strong alkalinity. Therefore, carbonized rice husk produced by a cyclone combustor is required to neutralize with proper normality. This work is the third part of a series on the production of carbonized rice husk by a cyclone combustor. In this work, the development of neutralization process was carried out in the range of experimental conditions recommended in the previous study. Those include the preheat temperature of combustion chamber of T1b=1273∼1373K, equivalence ratio =1.68∼2.17, auxiliary gas flow rates Qg=5.15∼6.43$\ell$/min. The injection technique of dilute acid was employed for neutralization. At the lower position of the outside of combustor, a dilute nitric acid selected as neutralization liquid was injected to the carbonized rice husk exhausted from the combustion chamber. The normalities of dilute nitric acid were varied to 0.01, 0.03 and 0.05N, respectively. The injection flow rates of the solution were changes from 1.7∼4$\ell$/min. The required carbonized and neutralized rice husk could be obtained at the dilute nitric acid with normality of 0.3N and flow rate of dilute nitric acid of 2∼3.5$\ell$/min. However, the carbonized and neutralized rice husks of about 10∼20% were destroyed by spray with high injection pressure.

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Thermostability of Monolithic and Reinforced Al-Fe-V-Si Materials

  • He, Yiqiang;Qiao, Bin;Wang, Na;Yang, Jianming;Xu, Zhengkun;Chen, Zhenhua;Chen, Zhigang
    • Advanced Composite Materials
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    • v.18 no.4
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    • pp.339-350
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    • 2009
  • Al-Fe-V-Si alloys reinforced with SiC particles were prepared by multi-layer spray deposition technique. Both microstructures and mechanical properties including hardness and tensile properties development during hot exposure process of Al-8.5Fe-1.3V-1.7Si, Al-8.5Fe-1.3V-1.7Si/15 vol% $SiC_P$ and Al-10.0Fe-1.3V-2Si/15 vol% $SiC_P$ were investigated. The experimental results showed that an amorphous interface of about 3 nm in thickness formed between SiC particles and the matrix. SiC particles injected silicon into the matrix; thus an elevated silicon concentration was found around $\alpha-Al_{12}(Fe,\;V)_3Si$ dispersoids, which subsequently inhibited the coarsening and decomposition of $\alpha-Al_{12}(Fe,\;V)_3Si$ dispersoids and enhanced the thermostability of the alloy matrix. Moreover, the thermostability of microstructure and mechanical properties of Al-10.0Fe-1.3V-2Si/15 vol% $SiC_P$ are of higher quality than those of Al-8.5Fe-1.3V-1.7Si/15 vol% $SiC_P$.

Engineering Cellulose Fibers for High-Value Added Products for Pulp & Paper Industry

  • Ko, Young Chan;Park, Jong-Moon
    • Journal of Korea Technical Association of The Pulp and Paper Industry
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    • v.47 no.6
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    • pp.22-40
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    • 2015
  • Cellulose fibers is one of the most abundant in nature. It has many distinctive features: abundant in nature, biodegradable, non-toxic, eco-friendly, sustainable, easy to fabricate, hydrophilic, and cost-effective. Cellulose fibers, known as pulp, is produced from cellulose-containing materials by the pulping process. As the raw material, wood has been most commonly used while recycled pulp has been also used to some degree. Thus, pulp usually refers to wood pulp. Generally, the pulp and paper industry is regarded as the commodity market where the cost should be much more important than the quality. It also belongs to a mature market where the growth is slow, or even in decline. Accordingly, technological development has been rather stagnant for the industry. Recently, however, the pulp and paper industry has faced very serious challenges. First, due to digital technology, there has been a steady decline in the need for pulp and paper products. The digital industry has continuously replaced printed products such as books, newspapers, and magazines. Second, there has been a trend initiated by developed countries to limit the use of wood as the raw material for the sake of environmental protection. This forces the industry to find a more efficient use of wood pulp as well as finding alternative, non-wood sources. Third, as an individual becomes wealthier and more conscious of health-care, the quality of a product becomes more important than the cost. Thus, a paradigm shift is needed from the cost-conscientious to the quality conscientious. The objective of this article is to review the technologies aimed at engineering cellulose fibers for producing high-value added paper products.

Design and Cold Flow Test of a Multi-injector Engine using Hydrogen Peroxide/Kerosene (과산화수소/케로신을 이용한 다중 분사기 엔진 설계 및 수류 실험)

  • Lee, Yang-Suk;Jeon, Jun-Su;Ko, Young-Sung;Kim, Yoo;Kim, Sun-Jin
    • Journal of the Korean Society of Propulsion Engineers
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    • v.16 no.1
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    • pp.36-44
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    • 2012
  • Multi-injector rocket engine using high-concentrated hydrogen peroxide and kerosene was designed and manufactured. Design requirements of a rocket engine were determined and main geometrical parameters of rocket engine were determined on the basis of fundament. Six coaxial swirl injectors were mounted on the multi-injector engine. Flow analysis in the hydrogen peroxide manifold was performed to minimize stagnation and recirculation zones. Finally, the optimized hydrogen peroxide manifold was manufactured and cold flow test was carried out to confirm mass flow rate per uni-element, spray pattern and atomization characteristics. The results of cold flow test showed that the mixing head design process was successful and enough to use as a essential database for the development of a full-scale engine.