• Title/Summary/Keyword: Nozzle Cleaning

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Performance Evaluation of Automatic Self-Cleaning Filter System using Twin-Fluid Nozzles for Air Cleaning in the Subway Stations (지하철 공기청정을 위한 2유체노즐형 자동세정 공기청정 시스템 개발에 관한 연구)

  • Ahn, Y.C.;Lee, J.K.
    • Journal of ILASS-Korea
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    • v.9 no.3
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    • pp.15-21
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    • 2004
  • The removal of the dusts in the subway stations, tunnels, factories and buildings becomes issue for comfortable indoor and outdoor conditions. There has been used an automatic self-cleaning filter system to collect the dusts. In general, the collected particles are removed by water spray nozzles. The new design for improving the cleaning efficiency of collected dusts and reducing the supplied water is the concept of the plane array of demister filters and the twin-fluid nozzle for mixing compressed air and water in the automatic self-cleaning filter system. Results show that the cleaning efficiency of twin-nozzle filter systems is 99.1%, compared to 47% in the conventional filter system. Therefore the automatic self-cleaning filter system using twin-fluid nozzle filter systems reduces water supplied in the filter system, and increases cleaning efficiency and drying efficiency.

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The optimization of nozzle size for pulse cleaning of ceramic filter (세라믹필터 역세정을 위한 노즐 사이즈 최적화)

  • Choi, Joo-Hong;Kim, Jin-Hyoung;Chi, Hua-Chang;Yu, Lang;Sakong, Kyoung-Min;Kim, Young-Ae
    • 한국신재생에너지학회:학술대회논문집
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    • 2007.06a
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    • pp.796-799
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    • 2007
  • In the bench scale test unit consisting of four commercial filter elements, the traces of the transient pressure around the nozzle and overpressure in the filter cavity were measured to estimate the effect of nozzle on pulse cleaning. For the given pulse cleaning system, the convergent nozzle displayed better performance than the straight one. The optimum ratio of outlet to inside diameter of convergent nozzle was determined, which minimized the pulse gas consumption and maximized the entrainment effect. The angle and height of nozzle convergent part was also optimum operational condition, which is meaningful to the industrial applying.

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Design and Performance Test of Wide Blasting Nozzle for Curved Surface Cleaning based on Compressible Flow Analysis (압축성 유동해석에 기초한 곡면 세정을 위한 브라스팅 광폭 노즐의 설계 및 성능시험)

  • Kim, Taehyung;Kwak, Jun Gu;Sohn, Myong Hwan
    • Journal of Energy Engineering
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    • v.28 no.1
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    • pp.57-64
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    • 2019
  • In this study, the blasting nozzle for surface treatment of the curved surface of parts in power plant industry was designed and the cleaning performance was examined through the compressible flow analysis. At this time, the outlet of the curved nozzle was designed as a curved surface along the surface of the part. After the nozzle was made by 3-D printing, the abrasive was sprayed on the surface of the cylindrical specimen and the cleaning performance test was performed. The effective cleaning area obtained after the analysis was similar to the size and shape of the effective cleaning area obtained after the experiment. From this, the validity and effectiveness of the curved nozzle design was confirmed.

Optimization of FPD Cleaning System and Processing by Using a Two-Phase Flow Nozzle (이류체 노즐을 이용한 FPD 세정시스템 및 공정 개발)

  • Kim, Min-Su;Kim, Hyang-Ran;Kim, Hyun-Tae;Park, Jin-Goo
    • Korean Journal of Materials Research
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    • v.24 no.8
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    • pp.429-433
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    • 2014
  • As the fabrication technology used in FPDs(flat-panel displays) advances, the size of these panels is increasing and the pattern size is decreasing to the um range. Accordingly, a cleaning process during the FPD fabrication process is becoming more important to prevent yield reductions. The purpose of this study is to develop a FPD cleaning system and a cleaning process using a two-phase flow. The FPD cleaning system consists of two parts, one being a cleaning part which includes a two-phase flow nozzle, and the other being a drying part which includes an air-knife and a halogen lamp. To evaluate the particle removal efficiency by means of two-phase flow cleaning, silica particles $1.5{\mu}m$ in size were contaminated onto a six-inch silicon wafer and a four-inch glass wafer. We conducted cleaning processes under various conditions, i.e., DI water and nitrogen gas at different pressures, using a two-phase-flow nozzle with a gap distance between the nozzle and the substrate. The drying efficiency was also tested using the air-knife with a change in the gap distance between the air-knife and the substrate to remove the DI water which remained on the substrate after the two-phase-flow cleaning process. We obtained high efficiency in terms of particle removal as well as good drying efficiency through the optimized conditions of the two-phase-flow cleaning and air-knife processes.

