• Title/Summary/Keyword: Power condensor

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DC Power Control for 3-Level Converter. (3-레벨 컨버터에 의한 직류전력제어)

  • 정연택;이사영;함년근
    • Proceedings of the KIPE Conference
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    • 1996.06a
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    • pp.126-129
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    • 1996
  • This paper study on the control method of 3-level converter. The control of converter is composed of active power control for controlling a output voltage and of reactive power control for high power factor drives. And also, output central voltage is controlled by sensing a each condensor voltage of bank connected the part of dc.

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A Study on the Power Factor Improvement of V47-660 kW Wind Turbine Generation System in Jeju Wind Farm (제주 풍력발전 단지의 V47-660 kW 시스템의 역률개선에 관한 연구)

  • Kim, Eel-Hwan;Jeon, Young-Jin;Kim, Jeong-Woong;Kang, Geong-Bo;Huh, Jong-Chul;Kim, Gun-Hoon
    • Journal of the Korean Solar Energy Society
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    • v.23 no.3
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    • pp.45-53
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    • 2003
  • This paper presents a study on the power factor improvement of V47- 660 [kW] Wind Turbine Generation System (WTGS) in Jeju wind farm, as a model system in this paper. In this system, the power factor correction is controlled by the conventional method with power condensor banks. Also, this system has only four bank steps, and each one capacitor bank step is cut in every one second when the generator has been cut in. This means that it is difficult to compensate the reactive power exactly according to the variation of them. Actually, model system has very low power factor in the area of low wind speed, which is almost from 4 to 6 [m/s]. This is caused by the power factor correction using power condenser bank. To improve the power factor in the area of low wind speed, we used the static var compensator(SVC) using current controlled PWM power converter using IGBT switching device. Finally, to verify the proposed method, the results of computer simulation using Psim program are presented to support the discussions.

Determination of Proto Type for 345kV CV Cable Accessories (345kV CV 케이블 접속함의 Proto Type 선정)

  • Lee, S.K.;Kim, I.T.;Son, S.H.;Choi, S.G.;Huh, G.D.;Park, W.K.
    • Proceedings of the KIEE Conference
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    • 1998.07e
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    • pp.1629-1631
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    • 1998
  • Crosslinked polyethylene (XLPE) insulated cables are now widely used all over the world for extra-high voltage underground transmission systems. Prefabricated type (compression type) joint has developed in order to shorten the assembly time and lower the possibility of contamination at site by many companies in the world. For outdoor termination, to control the electric field distribution as uniform as possible, especially for the use of extra-high voltage system. much of products are adopting the oil-impregnated condensor cone type instead of electric field control element which uses the permitivity of it only (not capacitance). For Gas-immersed termination, dimension of outer insulation bushing was determined by IEC Publication 859. The highest voltage of underground power cable system is 345kV now, in Korea. We have much of experiences of the development of prefabricated type accessories for CV cable systems (154kV, 161kV, 230kV level). So it was possible to inspect the proto type of accessories for 345kV CV cable system and seems that the need time for the development of products is reduced.

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Simultaneous Removal of SOx and NOx in Flue Gas of Oxy-fuel Combustion by Direct Contact Condenser (직접접촉식 응축기를 통한 가압순산소 연소 배가스 내 SOx, NOx 동시저감 연구)

  • Choi, Solbi;Mock, Chinsung;Yang, Won;Ryu, Changkook;Choi, Seuk-Cheon
    • Clean Technology
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    • v.25 no.3
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    • pp.245-255
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    • 2019
  • Pressurized oxy-fuel combustion is a promising technology for $CO_2$ capture with a benefit of improving power plant efficiency compared with atmospheric oxy-fuel combustion. Prior to $CO_2$ compression in this process, a flue gas condenser (FGC) is used to remove $H_2O$ while recovering the latent heat. At the same time, the FGC has a potential for high-efficiency removal of $SO_x$ and $NO_x$ by exploiting their good solubility in water. In this study, experiments were carried out in a lab-scale, direct contact FGC under different pressures varying between 1 and 20 bar to evaluate the removal efficiency of $SO_2$ and $NO_x$ for individual gases and their mixture. In the tests for individual gases, 20% and 76% of $NO_x$ was removed at 1 bar and 10 bar, respectively. Even higher removal efficiencies were achieved for $SO_2$, and also these were maintained for longer as the pressure increased. In the tests for $SO_2$ and $NO_x$ mixture, the removal efficiency of $NO_x$ increased from 13% at 1 bar to 56% at 20 bar because of higher solubility at elevated pressures. $SO_2$ in the mixture was initially dissolved almost completely and then increased by 1,219 ppm at 1 bar and by 165 ppm at 20 bar. Overall, the removal efficiency of $SO_2$ and $NO_x$ was increased at elevated pressures, but it was lower in the mixture compared with individual gases at identical conditions because of a lower pH and associated chemical reactions in water.