A Numerical Analysis Using CFD for Effective Process at CMP Equipment (CFD를 이용한 CMP장비의 효과적인 공정을 위한 수치해석적 연구)

  • Lee, Sue-Yeon;Kim, Kwang-Sun
    • Journal of the Semiconductor & Display Technology
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    • v.10 no.4
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    • pp.139-144
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    • 2011
  • CMP process is an essential element in the semiconductor product processes in Chemical Mechanical Polishing. Taken as a whole, CMP is one process, but concretely, it is a detail process which consists of polishing, cleaning, and so on. Especially, the polishing and cleaning are key points in the whole process. Polishing rate is the most important factor and is related with deposition of slurry in the polishing process. Each outlet velocities is the most important factors in cleaning process. And when the velocities are more uniform, the cleaning becomes more effective. In this research, based on these factors, we performed a numerical analysis for effective polishing and cleaning which can be applied to industrial field. Consequently, we figured out that more than one opened nozzle is more effective than one opened nozzle at the polishing pad in case of this research. And we confirmed that the revised models have the uniform velocity distribution more than the previous model of the cleaning nozzle.

65nm급 300mm Wafer 세정조 개발을 위한 유동 특성연구

  • Kim, Jin-Tae;Kim, Gwang-Seon;Lee, Seung-Hui;Jeong, Eun-Mi
    • Proceedings of the Korean Society Of Semiconductor Equipment Technology
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    • 2007.06a
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    • pp.174-178
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    • 2007
  • The cleaning process to remove small particles, ions, and other polluted sources is one of the major parts in the recent semiconductor industry because it can cause fatal errors on the quality of the final products. According to the other reports, the major factors of bath's fluid motion are the cleaning method, nozzle, the geometry (of bath, guide and wafer), and the position (of guide and wafer). So to enhance cleaning efficiency in the bath, these factors must be controlled. The purpose of this study is to analyze and visualize fluid motion in the cleaning bath as basic data for designing the nozzle system and finding the process control parameters. For that, we used the general CFD code FLUENT.

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A Study on the Manufacturing Process of Black Ink for Screen Printing by using Waste Ink (폐잉크를 이용한 스크린 인쇄용 블랙 잉크 제조에 관한 연구)

  • Kwon, Hee-Kyoung;Woo, Jin-Ho
    • Journal of the Korean Graphic Arts Communication Society
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    • v.28 no.2
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    • pp.87-99
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    • 2010
  • The ink which is left by sealed more than 6 months, it clogs head nozzle of machine due to precipitation and coagulation. In addition, if you stop printing about 3~4 hours in the middle of printing work, the head nozzles of printer could be naturally clogged. To prevent of this situation, worker should implement cleaning and checking head nozzle before hands. When the nozzle is clogged in the middle of work, running a head cleaning mode can clear the clogged nozzle. Yet, large amount of waste inks which are passed clogged nozzle will be remained after cleaning. It would be very nice that ink companies take the waste ink back by green marketing, but none of them are doing it currently. The purpose of this research is that making a black water-based recycle ink by waste inks which are left of nozzle clogging or passed expiration date. This recycle ink will improved working environment and reduce cost of disposing waste inks. Furthermore, it is very environment friendly and economical. It is called a recycle ink which is water-based black ink made by waste inks.

A Study for Improving the Durability of Print Heads in Binder Jet 3D Printers Method (바인더 젯 3D 프린터의 프린팅 헤드 내구성 향상을 위한 연구)

  • Jung-Chul Hwang;Tae-Sung Kim
    • Journal of the Korea Safety Management & Science
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    • v.25 no.2
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    • pp.153-158
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    • 2023
  • This research was conducted to reduce the defect rate caused by nozzle clogging of printing heads used in binder jet 3D printers. The binder jet 3D printing technology may adhere to the printing head nozzle by dispersing powder due to mechanical operation such as transferring the printing head and supplying powder, and may cause nozzle clogging by natural curing at the nozzle end depending on the type of binder used. To solve this problem, this study created a cleaning module exclusively for printing heads to check whether the durability of printing heads is improved through analysis of printing results before and after using the cleaning module. To this end, this research used a thermal bubble jet printing head, and the used powder was studied using gypsum powder.

Effect of Internal Flow inside Recirculation Chamber Nozzle for Automative Head Lamp on Cleaning Spray (자동차 헤드램프 세척용 재순환 챔버 노즐의 내부유동이 분무장에 미치는 영향)

  • Shin, J.H.;Lee, I.C.;Kang, Y.S.;Kim, J.H.;Koo, J.S.;Koo, J.Y.
    • Journal of ILASS-Korea
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    • v.16 no.2
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    • pp.90-96
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    • 2011
  • Atomized liquid jets from the washing nozzle which configured with recirculation chamber for cleaning hot-zone area are accelerated and impinged on the head lamp surface. Cleaning efficiency of head lamp can be increased with injecting washing fluids into the hot-zone area. Experimental and numerical studies with various design parameters were executed to reveal the relations between internal geometry and internal flow in the washing nozzle. Spray structures were fitted with each of the head lamp surfaces and spray nozzles were optimized to the spray pattern. The recirculation chamber induces a recirculation flow and can be decreased the pressures perturbation inside the chamber. Orifice determines the mass flow rate. When the diameter of orifice is excessively large, it showed an unstable spray pattern. As a nozzle exit angle increases, density distributions are separated with two section. Also, as a protrusion length of nozzle exit increases, spray patterns are spread into a large area and density distributions showed unstable trend.

Application Study of $CO_2$ Snow Cleaning for Cleaning of Foreign Matter and Corrosion Products on Iron Artifacts ($CO_2$ Snow Cleaning 적용 철제유물 표면 이물질 제거 연구)

  • Lee, Eun-Ji;Cho, Nam-Chul;Lee, Jong-Myong;Yu, Jae-Eun
    • Journal of Conservation Science
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    • v.27 no.3
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    • pp.333-344
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    • 2011
  • Cleaning of foreign matter and corrosion products on surface among conservation treatment of iron artifacts is an important part for looking up a original form. The sand blaster is the most popular equipment when it removes the foreign matter and corrosion products on iron artifacts surface. Current foreign matter and corrosion products equipment, which mostly uses, is sand blaster. Glass dust which sprayed from sand blaster is harmful and causing environmental pollution. In order to solve these problems, we investigated the $CO_2$ snow cleaning that use a eco-friendly equipment to apply for cleaning foreign matter and corrosion products on surface of iron artifacts. It examined by using sand blaster and $CO_2$ snow cleaning to aged steel coupon and iron artifacts. In case of aged steel coupon, the result showed that the sand blaster and $CO_2$ snow cleaning methods were similar to the degrees of cleaning foreign matter and corrosion products, through surface roughness, color measurement and SEM. $CO_2$ snow cleaning applied to aged steel coupons weren't worn out the surface in comparison with sand blaster by SEM. When applied to the iron artifacts, power nozzle of the $CO_2$ snow cleaning was an excellent cleaning effect that surface wern't worn out in comparison with sand blaster. And, it showed that internal structure change of metal was no found before and after cleaning by X-ray radiography. Consequently, we confirmed that cleaning of the sand blaster and power nozzle of $CO_2$ snow cleaning were similar to the effect. But, it's very careful to use this method because of high outlet pressure of power nozzle for applying to the iron artifacts. As a result of experiments, it could be found that the cleaning methods should be selected depending on internal state of the artifacts.